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Crash of a Cessna 340 in Covington: 2 killed

Date & Time: Apr 21, 2022 at 1844 LT
Type of aircraft:
Operator:
Registration:
N84GR
Flight Phase:
Flight Type:
Survivors:
No
Site:
Schedule:
Covington - Covington
MSN:
340-0178
YOM:
1973
Crew on board:
2
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
2
Captain / Total flying hours:
0
Captain / Total hours on type:
0.00
Copilot / Total flying hours:
3148
Copilot / Total hours on type:
0
Aircraft flight hours:
7581
Circumstances:
The student pilot, who was the new owner of the multi-engine airplane, and a private pilot flew commercially to Lubbock, Texas, utilized a ride-hailing service to drive to Portales, New Mexico; they met with the former owner of the airplane to finalize the purchase of the airplane and flew it back to Georgia the same day. The next day, the student pilot commenced flight training with the private pilot who offered to provide flight instruction to the student pilot in the student pilot’s newly acquired multi-engine airplane, even though he did not possess a flight instructor’s rating or a multi-engine airplane rating. Radar data showed that the track of the accident airplane's route consisted of their departure airport, a midway stop, and the third leg of the flight, where it crashed during the approach to their destination airport. Witnesses observed a sharp right turn before the airplane’s spiraling descent and impact with terrain and unoccupied semi-trailers. Surveillance footage from a parking lot security camera captured the airplane in a right spiral turn just before the accident. The airplane was destroyed by impact forces and the postimpact fire. The postaccident examination of the airframe, engines, and propellers revealed no anomalies that would preclude normal engine and airplane performance. Additionally, a review of the maintenance logbook revealed that the airplane was overdue for its annual maintenance inspection; no special flight permit (ferry permit) was obtained from the Federal Aviation Administration (FAA) for its return flight to Georgia. Toxicological testing of the student pilot revealed the presence amphetamine, a prescription Schedule II controlled substance that may result in cognitive deficits that pose a risk to aviation safety; however, its effect, if any on the accident flight could not be determined. It is likely that the private pilot’s failure to maintain aircraft control was exacerbated by his lack of a multi-engine airplane rating, his lack of a flight instructor rating, and his poor decision making.
Probable cause:
The private pilot’s loss of control in flight, which resulted in a collision with terrain. Contributing to the accident was the student pilot’s decision to obtain flight instruction from the private pilot and the private pilot's insufficient qualifications to fly or to provide flight instruction in a multi-engine airplane.
Final Report:

Crash of a Boeing 727-228F in New York

Date & Time: Aug 31, 1998 at 2235 LT
Type of aircraft:
Operator:
Registration:
N722DH
Flight Type:
Survivors:
Yes
Schedule:
New York - Covington
MSN:
19861
YOM:
1969
Flight number:
DHL1165
Crew on board:
5
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
16000
Captain / Total hours on type:
5000.00
Copilot / Total flying hours:
6000
Copilot / Total hours on type:
1200
Aircraft flight hours:
50861
Circumstances:
Shortly after takeoff, the No. 2 engine failed and shutdown procedures for the No. 2 engine were accomplished. The flight crew declared an emergency and requested to return to the airport. On approach, an engine out go-around was required as ATC had instructed the flight crew of a B-747 to "position and hold" on the end of the runway. The first officer was the pilot flying. Following an uneventful touchdown, as the airplane slowed to about 80 knots, the captain took control of the airplane. Shortly thereafter, the right main landing gear (MLG) collapsed and the airplane slid to a stop on the runway. Examination of the No. 2 engine revealed that 80 percent of the main fuel pump main drive shaft was worn to the spline root. The examination also revealed that the grease used to lubricate the main drive shaft output splines was not the authorized grease specified per OHM 73-11-1 or MIL-G-81322. Additionally, the magnetic seal compression O-ring that rides on the drive gear journal outer diameter was hardened and exhibited inner diameter axial cracks. The component manufacturer indicated that the failure of the magnetic seal was the first such reported incident in 30 years; however, it agreed to review operational data from airlines to reevaluate the mean time between overhaul intervals for the seal and to recommend an inspection interval, as necessary. Examination of the right MLG revealed a fracture failure of the trunnion bearing support fitting that was caused by fatigue cracking and stress corrosion cracking.
Probable cause:
The failure of the right main landing gear caused by fatigue cracking and stress corrosion cracking of the trunnion bearing support fitting.
Final Report:

Crash of a Beechcraft G18AS in DuPage

Date & Time: Dec 4, 1991 at 0405 LT
Type of aircraft:
Operator:
Registration:
N38RM
Flight Phase:
Flight Type:
Survivors:
Yes
Schedule:
DuPage - Covington
MSN:
BA-574
YOM:
1961
Location:
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
4571
Captain / Total hours on type:
330.00
Circumstances:
The pilot stated she felt the twin engined tailwheel cargo airplane yaw to the right during takeoff. The pilot stated she applied left rudder and set differential power to correct for the perceived right hand crosswind. As the airplane lifted off, it made a sharp right turn and performed left and right banks leveling off prior to colliding with the ground. The airplane slid through security fences and a fuel supply depot before stopping. The newspaper bundle cargo moved from the two forward bays to the aft end of the cargo compartment. The newspapers were covered with plastic wrapper. The cargo compartment floor was slippery when walked upon and had traces of snow on it. According to the pilot the cargo was covered by a cargo net secured at the forward end but not at the aft end. Two cargo straps were crisscrossed over the net and secured at the aft end of the cargo load. The left throttle was found in the full forward position. The right throttle was found one inch aft of the full forward position.
Probable cause:
A result of the pilot in command's not maintaining directional control, an improper inflight decision, and improper remedial action once the loss of directional control was recognized by the pilot. Factors contributing to this accident are inadequate cargo restraints, loose cargo, and improper security of the cargo not observed by the pilot. Additional factors contributing to this accident are the inadequate standards for aircraft equipment and training provided by the company employing and operating the airplane.
Final Report:

Crash of a Beechcraft E18S in Chicago: 1 killed

Date & Time: Sep 28, 1986 at 2254 LT
Type of aircraft:
Operator:
Registration:
N101VE
Flight Type:
Survivors:
No
Site:
Schedule:
Chicago - Covington
MSN:
BA-190
YOM:
1956
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
1
Captain / Total flying hours:
6400
Captain / Total hours on type:
2059.00
Aircraft flight hours:
17743
Circumstances:
The aircraft had departed on runway 13. He was then directed to climb to 6,000 feet. Thirty seconds later he advised he had engine trouble and was returning to the airport. Shortly thereafter he advised he could not maintain altitude. The aircraft, one mile southeast of the airport, struck the roofs of two family type residences. Then struck two garages, ground impacted and struck the rear area of a third residence. An intense fire followed. Left engine had impeller failure. Propeller was pitched between low and high rpm. The pilot, sole on board, was killed.
Probable cause:
Occurrence #1: loss of engine power (total) - mech failure/malf
Phase of operation: climb - to cruise
Findings
1. (f) eng assembly, blower/impeller/integral supercharger - failure, total
2. (f) lubricating system - lack of
----------
Occurrence #2: airframe/component/system failure/malfunction
Phase of operation: descent - emergency
Findings
3. (c) propeller system/accessories, feathering system - incorrect
4. Propeller feathering - attempted - pilot in command
5. (c) propeller system/accessories, feathering system - movement restricted
----------
Occurrence #3: forced landing
Phase of operation: descent - emergency
----------
Occurrence #4: in flight collision with object
Phase of operation: descent - emergency
Findings
6. (c) object - residence
----------
Occurrence #5: in flight collision with terrain/water
Phase of operation: descent - uncontrolled
Final Report:

Crash of a Beechcraft D18S in Covington

Date & Time: Feb 14, 1977 at 2326 LT
Type of aircraft:
Registration:
N321D
Flight Phase:
Flight Type:
Survivors:
Yes
Schedule:
Covington - Columbus
MSN:
A-413
YOM:
1948
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
14136
Captain / Total hours on type:
6233.00
Circumstances:
On a slush covered runway, the pilot completed a premature liftoff. After rotation, the airplane stalled during initial climb and crashed. The aircraft was destroyed and the pilot, sole on board, was seriously injured.
Probable cause:
Stall during initial climb after the pilot completed a premature liftoff and failed to maintain flying speed. The following contributing factors were reported:
- Inadequate preflight preparation,
- Physical impairment,
- Ice/slush on runway,
- Cargo net found underneath mail,
- Pilot no feeling well.
Final Report: