Crash of a Boeing 737-222 in Charlotte

Date & Time: Oct 25, 1986 at 2008 LT
Type of aircraft:
Operator:
Registration:
N752N
Survivors:
Yes
Schedule:
Newark - Charlotte - Myrtle Beach
MSN:
19073
YOM:
1968
Flight number:
PI467
Crew on board:
5
Crew fatalities:
Pax on board:
114
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
10000
Captain / Total hours on type:
2500.00
Copilot / Total flying hours:
4100
Copilot / Total hours on type:
500
Aircraft flight hours:
41714
Aircraft flight cycles:
59033
Circumstances:
During arrival, Piedmont flight 467 was vectored for an ILS runway 36R approach. At 2001 cdt (approximately 7 minutes before landing), all arriving flights were advised the weather was (in part): 400 feet overcast, visibility 2 miles with light rain and fog, wind from 090° at 8 knots. Runway 05/32 was out of-svc at that time. Flight 467 was vectored for right turns (from north and west) onto final approach. At 2002:42, the ATC final controller told another flight (same frequency) that there was a 20 to 25 knots right crosswind on final approach. When flight 467 was cleared for landing at 2005:36, the surface wind was reported from 100° at 4 knots. The aircraft was not configured for landing until just before touchdown and the copilot did not alert the captain of the deviation. The aircraft landed approximately 3,200 feet from the threshold and the captain was unable to stop on the wet runway. After departing the runway, the aircraft hit an ILS antenna and a culvert, then went thru a fence and stopped beside railroad tracks. Reportedly, the captain added 20 knots to approach speed for possible wind shear and delayed spoiler option after touchdown. There was evidence of hydroplaning and poor frictional quality on last 1,500 feet of runway. Three passengers received back injuries; both pilots and one flight attendant had minor injuries.
Probable cause:
The captain's failure to stabilize the approach and his failure to discontinue the approach to a landing that was conducted at an excessive speed beyond the normal touchdown point on a wet runway. Contributing to the accident was the captain's failure to optimally use the airplane decelerative devices. Also contributing to the accident was the lack of effective crew coordination during the approach. Contributing to the severity of the accident was the poor frictional quality of the last 1,500 feet of the runway and the obstruction presented by a concrete culvert located 318 feet beyond the departure end of the runway.
Final Report:

Crash of a Learjet 25 in Newark: 2 killed

Date & Time: Mar 30, 1983 at 0514 LT
Type of aircraft:
Registration:
N51CA
Flight Type:
Survivors:
No
Schedule:
Chicago - Newark
MSN:
25-030
YOM:
1969
Flight number:
CA27
Crew on board:
2
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
2
Captain / Total flying hours:
5100
Captain / Total hours on type:
1600.00
Copilot / Total flying hours:
4112
Copilot / Total hours on type:
1488
Aircraft flight hours:
5750
Circumstances:
The aircraft was on a night check courier flight. During arrival, the indicated airspeed was well above the legal limit of 250 knots for flight below 10,000 feet. Runway 04R was selected for landing after the crew were advised that their original choice (runway 11) was noise sensitive. They were advised not to descend below 2,000 feet until on final approach. The turn to final was completed about one mile from the runway at an altitude of approximately 700 feet. A steep (5°) final approach was flown with an estimated 1,000 fpm rate of descent. On landing, the aircraft bounced, banked/turned to the right, then it hit the ground, right wing first and burned. An exam of the wreckage revealed the aircraft was configured with the gear extended, the flaps down 20° and the spoilers retracted. No evidence of a preimpact part failure or malfunction was found. The trim was set for a heavy right wing and the fuel switches were set to x-feed fuel. Toxicological checks showed that both pilots had used or been exposed to marijuana and had CO2 in their blood from smoking; use of medication (phenylpropanolamine) by copilot. Evidence of possible fatigue/stress to both. Both pilots were killed.
Probable cause:
The probable causes of this accident were:
- Loss of control following ground contact,
- An unstabilized approach,
- Impairment of the flightcrew judgment, decision making, and flying abilities by a combination of physiological and psychological factors.
Final Report:

Crash of a Douglas DC-10-30CF in Boston: 2 killed

Date & Time: Jan 23, 1982 at 1936 LT
Type of aircraft:
Operator:
Registration:
N113WA
Survivors:
Yes
Schedule:
Oakland - Newark - Boston
MSN:
47821/320
YOM:
1980
Flight number:
WO30H
Crew on board:
12
Crew fatalities:
Pax on board:
200
Pax fatalities:
Other fatalities:
Total fatalities:
2
Captain / Total flying hours:
18091
Captain / Total hours on type:
1969.00
Copilot / Total flying hours:
8600
Aircraft flight hours:
6327
Circumstances:
Following a non-precision instrument approach to runway 15R at Boston-Logan International Airport, the airplane touched down about 2,800 feet beyond the displaced threshold of the 9,191-foot usable part of the runway. About 1936:40, the airplane veered to avoid the approach light pier at the departure end of the runway and slid into the shallow water of Boston Harbor. The nose section separated from the fuselage in the impact after the airplane dropped from the shore embankment. Of the 212 persons on board, 2 persons are missing and presumed dead. The other persons onboard evacuated the airplane safely, some with injuries.
Probable cause:
The minimal braking effectiveness on the ice-covered runway; the failure of the Boston-Logan International Airport management to exercise maximum efforts to assess the condition of the runway to assure continued safety of landing operations; the failure of air traffic control to transmit the most recent pilot reports of braking action to the pilot of Flight 30H; and the captain's decision to accept and maintain an excessive airspeed derived from the auto throttle speed control system during the landing approach which caused the aircraft to land about 2,800 feet beyond the runway's displaced threshold. Contributing to the accident were the inadequacy of the present system of reports to convey reliable braking effectiveness information and the absence of provisions in the Federal Aviation Regulations to require:
- Airport management to measure the slipperiness of the runways using standardized procedures and to use standardized criteria in evaluating and reporting braking effectiveness and in making decisions to close runways.
- Operators to provide flight crews and other personnel with information necessary to correlate braking effectiveness on contaminated runways with aircraft stopping distances, and
- Extended minimum runway lengths for landing on runways which adequately take into consideration the reduction of braking effectiveness due to ice and snow.
Final Report:

Crash of a Gulfstream GII in Burlington

Date & Time: Feb 22, 1976 at 1504 LT
Type of aircraft:
Operator:
Registration:
N397F
Survivors:
Yes
Schedule:
Newark - Burlington
MSN:
72
YOM:
1969
Crew on board:
3
Crew fatalities:
Pax on board:
1
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
4744
Captain / Total hours on type:
754.00
Circumstances:
On final approach, during the last segment, the airplane was unstable and rolled right and left. This caused the right wing to struck the runway surface then the left wing. The aircraft cartwheeled and came to rest. While all four occupants escaped uninjured, the aircraft was damaged beyond repair.
Probable cause:
Improper operation of flight controls caused the aircraft to cartwheel on landing. The following contributing factors were reported:
- Unfavorable wind conditions,
- Snow showers.
Final Report:

Crash of a Cessna 411 in Burlington: 4 killed

Date & Time: Dec 15, 1972 at 2006 LT
Type of aircraft:
Operator:
Registration:
N111DS
Flight Type:
Survivors:
No
Schedule:
Newark - Burlington
MSN:
411-0042
YOM:
1964
Crew on board:
1
Crew fatalities:
Pax on board:
3
Pax fatalities:
Other fatalities:
Total fatalities:
4
Captain / Total flying hours:
950
Circumstances:
While on an NDB approach to Burlington Airport by night, the pilot descended below the MDA when the twin engine airplane hit tree tops, stalled and crashed in flames in a wooded area located in Winooski, about 1,5 mile short of runway 15. The airplane was destroyed by a post crash fire and all four occupants have been killed.
Probable cause:
Improper IFR operation on part of the pilot. The following factors were reported:
- Low ceiling,
- Snow falls,
- High obstructions,
- Visibility below minimums,
- Hit trees approximately one mile from outer marker during a NDB approach.
Final Report:

Crassh of an Howard 350 in Philadelphia

Date & Time: Oct 15, 1972 at 1127 LT
Operator:
Registration:
N361MC
Survivors:
Yes
Schedule:
Newark – Philadelphia
MSN:
5275
YOM:
1943
Crew on board:
2
Crew fatalities:
Pax on board:
6
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
3768
Captain / Total hours on type:
68.00
Circumstances:
After touchdown at Philadelphia-Intl Airport, the crew inadvertently retracted the gear. The twin engine airplane sank on its belly and slid for several yards before coming to rest in flames. All eight occupants escaped uninjured while the aircraft was partially destroyed by a post crash fire that was caused by the rupture of a fuel tank in the left wing.
Probable cause:
The pilot inadvertently retracted the gear after landing. Left wing tank ruptured.
Final Report:

Crash of a Beechcraft E18S in Newark: 2 killed

Date & Time: Sep 23, 1972 at 0018 LT
Type of aircraft:
Operator:
Registration:
N107T
Flight Phase:
Flight Type:
Survivors:
No
Schedule:
Newark - Providence
MSN:
BA-122
YOM:
1956
Crew on board:
2
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
2
Captain / Total flying hours:
4850
Captain / Total hours on type:
62.00
Circumstances:
Shortly after takeoff, while climbing by night, one of the engine lost power. The twin engine airplane lost height and crashed in flames on a railroad track located near the airport. The aircraft was destroyed by impact forces and a post crash fire and both occupants were killed.
Probable cause:
Loss of control after takeoff due to a loss of power on one engine. The following factors were reported:
- Failure of the exhaust system: external supercharger,
- Material failure,
- The pilot-in-command failed to maintain flying speed,
- The crew failed to follow the approved procedures,
- Improper emergency procedures,
- Partial loss of power on one engine,
- Broken pieces of ball bearings from impeller shaft found in inertia coupling.
Final Report:

Crash of a Rockwell Aero Commander 560A in East Greenwich: 1 killed

Date & Time: Nov 22, 1971 at 0915 LT
Registration:
N87K
Survivors:
Yes
Schedule:
Chatham - Newark
MSN:
560-314
YOM:
1956
Crew on board:
2
Crew fatalities:
Pax on board:
4
Pax fatalities:
Other fatalities:
Total fatalities:
1
Captain / Total flying hours:
5000
Captain / Total hours on type:
1300.00
Circumstances:
While in cruising altitude on a flight from Chatham to Newark, the captain informed ATC about the failure of the left engine and was cleared to divert to the nearest airport located in East Greenwich, east Rhode Island. Unable to maintain a safe altitude, the crew attempted an emergency landing when the aircraft stalled and crashed in a field. A passenger was killed while five other occupants were injured.
Probable cause:
Inadequate preflight preparation and/or planning on part of the pilot-in-command. The following factors were reported:
- Improper operation of powerplant and powerplant controls,
- Improper operation or failed to use the anti-icing/deicing equipment,
- Conditions conducive to carburetor system icing,
- Icing conditions including sleet and freezing rain,
- Low ceiling and snow,
- Partial loss of power on one engine,
- Complete engine failure on one engine,
- Left engine lost power, propeller feathered. Unable to maintain safe altitude.
Final Report:

Crash of a Cessna 402 in Newark: 4 killed

Date & Time: Mar 18, 1970 at 1934 LT
Type of aircraft:
Operator:
Registration:
N3218Q
Survivors:
No
Schedule:
Sherbrooke - Newark
MSN:
402-0018
YOM:
1967
Crew on board:
1
Crew fatalities:
Pax on board:
3
Pax fatalities:
Other fatalities:
Total fatalities:
4
Captain / Total flying hours:
10461
Captain / Total hours on type:
83.00
Circumstances:
The pilot initiated the approach to Newark Airport in marginal weather conditions (heavy rain falls). On final, he failed to realize his altitude was insufficient when the airplane crashed onto a natural gas storage tank located in Elizabeth, few miles short of runway 04L threshold. The aircraft was totally destroyed and all four occupants were killed.
Probable cause:
Ground collision during initial approach caused by the combination of the following factors:
- The pilot-in-command failed to follow the approved procedures,
- Improper IFR operation on part of the pilot-in-command,
- Instruments misread or failed to read,
- Obstructions to vision,
- Rain,
- No second pilot on board,
- Descended below glide slope on an ILS approach to runway 04L.
Final Report:

Crash of a De Havilland DHC-6 Twin Otter 200 in New York: 3 killed

Date & Time: Jul 15, 1969 at 0657 LT
Operator:
Registration:
N558MA
Flight Phase:
Survivors:
Yes
Schedule:
New York - Newark
MSN:
175
YOM:
1968
Flight number:
NY901
Crew on board:
3
Crew fatalities:
Pax on board:
11
Pax fatalities:
Other fatalities:
Total fatalities:
3
Captain / Total flying hours:
12110
Captain / Total hours on type:
180.00
Circumstances:
As the crew was 12 minutes behind the schedule, he decided to start the takeoff procedure from an intersection and the departure was precipitated despite ATC warned the crew about the recent takeoff of a Boeing 707 from the same runway. Just after liftoff, while in initial climb, the airplane became unstable then stalled and crashed. Both pilots and a passenger were killed while 11 other occupants were injured, some of them seriously.
Probable cause:
It was determined that the crew lost control of the airplane due to wake turbulences caused by a Boeing 707 that just took off from the same runway. The crew failed to consider the warning from ATC.
Final Report: