Crash of a Swearingen SA226TC Metro II in Bahía Blanca

Date & Time: Nov 27, 2001 at 0538 LT
Type of aircraft:
Operator:
Registration:
LV-WSD
Flight Type:
Survivors:
Yes
Schedule:
Buenos Aires – Bahía Blanca
MSN:
TC-237E
YOM:
1977
Country:
Crew on board:
2
Crew fatalities:
Pax on board:
1
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
8200
Captain / Total hours on type:
929.00
Copilot / Total flying hours:
2000
Copilot / Total hours on type:
40
Circumstances:
Following an uneventful flight from Buenos Aires-Ezeiza-Ministro Pistarini Airport, the crew started a night approach to Bahía Blanca-Comandante Espora Airport. The approach and landing on runway 34R were considered as normal. After touchdown, the crew started the braking procedure and the aircraft rolled for a distance of 1,200 metres when it started to deviate to the right. It veered off runway, rolled for 150 metres then lost its nose gear and came to a halt. All three occupants escaped uninjured while the aircraft was damaged beyond repair.
Probable cause:
The aircraft veered off runway after landing due to the possible combination of the following factors:
- A possible (but not confirmed) failure or malfunction of the left engine reverse thrust system,
- Crosswind close to the maximums specified in the flight manual,
- Lack of corrective actions on part of the crew who failed to identify a possible failure,
- Inappropriate use of the nosewheel steering system.
Final Report:

Crash of a Swearingen SA226TC Metro II in Shamattawa: 2 killed

Date & Time: Oct 11, 2001 at 2333 LT
Type of aircraft:
Operator:
Registration:
C-GYPA
Flight Type:
Survivors:
Yes
Schedule:
Gods Lake Narrows – Shamattawa
MSN:
TC-250
YOM:
1978
Flight number:
PAG962
Country:
Crew on board:
2
Crew fatalities:
Pax on board:
1
Pax fatalities:
Other fatalities:
Total fatalities:
2
Captain / Total flying hours:
3100
Captain / Total hours on type:
1100.00
Copilot / Total flying hours:
1200
Copilot / Total hours on type:
900
Circumstances:
Perimeter Airlines Flight PAG962, a Fairchild SA226TC (Metroliner), with two pilots and a flight nurse on board, departed Gods Lake Narrows, Manitoba, at approximately 2300 central daylight time, on a MEDEVAC flight to Shamattawa. Approaching Shamattawa, the crew began a descent to the 100 nautical mile minimum safe altitude of 2300 feet above sea level (asl) and, when clear of an overcast cloud layer at about 3000 feet asl, attempted a night, visual approach to Runway 01. The aircraft was too high and too fast on final approach and the crew elected to carry out a missed approach. Approximately 30 seconds after the power was increased, at 2333, the aircraft flew into trees slightly to the left of the runway centreline and about 2600 feet from the departure end of Runway 01. The aircraft was equipped with a cockpit voice recorder (CVR) that indicated the crew were in control of the aircraft; they did not express any concern prior to impact. The aircraft broke apart along a wreckage trail of about 850 feet. Only the cabin aft of the cockpit retained some structural integrity. The captain and first officer were fatally injured on impact. The flight nurse was seriously injured but was able to exit the wreckage of the cabin. A post-crash fire was confined to the wings which had separated from the cabin and cockpit wreckage.
Probable cause:
Findings as to Causes and Contributing Factors:
1. The aircraft was flown into terrain during an overshoot because the required climb angle was not set and maintained to ensure a positive rate of climb.
2. During the go-around, conditions were present for somatogravic illusion, which most likely led to the captain losing situational awareness.
3. The first officer did not monitor the aircraft instruments during a critical stage of flight; it is possible that he was affected by somatogravic illusion and/or distracted by the non-directional
beacon to the extent that he lost situational awareness.
Other Findings:
1. The absence of approach aids likely decreased the crew=s ability to fly an approach from which a landing could be executed safely.
2. The company standard operating procedures (SOPs) did not define how positive rate is to be determined.
Final Report:

Crash of a Swearingen SA226TC Metro II in Fort Wayne: 1 killed

Date & Time: Nov 9, 2000 at 0123 LT
Type of aircraft:
Operator:
Registration:
N731AC
Flight Phase:
Flight Type:
Survivors:
No
Schedule:
Fort Wayne – Milwaukee
MSN:
TC-255
YOM:
1978
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
1
Captain / Total flying hours:
2870
Captain / Total hours on type:
75.00
Aircraft flight hours:
20885
Circumstances:
The airplane was destroyed on impact with trees and terrain after takeoff. A post-impact fire ensued. A courier stated that he put 14 cases and 5 bags into the airplane and that "everything took place as it normally does." A witness stated, "I heard a very low flying aircraft come directly over my house. ... It sounded very revved up like a chainsaw cutting through a tree at high speed." The accident airplane's radar returns, as depicted on a chart, exhibited a horseshoe shaped flight path. That chart showed that the airplane made a left climbing turn to a maximum altitude of 2,479 feet. That chart showed the airplane in a descending left turn after that maximum recorded altitude was attained. The operator reported the pilot had flown about 75 hours in the same make and model airplane and had flown about 190 hours in the last 90 days. The weather was: Wind 090 degrees at 7 knots; visibility 1 statute mile; present weather light rain, mist; sky condition overcast 200 feet; temperature 9 degrees C; dew point 9 degrees C. No pre-impact engine anomalies were found. NTSB's Materials Laboratory Division examined the annunciator panel and recovered light assemblies and stated, "Item '29' was a light assembly with an identification cover indicating that it was the '[Right-hand] AC BUS' light. Examination of the filaments in the two installed bulbs revealed that one had been stretched, deformed and fractured and the other had been stretched and deformed." The airplane manufacturer stated that the airplane's left-hand and right-hand attitude gyros are powered by the 115-volt alternating current essential bus. Two inverters are installed and one inverter is used at a time as selected by the inverter select switch. The inverter select switch is located on the right hand switch panel. The airplane was not equipped with a backup attitude gyro and was not required to be equipped with one. The airplane was certified with a minimum flight crew of one pilot. Subsequent to the accident, the operator transitioned "from the single pilot operation of our Fairchild Metroliner to the inclusion of a First Officer."
Probable cause:
The indicated failure of the right hand AC bus during takeoff with low ceiling. The factors were the low ceiling, night, and the excessive workload the pilot experienced on takeoff with an electrical failure without a second in command.
Final Report:

Crash of a Swearingen SA226TC Metro II in Bocas del Toro

Date & Time: May 10, 2000 at 1009 LT
Type of aircraft:
Operator:
Registration:
HP-1364MAM
Survivors:
Yes
MSN:
TC-324
YOM:
1980
Country:
Crew on board:
2
Crew fatalities:
Pax on board:
6
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
Upon landing at Bocas del Toro, in unclear circumstances, the aircraft went out of control and veered off runway. It lost its undercarriage and came to rest in a sugarcane field. All eight occupants escaped uninjured while the aircraft was damaged beyond repair.

Crash of a Swearingen SA226AC Metro II in Río Gallegos

Date & Time: Nov 23, 1998 at 1445 LT
Type of aircraft:
Registration:
LV-WDV
Survivors:
Yes
Schedule:
Lago Argentino - Río Gallegos
MSN:
TC-271
YOM:
1978
Country:
Crew on board:
2
Crew fatalities:
Pax on board:
5
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
After takeoff from Lago Argentino Airport, a red warning light came on in the cockpit panel, informing the crew about the incomplete retraction of the left main gear. The crew proceeded to a visual inspection and after confirmation that the left main gear was properly secured in its wheel well, the crew decided to continue to Río Gallegos. On approach, the left main gear did not deploy. After the crew failed to extend it manually, he raised the other landing gear and completed a belly landing. On short final, just prior to flare, both engines were shut down and their propellers were feathered. The aircraft landed on its belly, slid for few dozen metres and came to rest. All seven occupants escaped uninjured and the aircraft was damaged beyond repair.
Probable cause:
The crew completed a belly landing after it was impossible to extend the left main gear due to the deformation and fracture of the brace support of the gear's extension system. The following contributing factors were reported:
- The left main gear suffered previous incident,
- Marginal weather conditions with rain falls and unfavorable wind component,
- The crew started operations with know deficiencies,
- Inappropriate maintenance and technical controls.

Crash of a Swearingen SA226AC Metro II in Montreal: 11 killed

Date & Time: Jun 18, 1998 at 0728 LT
Type of aircraft:
Operator:
Registration:
C-GQAL
Survivors:
No
Schedule:
Montreal - Peterborough
MSN:
TC-233
YOM:
1977
Flight number:
PRO420
Country:
Crew on board:
2
Crew fatalities:
Pax on board:
9
Pax fatalities:
Other fatalities:
Total fatalities:
11
Captain / Total flying hours:
6515
Captain / Total hours on type:
4200.00
Copilot / Total flying hours:
2730
Copilot / Total hours on type:
93
Aircraft flight hours:
28931
Circumstances:
On the morning of 18 June 1998, Propair 420, a Fairchild-Swearingen Metro II (SA226-TC), C-GQAL, took off for an instrument flight rules flight from Dorval, Quebec, to Peterborough, Ontario. The aircraft took off from Runway 24 left (L) at 0701 eastern daylight time. During the ground acceleration phase, the aircraft was pulling to the left of the runway centreline, and the right rudder was required to maintain take-off alignment. Two minutes later, Propair 420 was cleared to climb to 16 000 feet above sea level (asl). At 0713, the crew advised the controller of a decrease in hydraulic pressure and requested to return to the departure airport, Dorval. The controller immediately gave clearance for a 180° turn and descent to 8000 feet asl. During this time, the crew indicated that, for the moment, there was no on-board emergency. The aircraft initiated its turn 70 seconds after receiving clearance. At 0713:36, something was wrong with the controls. Shortly afterward came the first perceived indication that engine trouble was developing, and the left wing overheat light illuminated about 40 seconds later. Within 30 seconds, without any apparent checklist activity, the light went out. At 0718:12, the left engine appeared to be on fire, and it was shut down. Less than one minute later, the captain took the controls. The flight controls were not responding normally: abnormal right aileron pressure was required to keep the aircraft on heading. At 0719:19, the crew advised air traffic control (ATC) that the left engine was shut down, and, in response to a second suggestion from ATC, the crew agreed to proceed to Mirabel instead of Dorval. Less than a minute and a half later, the crew informed ATC that flames were coming out of the 'engine nozzle'. Preparations were made for an emergency landing, and the emergency procedure for manually extending the landing gear was reviewed. At 0723:10, the crew informed ATC that the left engine was no longer on fire, but three and a half minutes later, they advised ATC that the fire had started again. During this time, the aircraft was getting harder to control in roll, and the aileron trim was set at the maximum. Around 0727, when the aircraft was on short final for Runway 24L, the landing gear lever was selected, but only two gear down indicator lights came on. Near the runway threshold, the left wing failed upwards. The aircraft then rotated more than 90° to the left around its longitudinal axis and crashed, inverted, on the runway. The aircraft immediately caught fire, slid 2500 feet, and came to rest on the left side the runway. When the aircraft crashed, firefighters were near the runway threshold and responded promptly. The fire was quickly brought under control, but all occupants were fatally injured.
Probable cause:
Findings as to Causes and Contributing Factors:
- The crew did not realize that the pull to the left and the extended take-off run were due to the left brakes' dragging, which led to overheating of the brake components.
- Dragging of the left brakes was most probably caused by an unidentified pressure locking factor upstream of the brakes on take-off. The dragging caused overheating and leakage, probably at one of the piston seals that retain the brake hydraulic fluid.
- When hydraulic fluid leaked onto the hot brake components, the fluid caught fire and initiated an intense fire in the left nacelle, leading to failure of the main hydraulic system.
- When the L WING OVHT light went out, the overheating problem appeared corrected; however, the fire continued to burn.
- The crew never realized that all of the problems were associated with a fire in the wheel well, and they did not realize how serious the situation was.
- The left wing was weakened by the wing/engine fire and failed, rendering the aircraft uncontrollable.
Findings as to Risk:
- Numerous previous instances of brake overheating or fire on SA226 and SA227 aircraft had the potential for equally tragic consequences. Not all crews flying this type of aircraft are aware of its history of numerous brake overheating or fire problems.
- The aircraft flight manual and the emergency procedures checklist provide no information on the possibility of brake overheating, precautions to prevent brake overheating, the symptoms that could indicate brake problems, or actions to take if overheated brakes are suspected.
- More stringent fire-blocking requirements would have retarded combustion of the seats, reducing the fire risk to the aircraft occupants.
- A mixture of the two types of hydraulic fluid lowered the temperature at which the fluid would ignite, that is, below the flashpoint of pure MIL-H-83282 fluid.
- The aircraft maintenance manual indicated that the two hydraulic fluids were compatible but did not mention that mixing them would reduce the fire resistance of the fluid.
Other Findings:
- The master cylinders were not all of the same part number, resulting in complex linkage and master cylinder adjustments, complicated overall brake system functioning, and difficult troubleshooting of the braking system. However, there was no indication that this circumstance caused residual brake pressure.
- The latest recommended master cylinders are required to be used only with specific brake assembly part numbers, thereby simplifying adjustments, functioning, and troubleshooting.
- Although the emergency checklist for overheating in the wing required extending the landing gear, the crew did not do this because the wing overheat light went out before the crew initiated the checklist.
- The effect of the fire in the wheel well made it difficult to move the ailerons, but the exact cause of the difficulty was not determined.
Final Report: