Crash of a Beechcraft B200 King Air off Dutch Harbor

Date & Time: Jan 16, 2020 at 0806 LT
Operator:
Registration:
N547LM
Flight Phase:
Flight Type:
Survivors:
Yes
Schedule:
Dutch Harbor - Adak
MSN:
BB-1642
YOM:
1998
Crew on board:
1
Crew fatalities:
Pax on board:
2
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
6470
Captain / Total hours on type:
756.00
Aircraft flight hours:
7058
Circumstances:
According to the pilot, when the airplane’s airspeed reached about 90 knots during the takeoff roll, he applied back pressure to the control yoke to initiate the takeoff and noted a brief positive rate of climb followed by a sinking sensation. The airspeed rapidly decayed, and the stall warning horn sounded. To correct for the decaying airspeed, he lowered the nose then pulled back on the airplane’s control yoke and leveled the wings just before impacting the ocean. The pilot stated there were no pre accident mechanical malfunctions or anomalies that would have precluded normal operation. Wind about the time of the accident was recorded as 110º downwind of the airplane at 15 knots gusting to 28 knots. The passengers recalled that the pilot’s preflight briefing mentioned the downwind takeoff but included no discussion of the potential effect of the wind conditions on the takeoff. The airplane’s estimated gross weight at the time of the accident was about 769.6 pounds over its approved maximum gross weight, and the airplane’s estimated center of gravity was about 8.24 inches beyond the approved aft limit at its maximum gross weight. It is likely that the pilot’s decision to takeoff downwind and operate the airplane over the maximum gross weight with an aft center of gravity led to the aerodynamic stall during takeoff and loss of control. Downwind takeoffs result in higher groundspeeds and increase takeoff distance. While excessive aircraft weight increases the takeoff distance and stability, and an aft center of gravity decreases controllability. Several instances of the operator’s noncompliance with its operational procedures and risk mitigations were discovered during the investigation, including two overweight flights, inaccurate and missing information on aircraft flight logs, and the accident pilot’s failure to complete a flight risk assessment for the accident flight. The operator had a safety management system (SMS) in place at the time of the accident that required active monitoring of its systems and processes to ensure compliance with internal and external requirements. However, the discrepancies noted with several flights, including the accident flight, indicate that the operator’s SMS program was inadequate to actively monitor, identify, and mitigate hazards and deficiencies.
Probable cause:
The pilot’s improper decision to takeoff downwind and to load the airplane beyond its allowable gross weight and center of gravity limits, which resulted in an aerodynamic stall and loss of control. Contributing to the accident was the inadequacy of the operator’s safety management system to actively monitor, identify, and mitigate hazards and deficiencies.
Final Report:

Crash of a Piper PA-31-350 Navajo Chieftain near Cooper Landing: 3 killed

Date & Time: Nov 29, 2019 at 1911 LT
Operator:
Registration:
N4087G
Flight Phase:
Flight Type:
Survivors:
No
Site:
Schedule:
Anchorage – Seward
MSN:
31-8152127
YOM:
1981
Flight number:
SVX36
Crew on board:
1
Crew fatalities:
Pax on board:
2
Pax fatalities:
Other fatalities:
Total fatalities:
3
Captain / Total flying hours:
35000
Captain / Total hours on type:
1200.00
Aircraft flight hours:
5502
Circumstances:
On November 29, 2019, about 1911 Alaska standard time, a Piper PA-31-350 airplane, N4087G, was destroyed by impact and postcrash fire when it collided with mountainous terrain about 15 miles west of Cooper Landing, Alaska. The three occupants; the airline transport pilot, a flight nurse, and the flight paramedic were fatally injured. The airplane was operated by Fly 4 You Inc., doing business as Security Aviation, as a Title 14 Code of Federal Regulations Part 135 visual flight rules air ambulance flight. Dark night visual meteorological conditions existed at the departure and destination locations and company flight following procedures were in effect. The flight departed Ted Stevens International Airport (PANC), Anchorage, Alaska, about 1848, destined for Seward Airport (PAWD), Seward, Alaska. Dispatch records indicated that, on November 29, Providence Seward Medical Center emergency clinic personnel contacted multiple air ambulance companies with a "weather check" for possible air ambulance transportation of a patient from Seward to Anchorage. The first company contacted was Guardian Flight, who declined the flight at 1624 due to limited daylight hours. The second company, LifeMed Alaska, declined the flight at 1637 due to weather. The third and final company contacted for the flight was Medevac Alaska. Their dispatch officer was not notified of the previous declined flight requests and forwarded the request to Security Aviation, who is their sole air charter provider. At 1731 Security Aviation accepted the flight, and Medevac Alaska flight SVX36 was staffed with a nurse and paramedic. A preliminary review of archived Federal Aviation Administration (FAA) radar and automatic dependent surveillance (ADS-B) data revealed that the accident airplane departed PANC and flew south about 3,000 ft mean sea level (msl) toward the Sterling Highway. The airplane was then observed descending to 2,200 ft msl while flying a right racetrack pattern before flying into the valley toward Cooper Landing. The last data point indicated that at 1911:14 the airplane was over the west end of Jean Lake at 2,100 ft msl, on a 127° course, and 122 kts groundspeed. Ground witnesses who were in vehicles on the Sterling Highway near milepost 63, reported that they saw the lights of the airplane flying over the highway that night. One witness stated that he saw the airplane west of the mountains turn in a circle as it descended and then entered the valley. He observed the wings rocking back and forth and while he was looking elsewhere, he heard an explosion and observed a large fire on the mountainside. Another witness reported seeing the airplane flying low and explode when it impacted the mountain. Witnesses to the fire called 911 and observed the wreckage high on the mountainside burning for a long time after impact. The airplane was reported overdue by the chief pilot for Security Aviation and the FAA issued an alert notice (ALNOT) at 2031. The Alaska Rescue Coordination Center dispatched an MH-60 helicopter to the last known position and located the burning wreckage that was inaccessible due to high winds in the area. On December 1, 2019, the Alaska State Troopers coordinated a mountain recovery mission with Alaska Mountain Rescue Group. The wreckage was observed on the mountain at an elevation of about 1,425 ft msl in an area of steep, heavily tree-covered terrain near the southeast end of Jean Lake in the Kenai National Wildlife Refuge. The airplane was highly fragmented and burned, however all major airplane components were accounted for. Multiple large trees around the wreckage were fractured and indicated an easterly heading prior to the initial impact.

Crash of a Saab 2000 in Unalaska: 1 killed

Date & Time: Oct 17, 2019 at 1740 LT
Type of aircraft:
Operator:
Registration:
N686PA
Survivors:
Yes
Schedule:
Anchorage - Unalaska
MSN:
017
YOM:
1995
Flight number:
AS3296
Crew on board:
3
Crew fatalities:
Pax on board:
39
Pax fatalities:
Other fatalities:
Total fatalities:
1
Captain / Total flying hours:
14761
Captain / Total hours on type:
131.00
Copilot / Total flying hours:
1447
Copilot / Total hours on type:
138
Aircraft flight hours:
12617
Aircraft flight cycles:
9455
Circumstances:
On October 17, 2019, a Saab SA-2000 airplane, operated by Peninsula Aviation Services Inc. d.b.a. PenAir flight 3296, overran the end of runway 13 at Unalaska Airport (DUT), Unalaska, Alaska. The flight crew executed a go-around during the first approach to runway 13; the airplane then entered the traffic pattern for a second landing attempt on the same runway. Shortly before landing, the flight crew learned that the wind at midfield was from 300° at 24 knots, indicating that a significant tailwind would be present during the landing. Because an airplane requires more runway length to decelerate and stop when a tailwind is present during landing, a landing in the opposite direction (on runway 31) would have favored the wind at the time. However, the flight crew continued with the plan to land on runway 13. Our postaccident calculations showed that, when the airplane touched down on the runway, the tailwind was 15 knots. The captain reported after the accident that the initial braking action after touchdown was normal but that, as the airplane traveled down the runway, the airplane had “zero braking” despite the application of maximum brakes. The airplane subsequently overran the end of the runway and the adjacent 300-ft runway safety area (RSA), which was designed to reduce airplane damage during an overrun, and came to rest beyond the airport property. The airplane was substantially damaged during the runway overrun; as a result, of the 3 crewmembers and 39 passengers aboard, 1 passenger sustained fatal injuries, and 1 passenger sustained serious injuries. Eight passengers sustained minor injuries, most of which occurred during the evacuation. The crewmembers and 29 passengers were not injured.
Probable cause:
The National Transportation Safety Board determines that the probable cause of this accident was the landing gear manufacturer’s incorrect wiring of the wheel speed transducer harnesses on the left main landing gear during overhaul. The incorrect wiring caused the antiskid system not to function as intended, resulting in the failure of the left outboard tire and a significant loss of the airplane’s braking ability, which led to the runway overrun.
Contributing to the accident were
1) Saab’s design of the wheel speed transducer wire harnesses, which did not consider and protect against human error during maintenance;
2) the Federal Aviation Administration’s lack of consideration of the runway safety area dimensions at Unalaska Airport during the authorization process that allowed the Saab 2000 to operate at the airport; and
3) the flight crewmembers’ inappropriate decision, due to their plan continuation bias, to land on a runway with a reported tailwind that exceeded the airplane manufacturer’s limit. The safety margin was further reduced because of PenAir’s failure to correctly apply its company-designated pilot-incommand airport qualification policy, which allowed the accident captain to operate at one of the most challenging airports in PenAir’s route system with limited experience at the airport and in the Saab 2000 airplane.
Final Report:

Crash of a Douglas C-118A Liftmaster in Candle

Date & Time: Aug 1, 2019 at 1400 LT
Type of aircraft:
Operator:
Registration:
N451CE
Flight Type:
Survivors:
Yes
Schedule:
Fairbanks – Candle
MSN:
43712/358
YOM:
1953
Location:
Crew on board:
3
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
9910
Captain / Total hours on type:
147.00
Copilot / Total flying hours:
8316
Copilot / Total hours on type:
69
Aircraft flight hours:
42037
Circumstances:
The flight crew was landing the transport-category airplane at a remote, gravel-covered runway. According to the captain, the terrain on the approach to the runway sloped down toward the approach end, which positioned the airplane close to terrain during the final stages of the approach. A video recorded by a bystander showed that while the airplane was on short final approach, it flew low on the glidepath and dragged its landing gear through vegetation near the approach end of the runway. The video showed that, just before the main landing gear wheels reached the runway threshold, the right main landing wheel impacted a dirt and rock berm. The captain said that to keep the airplane from veering to the right, he placed the No. 1 and No. 2 engine propellers in reverse pitch. The flight engineer applied asymmetric reverse thrust to help correct for the right turning tendency, and the airplane tracked straight for about 2,000 ft. The video then showed that the right main landing gear assembly separated, and the airplane continued straight down the runway before veering to the right, exiting the runway, and spinning about 180°, resulting in substantial damage to the fuselage. On-site examination of the runway revealed several 4-ft piles of rocks and dirt at the runway threshold, which is likely what the right main landing wheel impacted. Given that the airplane landing gear struck vegetation and rocks on the approach to the runway, it is likely that they were below the proper glidepath for the approach. The crew stated there were no preaccident mechanical malfunctions or anomalies that would have precluded normal operation.
Probable cause:
The pilot's failure to maintain an adequate glidepath during the approach, which resulted in the airplane impacting rocks and dirt at the runway threshold, a separation of the right main landing gear, and a loss of directional control.
Final Report:

Crash of a De Havilland DHC-2 Beaver off Seldovia: 1 killed

Date & Time: Jul 19, 2019 at 1010 LT
Type of aircraft:
Operator:
Registration:
N68083
Flight Phase:
Survivors:
Yes
Schedule:
Seldovia – Anchorage
MSN:
1254
YOM:
1958
Location:
Crew on board:
1
Crew fatalities:
Pax on board:
6
Pax fatalities:
Other fatalities:
Total fatalities:
1
Captain / Total flying hours:
2689
Captain / Total hours on type:
150.00
Aircraft flight hours:
29448
Circumstances:
The pilot stated that, during takeoff in the float-equipped airplane, he saw the left float begin to move into his peripheral vision from the left cockpit window and the airplane began to yaw to the left. The left wing subsequently impacted the water and the airplane nosed over, separating the right wing from the fuselage. The passengers consistently reported choppy water conditions at the time of the accident; one passenger reported that white caps were visible on the ocean waves in the distance. The passengers said that, during the takeoff, the airplane impacted a swell or wave and nosed over abruptly, and the cabin rapidly filled with water. Examination of the float assembly revealed fractures in the left front flying wire attachment fitting and the right rear flying wire attachment strap and hole elongation in the left rear flying wire attachment fitting. Additionally, the bolts attaching the two left flying wire attachment fittings to the left float were bent, and the two flying wires that had been attached to the fractured attachment fitting and attachment strap were buckled. While some areas of corrosion were observed on the fractured left forward fitting, the total area of corrosion was a small percentage of the total cross-section, and the remainder of the fracture and associated deformation of the lug was consistent with ductile overstress fracture. Similar areas of corrosion were also observed on each of the intact flying wire attachment fittings. Post-accident testing completed by the float manufacturer revealed that buckling of flying wires similar to that observed on the accident airplane was only reproduced at strap and fitting failure loads above 9,000 pounds force; the design specification load was 3,453 pounds of force. This indicates that the small amount of corrosion present on the fractured flying wire attachment fitting did not reduce its loadcarrying capability below the design specification load of 3,453 pounds of force, and that both the flying wire attachment fitting and flying wire attachment strap fractured due to overload. Therefore, it is likely that the accident airplane floats were subject to forces that exceeded their design limitations, resulting in overload of the flying wires attached to the left float. It is also likely that, given the lack of damage on either float, the force was due to impact with an ocean wave or swell and not by striking an object.
Probable cause:
The airplane's floats impact with an ocean wave or swell, which exceeded the design load specifications of the flying wire assemblies and resulted in a partial separation of the float assemblies.
Final Report:

Crash of a Cessna 208B Grand Caravan in Bethel

Date & Time: Jul 8, 2019 at 1505 LT
Type of aircraft:
Operator:
Registration:
N9448B
Survivors:
Yes
Schedule:
Newtok – Bethel
MSN:
208B-0121
YOM:
1988
Flight number:
GV262
Location:
Crew on board:
1
Crew fatalities:
Pax on board:
5
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
2258
Captain / Total hours on type:
787.00
Aircraft flight hours:
21206
Circumstances:
The commercial pilot was conducting a visual flight rules scheduled passenger flight with five passengers. During the return leg to the company’s base airport, the pilot requested, and was given clearance to, a short gravel runway of 1,858 ft that terminated at parallel cross-runways and had inbound airplanes. The wind was reported as variable at 3 knots, and the outside air temperature was 88°F which was 25° warmer than usual. The pilot stated that he conducted a steeper than normal approach and performed a normal 30° flap landing flare; however, the airplane floated halfway down the runway. He initiated a go-around by advancing the throttle to takeoff power and retracting the flaps to 20° as the main landing gear briefly touched down. Automatic dependent surveillance-broadcast (ADS-B) data indicated that the airplane arrived 0.1 mile from the runway threshold at 149 ft above ground level (agl) and 110 knots of ground speed, which was 32 knots faster than the short field landing approach speed listed in the pilot operating handbook. A witness in the air traffic control tower (the ground controller) stated that the airplane “bled off a lot of airspeed,” during the landing attempt and climbed out in a very flat profile. The tower local controller stated that after liftoff, the airplane’s right wing dropped and the airplane appeared to be turning right into conflicting landing traffic, so he twice instructed the airplane to “left turn out immediately.” The pilot stated that he attempted to comply with the tower controller’s instruction, but when he applied left aileron, the airplane appeared to stall, rolled rapidly right, and descended in a right-wing-low attitude. It subsequently impacted the surface between runways. A postimpact fire ensued, and the pilot helped the passengers egress. The airplane was destroyed by postimpact fire. Given the evidence, it is likely that the pilot decided to land on the short runway to expedite the arrival and did not perform an appropriate short field landing approach, which resulted in excessive airspeed and altitude over the runway threshold, a long landing flare, rapid deceleration, and a self-initiated go-around from a slow airspeed. Had the pilot initiated the go-around as he approached the runway with indications of an unstable visual approach, the airspeed would have been well above stall speed, which would have allowed for the desired positive climb out on runway heading. The pilot likely attempted to comply with the tower local controller’s urgent commands to turn while the airplane was near the limit of performance (the temperature was about 25 degrees warmer than average, which would have resulted in a higher density altitude than the pilot was accustomed to and degraded aircraft and engine performance). The pilot’s maneuvering resulted in the exceedance of the critical angle-of-attack of the high wing (right wing) during the left turn, and an aerodynamic stall.
Probable cause:
The pilot’s failure to maintain adequate airspeed while maneuvering during an attempted go around, which resulted in an exceedance of the airplane's critical angle of attack and an aerodynamic stall at low altitude. Contributing to the accident, was the pilot’s decision to perform an approach to a short runway at an excessive airspeed and his late decision to perform a go-around, which resulted in a slow climb at a reduced safe margin above stall airspeed.
Final Report:

Crash of a De Havilland DHC-2 Beaver off Metlakatla: 2 killed

Date & Time: May 20, 2019 at 1556 LT
Type of aircraft:
Operator:
Registration:
N67667
Survivors:
No
Schedule:
Ketchikan – Metlakatla
MSN:
1309
YOM:
1959
Crew on board:
1
Crew fatalities:
Pax on board:
1
Pax fatalities:
Other fatalities:
Total fatalities:
2
Captain / Total flying hours:
1623
Captain / Total hours on type:
20.00
Aircraft flight hours:
29575
Circumstances:
The commercial pilot was conducting his first scheduled commuter flight from the company’s seaplane base to a nearby island seaplane base with one passenger and cargo onboard. According to company pilots, the destination harbor was prone to challenging downdrafts and changing wind conditions due to surrounding terrain. Multiple witnesses at the destination stated that the airplane made a westerly approach, and the wind was from the southeast with light chop on the water. Two witnesses reported the wings rocking left and right before touchdown. One witness stated that a wind gust pushed the tail up before the airplane landed. A different witness reported that the airplane was drifting right during the touchdown, and another witness saw the right (downwind) float submerge under water after touchdown, and the airplane nosed over as it pivoted around the right wingtip, which impacted the water. Flight track and performance data from the cockpit display units revealed that, as the airplane descended on the final approach, the wind changed from a right headwind of 6 knots to a left quartering tailwind of 8 knots before touchdown. The crosswind and tailwind components were within the airplane’s operational limitations. Examination of the airframe, engine, and associated systems revealed no evidence of mechanical malfunctions or failures that would have precluded normal operation or egress. During the final approach and descent, the pilot had various wind information available to him; the sea surface wind waves and signatures, the nearest airport observation winds, the cockpit display calculated wind, and the visual relative ground speed. Had the pilot recognized that the winds had shifted to a quartering tailwind and the airplane’s ground speed was faster than normal, he could have aborted the landing and performed another approach into the wind. Although crosswind landings were practiced during flight training, tailwind landings were not because new pilots were not expected to perform them. Although the crosswind component was well within the airplane’s limits, it is possible that combined with the higher ground speed, the inexperienced pilot was unable to counteract the lateral drift during touchdown in a rapidly shifting wind. The pilot was hired the previous month with 5 hours of seaplane experience, and he completed company-required training and competency checks less than 2 weeks before the accident. According to the chief pilot (CP), company policy was to assign newly hired pilots to tour flights while they gained experience before assigning them to commuter flights later in the season. The previous year, the CP distributed a list of each pilot’s clearances for specific types of flights and destinations; however, an updated list had not been generated for the season at the time of the accident, and the flight coordinators, who were delegated operational control for assigning pilots to flights, and station manager were unaware of the pilot’s assignment limitations. Before the flight, the flight coordinator on duty completed a company flight risk assessment that included numerical values based on flight experience levels. The total risk value for the flight was in the caution area, which required management notification before releasing the flight, due to the pilot’s lack of experience in the accident airplane make and model and with the company, and his unfamiliarity with the geographical area; however, the flight coordinator did not notify management before release because the CP had approved a tour flight with the same risk value earlier in the day. Had the CP been notified, he may not have approved of the pilot's assignment to the accident flight. The pilot's minimal operational experience in seaplane operations likely affected his situational awareness in rapidly changing wind conditions and his ability to compensate adequately for a quartering tailwind at a higher-than-normal ground speed, which resulted in a loss of control during the water landing and a subsequent nose-over.
Probable cause:
The pilot’s inadequate compensation for a quartering tailwind during a water landing, which resulted in a loss of control and subsequent nose-over. Contributing to the accident was the company’s inadequate operational control of the flight release process, which resulted in assignment of an inexperienced pilot to a commuter seaplane flight.
Final Report:

Crash of a De Havilland DHC-3T Otter in the George Inlet: 1 killed

Date & Time: May 13, 2019 at 1221 LT
Type of aircraft:
Operator:
Registration:
N959PA
Flight Phase:
Survivors:
Yes
Schedule:
Ketchikan - Ketchikan
MSN:
159
YOM:
1956
Crew on board:
1
Crew fatalities:
Pax on board:
10
Pax fatalities:
Other fatalities:
Total fatalities:
1
Captain / Total flying hours:
25000
Aircraft flight hours:
30296
Circumstances:
On May 13, 2019, about 1221 Alaska daylight time, a float-equipped de Havilland DHC-2 (Beaver) airplane, N952DB, and a float-equipped de Havilland DHC-3 (Otter) airplane, N959PA, collided in midair about 8 miles northeast of Ketchikan, Alaska. The DHC-2 pilot and four passengers sustained fatal injuries. The DHC-3 pilot sustained minor injuries, nine passengers sustained serious injuries, and one passenger sustained fatal injuries. The DHC-2 was destroyed, and the DHC-3 sustained substantial damage. The DHC-2 was registered to and operated by Mountain Air Service LLC, Ketchikan, Alaska, under the provisions of Title 14 Code of Federal Regulations (CFR) Part 135 as an on-demand sightseeing flight. The DHC-3 was registered to Pantechnicon Aviation LTD, Minden, Nevada, and operated by Venture Travel, LLC, dba Taquan Air, Ketchikan, Alaska, under the provisions of Part 135 as an on-demand sightseeing flight. Visual meteorological conditions prevailed in the area at the time of the accident. According to information provided by the operators, both airplanes had been conducting sightseeing flights to the Misty Fjords National Monument area. They were both converging on a scenic waterfall in the Mahoney Lakes area on Revillagigedo Island before returning to the Ketchikan Harbor Seaplane Base (5KE), Ketchikan, Alaska, when the accident occurred. According to recorded avionics data recovered from the DHC-3, it departed from an inlet (Rudyerd Bay) in the Misty Fjords National Monument area about 1203 and followed the inlet westward toward Point Eva and Manzanita Island. At 1209, at an altitude between 1,900 and 2,200 ft, the DHC-3 crossed the Behm Canal then turned to the southwest about 1212 in the vicinity of Lake Grace. Automatic dependent surveillance-broadcast (ADS-B) tracking data for both airplanes, which were provided by the Federal Aviation Administration (FAA), began at 1213:08 for the DHC-3, and at 1213:55 for the DHC-2. At 1217:15, the DHC-3 was about level at 4,000 ft mean sea level (msl) over Carroll Inlet on a track of 225°. The DHC-2 was 4.2 nautical miles (nm) south of the DHC-3, climbing through 2,800 ft, on a track of 255°. The DHC-3 pilot stated that, about this time, he checked his traffic display and “there were two groups of blue triangles, but not on my line. They were to the left of where I was going.” He stated that he did not observe the DHC-2 on his traffic display before the collision. The ADS-B data indicated that, about 1219, the DHC-3 started a descent from 4,000 ft, and the DHC-2 was climbing from 3,175 ft. During the next 1 minute 21 seconds, the DHC-3 continued to descend on a track between 224° and 237°, and the DHC-2 leveled out at 3,350 ft on a track of about 255°. Between 1220:21 and 1221:14, the DHC-3 made a shallow left turn to a track of 210°, then a shallow right turn back to a track of 226°. The airplanes collided at 1221:14 at an altitude of 3,350 ft, 7.4 nm northeast of 5KE. The ADS-B data for both airplanes end about the time of the collision. The DHC-2 was fractured into multiple pieces and impacted the water and terrain northeast of Mahoney Lake. Recorded avionics data for the DHC-3 indicate that at 1221:14, the DHC-3 experienced a brief upset in vertical load factor and soon after entered a right bank, reaching an attitude about 50° right wing down at 1221:19 and 27° nose down at 1221:22. The DHC-3 began descending and completed a 180° turn before impacting George Inlet at 1222:15 along a northeast track.
Probable cause:
The NTSB determines that the probable cause of this accident was the inherent limitations of the see-and-avoid concept, which prevented the two pilots from seeing the other airplane before the collision, and the absence of visual and aural alerts from both airplanes’ traffic display systems, while operating in a geographic area with a high concentration of air tour activity.
Contributing to the accident were
1) the Federal Aviation Administration’s provision of new transceivers that lacked alerting capability to Capstone Program operators without adequately mitigating the increased risk associated with the consequent loss of the previously available alerting capability and
2) the absence of a requirement for airborne traffic advisory systems with aural alerting among operators who carry passengers for hire.
Final Report:

Crash of De Havilland DHC-2 Beaver in the Goerge Inlet: 5 killed

Date & Time: May 13, 2019 at 1221 LT
Type of aircraft:
Operator:
Registration:
N952DB
Flight Phase:
Survivors:
No
Schedule:
Ketchikan - Ketchikan
MSN:
237
YOM:
1952
Crew on board:
1
Crew fatalities:
Pax on board:
4
Pax fatalities:
Other fatalities:
Total fatalities:
5
Captain / Total flying hours:
11000
Aircraft flight hours:
16452
Circumstances:
On May 13, 2019, about 1221 Alaska daylight time, a float-equipped de Havilland DHC-2 (Beaver) airplane, N952DB, and a float-equipped de Havilland DHC-3 (Otter) airplane, N959PA, collided in midair about 8 miles northeast of Ketchikan, Alaska. The DHC-2 pilot and four passengers sustained fatal injuries. The DHC-3 pilot sustained minor injuries, nine passengers sustained serious injuries, and one passenger sustained fatal injuries. The DHC-2 was destroyed, and the DHC-3 sustained substantial damage. The DHC-2 was registered to and operated by Mountain Air Service LLC, Ketchikan, Alaska, under the provisions of Title 14 Code of Federal Regulations (CFR) Part 135 as an on-demand sightseeing flight. The DHC-3 was registered to Pantechnicon Aviation LTD, Minden, Nevada, and operated by Venture Travel, LLC, dba Taquan Air, Ketchikan, Alaska, under the provisions of Part 135 as an on-demand sightseeing flight. Visual meteorological conditions prevailed in the area at the time of the accident. According to information provided by the operators, both airplanes had been conducting sightseeing flights to the Misty Fjords National Monument area. They were both converging on a scenic waterfall in the Mahoney Lakes area on Revillagigedo Island before returning to the Ketchikan Harbor Seaplane Base (5KE), Ketchikan, Alaska, when the accident occurred. According to recorded avionics data recovered from the DHC-3, it departed from an inlet (Rudyerd Bay) in the Misty Fjords National Monument area about 1203 and followed the inlet westward toward Point Eva and Manzanita Island. At 1209, at an altitude between 1,900 and 2,200 ft, the DHC-3 crossed the Behm Canal then turned to the southwest about 1212 in the vicinity of Lake Grace. Automatic dependent surveillance-broadcast (ADS-B) tracking data for both airplanes, which were provided by the Federal Aviation Administration (FAA), began at 1213:08 for the DHC-3, and at 1213:55 for the DHC-2. At 1217:15, the DHC-3 was about level at 4,000 ft mean sea level (msl) over Carroll Inlet on a track of 225°. The DHC-2 was 4.2 nautical miles (nm) south of the DHC-3, climbing through 2,800 ft, on a track of 255°. The DHC-3 pilot stated that, about this time, he checked his traffic display and “there were two groups of blue triangles, but not on my line. They were to the left of where I was going.” He stated that he did not observe the DHC-2 on his traffic display before the collision. The ADS-B data indicated that, about 1219, the DHC-3 started a descent from 4,000 ft, and the DHC-2 was climbing from 3,175 ft. During the next 1 minute 21 seconds, the DHC-3 continued to descend on a track between 224° and 237°, and the DHC-2 leveled out at 3,350 ft on a track of about 255°. Between 1220:21 and 1221:14, the DHC-3 made a shallow left turn to a track of 210°, then a shallow right turn back to a track of 226°. The airplanes collided at 1221:14 at an altitude of 3,350 ft, 7.4 nm northeast of 5KE. The ADS-B data for both airplanes end about the time of the collision. The DHC-2 was fractured into multiple pieces and impacted the water and terrain northeast of Mahoney Lake. Recorded avionics data for the DHC-3 indicate that at 1221:14, the DHC-3 experienced a brief upset in vertical load factor and soon after entered a right bank, reaching an attitude about 50° right wing down at 1221:19 and 27° nose down at 1221:22. The DHC-3 began descending and completed a 180° turn before impacting George Inlet at 1222:15 along a northeast track.
Probable cause:
The NTSB determines that the probable cause of this accident was the inherent limitations of the see-and-avoid concept, which prevented the two pilots from seeing the other airplane before the collision, and the absence of visual and aural alerts from both airplanes’ traffic display systems, while operating in a geographic area with a high concentration of air tour activity.
Contributing to the accident were
1) the Federal Aviation Administration’s provision of new transceivers that lacked alerting capability to Capstone Program operators without adequately mitigating the increased risk associated with the consequent loss of the previously available alerting capability and
2) the absence of a requirement for airborne traffic advisory systems with aural alerting among operators who carry passengers for hire.
Final Report:

Crash of a Beechcraft B200 Super King Air off Kake: 3 killed

Date & Time: Jan 29, 2019 at 1811 LT
Operator:
Registration:
N13LY
Flight Type:
Survivors:
No
Schedule:
Anchorage - Kake
MSN:
BB-1718
YOM:
2000
Location:
Crew on board:
1
Crew fatalities:
Pax on board:
2
Pax fatalities:
Other fatalities:
Total fatalities:
3
Captain / Total flying hours:
17774
Captain / Total hours on type:
1644.00
Aircraft flight hours:
5226
Circumstances:
The pilot of the medical transport flight had been cleared by the air traffic controller for the instrument approach and told by ATC to change to the advisory frequency, which the pilot acknowledged. After crossing the initial approach fix on the RNAV approach, the airplane began a gradual descent and continued northeast towards the intermediate fix. Before reaching the intermediate fix, the airplane entered a right turn and began a rapid descent, losing about 2,575 ft of altitude in 14 seconds; radar returns were then lost. A witness at the destination airport, who was scheduled to meet the accident airplane, observed the pilot-controlled runway lights illuminate. When the airplane failed to arrive, she contacted the company to inquire about the overdue airplane. The following day, debris was found floating on the surface of the ocean. About 48 days later, after an extensive underwater search, the heavily fragmented wreckage was located on the ocean floor at a depth of about 500 ft. A postaccident examination of the engines revealed contact signatures consistent with the engines developing power at the time of impact and no evidence of mechanical malfunctions or failures that would have precluded normal operation. A postaccident examination of the airframe revealed about a 10° asymmetric flap condition; however, significant impact damage was present to the flap actuator flex drive cables and flap actuators, indicating the flap actuator measurements were likely not a reliable source of preimpact flap settings. In addition, it is unlikely that a 10° asymmetric flap condition would result in a loss of control. The airplane was equipped with a total of 5 seats and 5 restraints. Of the three restraints recovered, none were buckled. The unbuckled restraints could suggest an emergency that required crewmembers to be up and moving about the cabin; however, the reason for the unbuckled restraints could not be confirmed. While the known circumstances of the accident are consistent with a loss of control event, the factual information available was limited because the wreckage in its entirety was not recovered, the CVR recording did not contain the accident flight, no non-volatile memory was recovered from the accident airplane, and no autopsy or toxicology of the pilot could be performed; therefore, the reason for the loss of control could not be determined. Due to the limited factual information that was available, without a working CVR there is little we know about this accident.
Probable cause:
A loss of control for reasons that could not be determined based on the available information.
Final Report: