Crash of a Learjet 35A at Hohn AFB: 2 killed

Date & Time: May 15, 2023 at 1247 LT
Type of aircraft:
Operator:
Registration:
D-CGFQ
Flight Phase:
Flight Type:
Survivors:
No
Schedule:
Hohn - Hohn
MSN:
35-676
YOM:
1993
Country:
Region:
Crew on board:
2
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
2
Captain / Total flying hours:
11955
Captain / Total hours on type:
8083.00
Copilot / Total flying hours:
10349
Copilot / Total hours on type:
6265
Aircraft flight hours:
9846
Aircraft flight cycles:
6739
Circumstances:
On the day of the occurrence, six Learjet flight crews of the operator involved planned to take off almost at the same time from Hohn Military Airport to different missions. The airplane involved was the third to take off. Two pilots were on board of the Learjet 35A. The Pilot Flying (PF) sat in the left-hand seat and the Pilot Monitoring (PM) in the right. It was planned to fly from Hohn to Wunstorf Military Airport and conduct several instrument approaches for training purposes of the local air traffic control personnel. At the same time, the flight was to be used as proficiency check for the pilot in the left-hand seat for his type and instrument rating for Learjet 20/30. According to the Cockpit Voice Recorder (CVR) recording, the pilots completed the Before Starting Engine checklist prior to starting the engines. A Yaw Damper check and a so-called Full Travel check of the flight controls were performed, among other things. At 1224 hrs, the right engine was started; at 1226 hrs, the left. At 1237 hrs, while still on taxiway C3, the take-off emergency briefing was performed with the words: „[…] when airborn keine [no] Items ausser [except] gear below 500 ft, continue climb, in real life accelerate to V2 plus 30, Klappen [flaps] rein, slight climb weiter auf [to] […]“. At 1238 hrs, another Learjet received take-off clearance with simulated engine failure from the Tower. That flight crew asked over the radio if the single engine take-off was approved and the Tower once again acknowledged it. After the take-off of that Learjet, the flight crew taxied with the airplane involved on the runway to Ramp 1, turned and waited for the clearance to line up on runway 26. At 1244 hrs, the flight crew received the instruction to roll on to runway 26 and wait. They completed the Line-up check and the Before Take-off check. They planned to take-off with flaps 8° and engine full thrust with N1 of 96.6%. After they had received take-off clearance at about 1247 hrs, the airplane accelerated and took off at 1247:34 hrs, according to witnesses in the area of taxiway C3, and entered climb. According to the CVR recording, after take-off the PF instructed the PM to retract the landing gear and engage the Yaw Damper. At 1247:39 hrs, the PM responded with: “Vorab verlierst du simuliert das rechte Triebwerk (in advance, you will lose the right engine)“, the PF acknowledged it by saying: “Copy, gear up“. Then the thrust of the right engine reduced, the left engine maintained the set take-off thrust. At that time, indicated speed was about 160 kt, according to the FDR. At 1247:44 hrs, the PF instructed: “Damper on”. At 1247:45 hrs, the PM answered “Jawohl (yes)”, almost at the same time the PF said quietly: “Oh shit“. At 1247:44 hrs, the PF called out loud several times: “Fuck” and at 1247:54 hrs the PM several times “Shit”. At 1247:55 hrs, the last recording was the landing gear warning generated by the airplane: “Too low“. From the PM’s announcement about the simulated engine failure at 1247:39 hrs until the impact, Hohn Tower transmitted traffic information regarding two Tornado aircraft in the vicinity and instructed the frequency change to Hohn Radar. Witnesses observed that the airplane performed a sort of snap roll and then crashed to the ground at the end of the runway. On impact, an explosive fireball occurred. The pilots suffered fatal injuries and the airplane was destroyed.
Probable cause:
The accident, loss of control of the airplane, was the result of an untimely or significantly too low rudder deflection to correct the asymmetric thrust after initiation of a simulated engine failure. The large yaw angle resulted in a stall of the vertical tail and on the wing and an uncontrolled roll of the airplane. It was not possible to determine without doubt the reason for the untimely or significantly too low rudder deflection.
Final Report:

Crash of a Learjet 35A near Olsberg: 2 killed

Date & Time: Jun 23, 2014 at 1438 LT
Type of aircraft:
Operator:
Registration:
D-CGFI
Flight Phase:
Flight Type:
Survivors:
No
Schedule:
Hohn - Hohn
MSN:
35A-612
YOM:
1985
Country:
Region:
Crew on board:
2
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
2
Captain / Total flying hours:
7505
Captain / Total hours on type:
3554.00
Copilot / Total flying hours:
3560
Copilot / Total hours on type:
745
Aircraft flight hours:
8259
Circumstances:
On 23 June 2014 at 1522 hrs the Bundeswehr (German Armed Forces) informed the German Federal Bureau of Aircraft Accident Investigation (BFU) that a collision involving a civil Learjet 35A (Learjet) and a German Air Force Eurofighter had occurred during aerial target demonstrations. According to the Law Relating to the Investigation into Accidents and Incidents Associated with the Operation of Civil Aircraft (FlUUG) accidents and incidents involving civil and military aircraft will be investigated under the responsibility of the BFU. The BFU immediately deployed a team of five investigators to the accident site. The BFU was supported by the Directorate Aviation Safety of the German Armed Forces (AbtFlSichhBw). The Learjet, operated by a civil operator specializing in manned aerial target demonstrations, had taken off at Hohn Airport and had initially been flying with a southern heading in accordance with Instrument Flight Rules (IFR). At the time of the accident the Learjet had changed to Visual Flight Rules (VFR) and was flying in airspace E with a northern heading. A formation consisting of two Eurofighters had taken off from Nörvenich Air Base with the order to conduct a so-called Renegade mission, i.e. the unknown civil aircraft had to be intercepted, identified, and accompanied to a military airport. After the collision with a Eurofighter, the Learjet crashed to the ground. The pilots of the Learjet suffered fatal injuries and the aircraft was destroyed. The pilot of the Eurofighter could land the severely damaged airplane at Nörvenich Air Base.
Probable cause:
The causes of the flight accident were:
Immediate Causes:
- During positioning for the intervention the collision risk due to unexpected manoeuvres of the intercepted airplane was not sufficiently taken into consideration.
- The Learjet crew did not take into account the risks due to possible limitations of the field of vision and the distraction by using the computer when deciding about the task distribution. Due to insufficient situational awareness during the intervention, the Learjet crew continued the turn with an excessive bank angle despite the loss of visual contact with the Eurofighter flying at the inside of the turn.
Systemic Causes:
- The operator had not specified in detail how the crew should distribute their tasks during Renegade exercises.
- Neither the operator commissioned to conduct the aerial target demonstration nor the Air Force had sufficiently described the Renegade training nor had a commensurate risk analysis been done.
Final Report:

Crash of a Transall C-160D near Chania: 42 killed

Date & Time: Feb 9, 1975 at 1730 LT
Type of aircraft:
Operator:
Registration:
50+63
Flight Type:
Survivors:
No
Site:
Schedule:
Hohn - Chania
MSN:
D085
YOM:
1970
Country:
Region:
Crew on board:
5
Crew fatalities:
Pax on board:
37
Pax fatalities:
Other fatalities:
Total fatalities:
42
Circumstances:
The airplane departed Hohn Air Base in Schleswig-Holstein on a flight to Chania-Souda Airport, Greece, carrying 37 German soldiers and a crew of five who were to join a NATO contingency in Crete. The approach to Chania Airport was initiated in poor weather conditions with fog and snow falls. While descending to an altitude of 5,000 feet, the airplane struck the slope of Mt Kukules located about 24 km from the airport. The aircraft disintegrated on impact and all 42 occupants were killed.