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Crash of a Cessna 560 Citation V near Staunton: 4 killed

Date & Time: Jun 4, 2023 at 1525 LT
Type of aircraft:
Operator:
Registration:
N611VG
Flight Phase:
Flight Type:
Survivors:
No
Site:
Schedule:
Elizabethton - Ronkonkoma
MSN:
560-0091
YOM:
1990
Crew on board:
1
Crew fatalities:
Pax on board:
3
Pax fatalities:
Other fatalities:
Total fatalities:
4
Circumstances:
The airplane departed Elizabethton Airport in Tennessee on a private flight to Ronkonkoma-Long Island-McArthur Field (Islip), New York. Approaching the destination, the airplane did not initiate a descent but an almost 180 turn and continued to the southwest. As there was no radio contact with the pilot anymore and as it was approaching the Washington DC area, ATC informed the authorities about the situation and two F-16 fighters were dispatched. The military pilots were unable to establish any contact with the crew. Flying at an altitude of 34,000 feet, the Cessna entered a right turn then an uncontrolled descent and spiraled to the ground before crashing in a wooded and hilly terrain located near Staunton, Virginia, some 600 km southwest from the destination airport. All four occupants were killed.
Probable cause:
Failure of the cabin pressurization system suspected.

Crash of a Beechcraft B200 Super King Air in Cape Girardeau

Date & Time: Feb 2, 2007 at 0930 LT
Registration:
N777AJ
Flight Phase:
Survivors:
Yes
Schedule:
Rogers - Staunton
MSN:
BB-1638
YOM:
1998
Crew on board:
2
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
4048
Captain / Total hours on type:
110.00
Copilot / Total flying hours:
2806
Copilot / Total hours on type:
28
Aircraft flight hours:
1834
Circumstances:
The airplane was operated by a company pilot. A noncompany pilot, who had not attended or completed a training course or received a checkout for Raytheon Aircraft Company Beech King Air 200 airplanes, was asked by the pilot to accompany him on the flight so that the noncompany pilot could accumulate flight time. The flight only required one pilot. While the airplane was in cruise flight (27,000 feet mean sea level), the cockpit voice recorder (CVR) recorded the sound of the windshield fracturing. The CVR transcript indicated that the company pilot was not in the cockpit when the windshield fractured because he was emptying trash in the cabin. This action showed poor judgment considering the noncompany pilot was not qualified in the airplane. Although the windshield stayed in place, the company pilot stated that “within seconds” after it fractured, he depressurized the airplane because he was unsure about the windshield’s “integrity.” However, the Beech King Air Airplane Flight Manual (AFM) states to maintain cabin pressurization in the event of a fractured windshield and further states that the airplane can continue flight for up to 25 hours with the windshield fractured. During the on-scene examinations, an unapproved document (not derived from the AFM) that contained several checklists was found on the airplane. The company pilot stated that he used this document and that it “came with the airplane.” The document did not include a checklist addressing a cracked or shattered windshield. The company pilot most likely was not aware that the airplane should not have been depressurized nor that it could operate for 25 hours after the fracture occurred and, therefore, that the fractured windshield did not present an in-flight emergency. The CVR transcript revealed that, after depressurizing the airplane, the pilots attempted to use the oxygen masks but were unable to receive any oxygen. (The pilots most likely did not turn the oxygen on once they needed it because they either forgot as a result of the emergency or because they did not have time to do so before they lost consciousness.) According to the company pilot, during his preflight inspection of the airplane, the oxygen system was functional. He stated that, after the inspection, he turned the oxygen system ready switch to the OFF position because he wanted to “save” the oxygen, which was not in accordance with the Before Start checklist in the AFM. Post accident functional testing of the oxygen system revealed normal operation. The unapproved checklists document did not include the instruction to leave the oxygen system on. Regardless, the pilot stated that he knew the approved checklist stated to leave the oxygen system on but that he still chose to turn it off. The pilot exhibited poor judgment by using an unapproved, incomplete checklists document and by knowingly deviating from approved preflight procedures. About 1 minute after the pilots tried to get oxygen, the CVR recorded the last comment by either pilot. For about the next 7 minutes until it stopped recording, the CVR recorded the sounds of increased engine propeller noise, the landing gear and overspeed warning horns, and altitude alerts indicating that the airplane had entered an uncontrolled descent. (The CVR’s 4-g impact switch was found in the open position during the on-scene examination, indicating that the airplane experienced at least 4 acceleration of gravity forces.) Further, a plot of two radar data points, recorded after the last pilot comment, showed that the airplane descended from 25,400 feet to 7,800 feet within 5 minutes. Shortly thereafter, the pilots regained consciousness and recovered from the uncontrolled descent. The airplane was substantially damaged by the acceleration forces incurred during the uncontrolled descent and subsequent recovery. Examination of the windshield revealed that a dense network of fractures was located on the inner glass ply; however, the windshield did not lose significant pieces of glass and maintained its structural integrity. Therefore, the fractures did not preclude safe continued flight. Post accident examinations revealed evidence that the fracture initiated due to a design deficiency in the glass. The manufacturer redesigned the windshield in 2001 (the accident airplane was manufactured in 1998), and no known similar fractures have occurred in the newly designed windshield. The manufacturer chose not to issue a service bulletin for a retrofit of the new windshield design in airplanes manufactured before 2001 because the fracture of one pane of glass is not a safety-of-flight issue.
Probable cause:
The company pilot’s poor judgment before and during the flight, including turning the oxygen system ready switch to the OFF position after he conducted the preflight inspection and using an unapproved checklist, which did not provide guidance for a fractured windshield and resulted in his depressurizing the airplane. Members Hersman and Sumwalt did not approve this probable cause. Member Hersman filed a dissenting statement, with which Member Sumwalt concurred. The statement can be found in the public docket for this accident.
Final Report:

Crash of a Beechcraft B99 Airliner near Staunton: 14 killed

Date & Time: Sep 23, 1985 at 1020 LT
Type of aircraft:
Operator:
Registration:
N339HA
Survivors:
No
Site:
Schedule:
Baltimore - Staunton
MSN:
U-156
YOM:
1974
Flight number:
AL1517
Crew on board:
2
Crew fatalities:
Pax on board:
12
Pax fatalities:
Other fatalities:
Total fatalities:
14
Captain / Total flying hours:
3447
Captain / Total hours on type:
301.00
Copilot / Total flying hours:
3329
Copilot / Total hours on type:
119
Aircraft flight hours:
23455
Aircraft flight cycles:
41215
Circumstances:
Henson Airlines flight 1517 was cleared for an instrument approach to the Shenandoah Valley Airport, Weyers Cave, Virginia, at 0959 on September 23, 1985, after a routine flight from Baltimore-Washington International Airport, Baltimore, Maryland. Instrument meteorological conditions prevailed at Shenandoah Valley Airport. there were 12 passengers and 2 crew members aboard the scheduled domestic passenger flight operating under 14 CFR 135. Radar service was terminated at 1003. The crew of flight 1517 subsequently contacted the Henson station agent and Shenandoah unicom. The last recorded radar return was at 1011, at which time the airplane was east of the localizer course at 2,700 feet mean sea level and on a magnetic track of about 075°. At 1014 the pilot said, '..we're showing a little west of course...' and at 1015 he asked if he was east of course. At 1017, the controller suggested a missed approach if the airplane was not established on the localizer course. There was no response from the crew of flight 1517 whose last recorded transmission was at 1016. The wreckage of flight 1517 was located about 1842 approximately six miles east of the airport. Both crew members and all 12 passengers were fatally injured.
Probable cause:
The probable cause of this accident was a navigational error by the flightcrew resulting from their use of the incorrect navigational facility and their failure to adequately monitor the flight instruments.
Factors which contributed to the flightcrew's errors were:
- The non standardized navigational radio systems installed in the airline's Beech 99 fleet,
- Intra cockpit communications difficulties associated with high ambient noise levels in the airplane,
- Inadequate training of the pilots by the airline,
- The first officer's limited multi engine and instrument flying experience,
- The pilots' limited experience in their positions in the Beechcraft 99,
- Stress inducing events in the lives of the pilots.
Also contributing to the accident was the inadequate surveillance of the airline by the Federal Aviation Administration which failed to detect the deficiencies which led to the accident.
Final Report: