Crash of a Convair CV-340-35 in Midland

Date & Time: Mar 16, 1954 at 0838 LT
Type of aircraft:
Operator:
Registration:
N90853
Flight Phase:
Survivors:
Yes
Schedule:
El Paso – Midland – Kansas City
MSN:
44
YOM:
1953
Flight number:
CO046
Location:
Crew on board:
3
Crew fatalities:
Pax on board:
8
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
11038
Captain / Total hours on type:
620.00
Copilot / Total flying hours:
2742
Copilot / Total hours on type:
659
Aircraft flight hours:
3099
Circumstances:
At 0833 Trip 46 was cleared to Runway 10 for takeoff. At this time the aircraft carried 585 gallons of fuel and was loaded to a gross takeoff weight of 36,345 pounds which was 10,655 pounds less than the maximum allowable. The load was properly distributed so that the center of gravity of the aircraft was within the approved limits. A pre-takeoff check was conducted adjacent to Runway 10 at which time the propellers, engines and instruments gave normal Indications. A part of this check included moving the control column fore and aft and turning the wheel left and right in order to check the control system for freedom of movement and full travel. At 0838 the flight was cleared for takeoff which was made using normal takeoff power. Immediately after becoming airborne the crew noted a slight vibration which was attributed to an unbalanced condition of the spinning main landing gear wheels. Captain Persing applied brakes during the landing gear retraction to eliminate this vibration; however, it not only continued but rapidly increased in severity. The aircraft reached an altitude of approximately 75 feet, the highest attained, and was near the airport boundary when the vibration stopped with a sudden jolt and the aircraft assumed a nose-down attitude. The first officer immediately sensing the situation joined the captain and both exerted their entire strength applying back pressure to their respective control columns to keep the aircraft from plunging into the ground. The captain quickly reduced power; however, the nose-down pressure could not be completely overcome. The first officer used nose-up trim control in an effort to relieve the nose-down pressure; this action had no appreciable effect and during the last attempt the trim tab control wheel appeared to be stuck. The captain established a shallow left turn with the thought of returning to the airport and continued the turn about 45 degrees from the takeoff heading. As air speed decreased power was momentarily increased whereupon it became evident to the crew that using power sufficient to maintain flight resulted in an insurmountable nose-down pressure. The captain therefore decided to make a wheels-up landing straight ahead. Close to the ground the first officer closed the throttles and the captain pulled the electrical crash bar. Contact with the ground followed with the aircraft in a near-level attitude and at approximately 100 m.p.h. Although the passengers and crew received injuries of varying degrees, they were able to get out of the aircraft unassisted in an orderly manner. The evacuation was mainly through the rear service door (emergency exit) and was accomplished in about 30 seconds. There was no fire.
Probable cause:
The Board determines that the probable cause of this accident was loss of control due to a failure of the right elevator trim tab push-pull rod caused by a reversed installation of the right elevator trim tab idler as a result of the carrier’s reliance on the Manufacturers Illustrated Parts Catalog as a maintenance reference. The following findings were reported:
- Immediately following a normal takeoff the right elevator trim tab push-pull rod failed and the stub end became wedged, holding the trim tab in a full-up or aircraft nose-down position,
- The trim tab position resulted in the crew being unable to control the aircraft and a wheels-up landing resulted,
- The push-pull rod failed as a result of excessive stresses caused by interference resulting from a reversed idler installation,
- The right elevator trim tab assembly as removed, reinstalled, inspected and functionally checked by company maintenance personnel 14:40 flight hours prior to the accident,
- Correct positioning of the right idler component could not be determined from the Maintenance Manual figure, 7.4.101, which the carrier considered appropriate for the installation,
- The Manufacturers Illustrated Parts Catalog was used in accordance with company policy as an installation reference to determine the idler position,
- Under conventional interpretation of the appropriate exploded diagram of the Parts Catalog, the idler was installed in reverse,
- The Illustrated Parts Catalog was not intended and should not have been used as a maintenance reference.
Final Report:

Crash of a Douglas TB-26C-35-DT Invader near Midland: 5 killed

Date & Time: Oct 23, 1949
Type of aircraft:
Operator:
Registration:
44-35442
Flight Phase:
Flight Type:
Survivors:
No
MSN:
28721
YOM:
1944
Location:
Crew on board:
5
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
5
Circumstances:
Crashed in unknown circumstances 20 miles southeast of Midland, killing all five crew members.

Crash of a Douglas C-47-DL in Sweetwater: 25 killed

Date & Time: Apr 20, 1945 at 0640 LT
Operator:
Registration:
41-18451
Flight Phase:
Flight Type:
Survivors:
No
Schedule:
Midland – Nashville
MSN:
4513
YOM:
1942
Crew on board:
3
Crew fatalities:
Pax on board:
22
Pax fatalities:
Other fatalities:
Total fatalities:
25
Circumstances:
Enroute, the crew encountered poor weather conditions with thunderstorm activity and turbulence. While cruising at an estimated altitude of 5,000 feet, the twin engine aircraft went out of control, dove into the ground and crashed in a field located 4 miles south of Sweetwater. All 25 occupants were killed.
Crew:
2nd Lt Richard Britton Arnold,
1st Lt James A. Bailey,
1st Lt David L. Bennell,
Sgt Robert H. Blaess,
Cpl Daniel B. Boone,
Pfc Grady O. Boyd,
Pfc Kenneth W. Carlson,
Cpl Vincent R. DiSterano,
Sgt William T. Downey,
Sgt William H. Edwards,
1st Lt Leonard K. Epperly,
Pvt Robert L. Fuller,
Sgt Robert C. Goodenough,
Pfc William A. Green,
Cpl D. E. Jennelle,
1st Lt Samuel Kamrass,
Pfc James D. McLaughlin,
1st Lt Chester W. Mrozek,
1st Lt Frank A. Prete,
Cpt John R. Rawls,
1st Lt Joseph A. Scieszka,
Cpl Myron V. Testement,
1st Lt James H. Wallace Jr.,
Cpl Virgil E. Walston,
1st Lt Robert L. West.
Probable cause:
It appears that severe turbulence caused the elevators and stabilizers to fail in flight. In such condition, the aircraft was unflyable.

Crash of a Beechcraft AT-11 Kansan in Midland

Date & Time: Mar 11, 1944
Type of aircraft:
Operator:
Registration:
41-27495
Flight Type:
Survivors:
Yes
Schedule:
Midland - Midland
MSN:
1340
YOM:
1942
Location:
Crew on board:
3
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
Belly landed for unknown reason. No casualties.

Crash of a Beechcraft AT-11 Kansan in Midland: 4 killed

Date & Time: Mar 23, 1942
Type of aircraft:
Operator:
Registration:
41-9535
Flight Phase:
Flight Type:
Survivors:
No
MSN:
961
YOM:
1942
Location:
Crew on board:
4
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
4
Circumstances:
The twin engine airplane crashed in Midland following a mid-air collision. All four crew members were killed.
Crew:
2nd Lt Robert W. Ingle,
2nd Lt William M. Bolton,
Avc William T. Hallstead,
Avc Oliver R. Harja.

Crash of a Fokker Y1C-14 in Midland

Date & Time: May 5, 1933
Type of aircraft:
Operator:
Registration:
31-396
Flight Type:
Survivors:
Yes
MSN:
1430
YOM:
1931
Location:
Crew on board:
0
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
The airplane suffered a landing accident and was damaged beyond repair. There were no casualties.