Crash of a Beechcraft D18 in Charleston: 1 killed

Date & Time: May 25, 1979 at 2317 LT
Type of aircraft:
Registration:
N1812D
Flight Type:
Survivors:
No
Schedule:
Charlotte - Youngstown
MSN:
A-826
YOM:
1952
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
1
Captain / Total flying hours:
7928
Captain / Total hours on type:
1800.00
Circumstances:
While in cruising altitude on a cargo flight from Charlotte to Youngstown, the pilot reported engine problems and elected to divert to Charleston-Kanawha Airport for an emergency landing. After being cleared, he initiated the descent when the airplane went out of control and crashed in flames few miles from the airfield. The aircraft was destroyed and the pilot, sole on board, was killed.
Probable cause:
Uncontrolled collision with ground on final approach after the pilot attempted operation with known deficiencies in equipment. The following contributing factors were reported:
- Improper IFR operation,
- Lubricating system: lines, hoses, fitting,
- Oil leak,
- Pilot fatigue,
- Low ceiling,
- Forced landing off airport on land,
- Pilot departed on last leg of flight despite observing large oil leak,
- Pilot on duty since 0730LT.
Final Report:

Crash of a Beechcraft C90 King Air in Charleston: 6 killed

Date & Time: Nov 4, 1975 at 0814 LT
Type of aircraft:
Registration:
N221MJ
Flight Phase:
Survivors:
No
Schedule:
Charleston - Wilmington
MSN:
LJ-512
YOM:
1971
Crew on board:
2
Crew fatalities:
Pax on board:
4
Pax fatalities:
Other fatalities:
Total fatalities:
6
Captain / Total flying hours:
4596
Captain / Total hours on type:
3923.00
Circumstances:
At liftoff, one of the engine failed. The crew lost control of the airplane that lost height and crashed in flames in woods downhill of dirt bank. The aircraft was destroyed and all six occupants have been killed.
Probable cause:
Powerplant failure for undetermined reasons. The following contributing factors were reported.
- Delayed action in aborting takeoff.
Final Report:

Crash of a Howard 500 in Charleston

Date & Time: Jul 10, 1969 at 1948 LT
Operator:
Registration:
N320L
Survivors:
Yes
Schedule:
Washington DC – Dallas
MSN:
500-117
YOM:
1943
Crew on board:
2
Crew fatalities:
Pax on board:
5
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
7053
Captain / Total hours on type:
289.00
Circumstances:
While in cruising altitude, en route from Washington-Dulles Airport to Dallas, the crew encountered technical problems with the right engine. Decision was taken to shut down the engine and to feather the propeller. The crew was then cleared to divert to Charleston-Kanawha Airport for an emergency landing. During the final approach, the pilot supervisor interfered verbally in the process and the airplane landed 3,000 feet down the runway 23 which is 5,600 feet long. Unable to stop within the remaining distance, the airplane overran and came to rest in flames on a dirt bank. All seven occupants evacuated safely and the aircraft was destroyed.
Probable cause:
The exact cause of the powerplant failure could not be determined. However, it was reported that the pilot-in-command misjudged distance and speed upon landing.
Final Report:

Crash of a Fairchild-Hiller FH-227B in Charleston: 35 killed

Date & Time: Aug 10, 1968 at 0857 LT
Type of aircraft:
Operator:
Registration:
N712U
Survivors:
Yes
Schedule:
Cincinnati - Charleston
MSN:
557
YOM:
1967
Flight number:
PI230
Crew on board:
3
Crew fatalities:
Pax on board:
34
Pax fatalities:
Other fatalities:
Total fatalities:
35
Captain / Total flying hours:
6884
Captain / Total hours on type:
2809.00
Copilot / Total flying hours:
3722
Copilot / Total hours on type:
403
Aircraft flight hours:
2197
Circumstances:
Flight 230 was a scheduled domestic flight from Louisville, Kentucky, to Roanoke, Virginia, with en-route stops at Cincinnati, Ohio and Charleston, Kanawha County Airport, West Virginia. The flight to Cincinnati was routine. At 0805 hours eastern daylight time the flight departed Cincinnati on an IFR clearance to Charleston via Victor Airways 128 south to York, thence Victor 128 to Charleston, to maintain 9 000 ft. At 0835 hours the flight contacted the Charleston Tower to request the latest weather information, which was provided as: sky partially obscured, visibility 4 mile fog and smoke, runway 23 visibility less than 1/8 of a mile. Shortly thereafter it was cleared by the Indianapolis ARTCC to the Milton Intersection (10 miles west-northwest of the Charleston VORTAC on Victor 128) and to descend to and maintain 5 000 ft. At approximately 0841 hours the flight contacted Charleston Approach Control and reported leaving 6 000 for 5 000 ft. The controller advised the flight that radar contact had been established and instructed the flight to take a 070' heading for a vector to the holding pattern at the ILS outer marker. The latest weather was also given at this time as: sky partially obscured, visibility 4 mile, fog and smoke, runway visibility runway 23 zero, altimeter setting 29.94 in. The flight was then provided with holding instructions to be followed upon arrival over the outer marker compass locator (LOM) and was given an expected approach time of 0915 hours subject to weather conditions. At 0850 hours prior to reaching the LOM, the flight was instructed to turn right to a heading of 140°, cleared to descend to 2 400 ft and advised that the runway visibility for runway 23 had improved to seven-eighths of a mile. At 0851 hours the flight was advised that it was seven miles northeast of the outer locator, instructed to turn right to a 200' heading and cleared for an ILS approach. The flight acknowledged the clearance and it shortly thereafter was advised by the approach controller that the glide path was out of service. At 0852 hours the flight was advised that it was 5 miles from the LOM and instructed to contact Charleston Tower on 120.3 MHz. At 0853 hours radio contact with the flight was established by the tower local 'controller who cleared the flight to land. By that time the landing check had been completed by the crew and descent was established at a fairly constant rate of descent of approximately 620 ft/min. At 0854:40 hours the flight reported passing the outer marker inbound and requested the wind which was given as being 230°/4 kt. At 0855:55 hours the flight asked the tower if the approach lights and high intensity runway lights were turned all the way up and the controller replied in the affirmative, adding "a little fog right off the end there and its wide open after you get by that, it's more than a mile and a half on the runway". This was the last known radio communication from the flight. At 0856:09 hours the pilot-in-command mentioned to the co-pilot that he was going to hold the present altitude which was approximately 1 250 ft AMSL (350 ft above the elevation of runway 23 threshold). At 0856:24 hours the co-pilot informed the pilot-in-command that he had the lights in sight "down low" and asked him if he could see them. The pilot-in-command replied he had them in sight and requested landing flaps. The co-pilot then commented "I got to get to the chart right here we're likely to lose it". At 0856:42 hours the co-pilot asked the pilot-in-command if he saw the lights "there", the pilot-in-command replied in the affirmative and shortly thereafter reduced the power and 2 sec later increased it - 1 sec later the co-pilot commented "watch it". About 1 sec later the aircraft crashed. The controller observed a column of smoke rising near the approach end of the runway and immediately activated the crash siren and called for the dispatch of airport emergency equipment. The aircraft struck the steep hillside about 250 ft short of the runway threshold at an elevation of 865 ft AMSL (approximately 33 ft below the elevation of the threshold). The aircraft then careened up and over the side of the hill and on to the airport, coming to rest off the right side of runway 23. The accident occurred at 0856:53 hours during daylight. Two passengers were seriously injured while 35 other occupants were killed.
Probable cause:
The Board determined that the probable cause of this accident was an unrecognized loss of altitude orientation during the final portion of an approach into shallow, dense fog. The disorientation was caused by a rapid reduction in the ground guidance segment available to the pilot, at a point beyond which a go-around could not be successfully effected. The following findings were reported:
- The aircraft was being operated in visual meteorological conditions until approximately 6 sec before the crash, when it entered a shallow fog overlying the approach lights and the approach end of runway 23,
- Visual range in the final portion of the approach zone and over the runway 23 threshold was 500 ft or less in the fog,
- Because of the visual guidance segment available in the initial part of the approach, the pilot would have no way of judging the visual range in fog until the moment of penetration,
- Descent below MDA into the restricted visibility was permissible under present regulations.
Final Report:

Crash of a Lockheed L-049E-46 Constellation in Charleston: 2 killed

Date & Time: May 12, 1959 at 1520 LT
Operator:
Registration:
N2735A
Survivors:
Yes
Schedule:
Washington DC – Rochester – Buffalo – New York – Pittsburgh – Charleston – Atlanta
MSN:
1978
YOM:
1946
Flight number:
CA983
Crew on board:
6
Crew fatalities:
Pax on board:
38
Pax fatalities:
Other fatalities:
Total fatalities:
2
Captain / Total flying hours:
4966
Captain / Total hours on type:
408.00
Copilot / Total flying hours:
2321
Copilot / Total hours on type:
822
Aircraft flight hours:
29589
Circumstances:
Capital Airlines Flight 983 of May 12, 1959, a Constellation model L-049, N 2735A, following a landing at 1529 e.s.t., on a wet runway, was intentionally ground looped and during the maneuver skidded and slid down a steep embankment beyond the boundary of the airport at Charleston, West Virginia. One of the 38 passengers and one of the six crew members died in the fire which followed; one passenger was seriously burned amd all others on board the aircraft escaped with little or no injury; the aircraft was destroyed. The aircraft was landed within the first third of the runway and the captain said that finding braking to be ineffective, he chose to ground loop the aircraft rather than risk going down a sharp declivity at the far end of the runway. The aircraft left the runway about 600 feet from the far end. Investigation revealed operational deficiencies in the conduct of the approach and touchdown, and that crew coordination throughout the emergency was poor. Because of crew statements, the brakes were believed to have been capable of functioning in a normal manner; however, water on the runway would have permitted the aircraft to aquaplane and thus make them ineffective.
Probable cause:
The Board determines that the probable cause of this accident was the pilot's action of landing the aircraft too fast on the wet runway under conditions conducive to aquaplaning, making early deceleration impossible. An additional factor was the poor coordination of the crew throughout the approach and landing.
Final Report: