Crash of a Britten-Norman BN-2A Trislander III near Port Vila

Date & Time: Jan 3, 1990
Type of aircraft:
Operator:
Registration:
YJ-RV3
Flight Phase:
Survivors:
Yes
Schedule:
Lenakel - Port-Vila
MSN:
349
YOM:
1973
Country:
Region:
Crew on board:
0
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
While approaching Port Vila following an uneventful flight from Lenakel, all three engines failed due to fuel exhaustion. The pilot attempted an emergency landing when the aircraft struck coconut trees and crashed in a pasture. The aircraft was damaged beyond repair and all occupants were rescued.
Probable cause:
Engine failure caused by fuel exhaustion. It is believed that the fuel selector was positioned on the main fuel tanks which were empty at the time of the accident while fuel remained in the auxiliary tanks.

Crash of a Cessna 207 Skywagon in Milford Sound: 7 killed

Date & Time: Dec 30, 1989 at 1532 LT
Operator:
Registration:
ZK-DQF
Flight Phase:
Survivors:
No
Site:
Schedule:
Milford Sound - Queenstown
MSN:
207-0053
YOM:
1969
Country:
Region:
Crew on board:
1
Crew fatalities:
Pax on board:
6
Pax fatalities:
Other fatalities:
Total fatalities:
7
Captain / Total flying hours:
455
Captain / Total hours on type:
4.00
Circumstances:
Two Cessna 207 Skywagon of Air Fiordland (ZK-DQF) and Milford Sound Scenic Flights (ZK-DAX) were engaged in a charter flight from Milford Sound to Queenstown, carrying Japanese tourists. On board ZK-DQF were six passengers and one pilot and four passengers and one pilot on board ZK-DAX. En route, while cruising over the Milford Sound area, both aircraft collided. While the pilot of ZK-DAX was able to perform an emergency landing, ZK-DQF entered a dive and crashed, killing all seven occupants. All five people on board ZK-DAX were rescued but both aircraft were destroyed.
Probable cause:
The mid-air collision occurred because neither pilot saw the other aircraft in time. Causal factors were the pilot's restricted cockpit vision, a lack of pilot awareness to maintain an effective look-out; the unnecessarily high density of traffic and the unplanned merging of two streams of aircraft after a weather deterioration necessitated a change in route after departure.
Final Report:

Crash of a Cessna 207 Skywagon in Milford Sound

Date & Time: Dec 30, 1989 at 1532 LT
Operator:
Registration:
ZK-DAX
Flight Phase:
Survivors:
Yes
Site:
Schedule:
Milford Sound - Queenstown
MSN:
207-0131
YOM:
1969
Country:
Region:
Crew on board:
1
Crew fatalities:
Pax on board:
4
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
1120
Captain / Total hours on type:
718.00
Circumstances:
Two Cessna 207 Skywagon of Air Fiordland (ZK-DQF) and Milford Sound Scenic Flights (ZK-DAX) were engaged in a charter flight from Milford Sound to Queenstown, carrying Japanese tourists. On board ZK-DQF were six passengers and one pilot and four passengers and one pilot on board ZK-DAX. En route, while cruising over the Milford Sound area, both aircraft collided. While the pilot of ZK-DAX was able to perform an emergency landing, ZK-DQF entered a dive and crashed, killing all seven occupants. All five people on board ZK-DAX were rescued but both aircraft were destroyed.
Probable cause:
The mid-air collision occurred because neither pilot saw the other aircraft in time. Causal factors were the pilot's restricted cockpit vision, a lack of pilot awareness to maintain an effective look-out; the unnecessarily high density of traffic and the unplanned merging of two streams of aircraft after a weather deterioration necessitated a change in route after departure.
Final Report:

Crash of a Fletcher FU24-950 in Frogmore: 1 killed

Date & Time: Nov 29, 1989 at 1150 LT
Type of aircraft:
Operator:
Registration:
VH-HTB
Flight Phase:
Survivors:
No
Schedule:
Frogmore - Frogmore
MSN:
174
YOM:
1971
Country:
Region:
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
1
Circumstances:
The aircraft was engaged in superphosphate spreading operations. An aerial survey of the property had been conducted by the pilot in company with the property owner. Power poles in the valley ahead and to the left of the airstrip were marked. When operations started the wind was a light north-easterly and ambient temperature was 16° Celsius. By the time the aircraft had refuelled and was ready for the thirty-sixth flight of the day, the ambient temperature had increased to 28° Celsius and the wind direction had changed to a south-westerly. Shortly after takeoff, the aircraft was observed to sink after overflying the high-voltage power lines between the marked poles. On the next flight the aircraft was observed to make a tight left turn and fly down the valley adjacent to the left marked powerpole. On the next and final flight, the aircraft was apparently attempting to follow the track of the previous flight. While crossing the power lines south-west of the marked power pole, the aircraft's landing gear and left wing tip struck the powerlines. With the broken powerline jammed behind the left aileron washout plate, the aircraft impacted the ground 100 metres beyond the powerpole. Ground impact forces destroyed the aircraft and reduced the cockpit area to non-survivable dimensions.
Probable cause:
On-site examination of the aircraft and subsequent laboratory examination and testing of components did not reveal any pre-existing mechanical defects or abnormalities which could be considered as factors in, or contributory to, this accident. Powerline impact marks on the aircraft were consistent with the aircraft being in a left banked attitude when it struck the wire. The investigation revealed that the loader driver's truck bucket load gauge had no conversion/calibration chart, and that the aircraft was being operated in excess of the maximum allowable weight for takeoff. It is considered probable that the pilot had elected to fly down the valley, (thus taking advantage of the downslope), to compensate for a degradation of aircraft performance whilst operating overweight in the changed ambient conditions. The absence of a superphosphate trail before wire impact indicates that the pilot did not dump any of the load and was either unaware
of, or had forgotten about, the existence of powerlines to the south-west of the marked powerpole.
The following factors were considered relevant to the development of the accident:
1. The aircraft was being operated in an overweight configuration for takeoff.
2. The pilot did not adjust the takeoff weight of the aircraft to give an acceptable climb performance.
3. The pilot was unaware of, or had forgotten about, the powerlines to the south-west of the marked pole; or,
4. the pilot misjudged the clearance between the powerlines and the aircraft whilst trying to overfly them.
Final Report:

Crash of a Rockwell 500U Shrike Commander on Mt Barren Jack: 2 killed

Date & Time: Nov 18, 1989 at 1241 LT
Operator:
Registration:
VH-BMR
Flight Phase:
Survivors:
No
Site:
Schedule:
Canberra – Dalby
MSN:
500-1754-45
YOM:
1968
Country:
Region:
Crew on board:
2
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
2
Circumstances:
When the survey aircraft failed to arrive at the destination, and on expiry of the SAR time, a search was commenced. Wreckage of the aircraft was subsequently found on the eastern slope of Mt Barren Jack, to the north west of the mouth of Carrolls Creek, and on the planned track for the survey operation. Observers at the Burrinjuck reservoir near the mouth of Carrolls Creek described the weather in the accident area at the time as black clouds spilling over and obscuring the mountain tops. The aircraft collided with trees on the side of the mountain, while banked steeply to the right and in a tail low attitude. The pilot was thrown from the aircraft during the impact sequence. Medical opinion held that there was no evidence of body trauma consistent with the seat belt being fastened at the time of impact. The flight was completed on behalf of the Bureau of Mineral Resources (BMR) and both occupants were killed.
Probable cause:
Because of the destruction of the aircraft by the ensuing fire the status of the seat belt assemblies were unable to be determined. The investigation revealed that both engines were operating at high power at the time of impact. No malfunction or defect could be found with the aircraft which could have contributed to the accident. The survey task required the pilot to adhere strictly to a particular track and the target height for the flight was 500 feet above ground level while maintaining visual contact with the ground at all times. The pilot was suitably qualified to act as pilot in command of survey operations down to a height of 200 feet above ground level. The investigation concluded that the aircraft was being operated at a height substantially lower that 500 feet above ground level prior to the accident. Impact marks, wreckage and mechanical evidence suggest that the aircraft impacted terrain at a time when the pilot was attempting to carry out an evasive manoeuvre to remain clear of terrain. The reason why the aircraft was being operated at such a height and why the pilot delayed turning away from the steeply rising terrain could not be determined.
The following factors were reported:
- The pilot continued the flight into adverse weather conditions.
- The pilot flew the aircraft towards steeply rising terrain at a height substantially lower that 500 feet above ground level.
Final Report:

Crash of a Cessna 414A Chancellor near Wonthaggi

Date & Time: Oct 27, 1989 at 0833 LT
Type of aircraft:
Operator:
Registration:
VH-SDV
Flight Phase:
Flight Type:
Survivors:
Yes
Schedule:
Melbourne – Port Welshpool
MSN:
414A-0261
YOM:
1979
Country:
Region:
Crew on board:
1
Crew fatalities:
Pax on board:
6
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
The pilot reported that whilst enroute from Essendon to Wonthaggi he descended to the lowest safe altitude of 3600 feet above sea level, lowered the landing gear, reduced power and airspeed to counter the effect of turbulence and entered a holding pattern to the south south west of the Wonthaggi navigation aid. During the holding pattern the aircraft descended until it collided with trees that were 865 feet above sea level. The weather at the time included gale force winds, rain and low cloud. There were no thunderstorms or microbursts in the area, however, other aircraft reported a very low cloud base and severe turbulence. A few minutes prior to the accident ground witnesses, south south west of the accident site, reported an aircraft matching the description of VH-SDV, flying below a low, misty, ragged cloud base. There was no record of another aircraft in the area at the time. Information was available which indicated that the aircraft had descended below 3600 feet during the approach to Wonthaggi. The passengers reported that the pilot gave no indication of any problem or danger. Until the impact, they believed the aircraft was descending normally for a landing at Port Welshpool.
Probable cause:
No aircraft defects were found which may have been factors in the accident. The investigation indicates that the pilot attempted to fly under the low cloud base, in order to reach the Port Welshpool destination where weather conditions were earlier reported to have been partially sunny. Port Welshpool is not serviced by an approved navigation aid. The pilot attempted to descend below the cloud base, hoping to achieve visual flight conditions to continue to his destination.
Final Report:

Crash of a De Havilland DHC-2 Beaver in Orroroo: 1 killed

Date & Time: Sep 20, 1989 at 1222 LT
Type of aircraft:
Operator:
Registration:
VH-IDD
Flight Phase:
Survivors:
No
Schedule:
Orroroo - Orroroo
MSN:
1532
YOM:
1963
Country:
Region:
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
1
Circumstances:
The aircraft had been delayed in servicing and repair and had only been released six weeks prior to the accident. This delay had caused the operator/pilot to fall behind in his commitments and, according to some witnesses, caused him to worry about the situation. On the day of the accident, the pilot had just completed spraying a 243 hectare paddock and had landed to reload. After take-off for the new task, the pilot was seen to make an aerial inspection of the paddock before entering the first swath run. At the end of this run, the aircraft collided with a Single Wire Earth Return (SWER) powerline and crashed. It was later shown that the aircraft was in a bank to the right of about 18 degrees. The SWER line ran across one end of the paddock at an angle and on the crop side of a windmill just inside the fence which bordered the road. The line contacted the right maingear and outboard sprayboom attachment struts on the right wing. The wire broke after impact but the aircraft hit the ground heavily on the right main gear. The gear detached from the aircraft, the propeller struck the ground and the aircraft slewed around as it came to rest after some 27 metres of ground travel. The front half of the aircraft was destroyed by fire which broke out almost immediately the aircraft stopped. The pilot, sole on board, was killed.
Probable cause:
Two main hypothesis were proposed. One was that the pilot was distracted from a less than demanding task by business worries. The other was that the pilot had perceived that the SWER line was on the right of the windmill and outside the fence and therefore did not present an obstacle to his procedure turn. Neither hypothesis could be substantiated. An additional concern was the fact that the pilot had died from impact injuries in an accident that, prima facie, was survivable. Concern focused on whether the pilot had secured his harness properly and/or whether the inertia reel had failed. Detailed engineering inspection of the inertia reel by the Bureau and the manufacturer could not positively determine the mode of operation of the inertia reel. However, the post mortem report showed that the nature of injuries to the pilot, while sufficient to cause death prior to the fire, were such as to indicate that the inertia reel had probably not failed. The pilot did not see the powerline in time to avoid a collision.
Final Report:

Crash of a Piper PA-31-310 Navajo in Carnarvon

Date & Time: Aug 18, 1989 at 1856 LT
Type of aircraft:
Operator:
Registration:
VH-DEG
Flight Type:
Survivors:
Yes
Schedule:
Geraldton – Carnarvon
MSN:
31-7812098
YOM:
1978
Country:
Region:
Crew on board:
1
Crew fatalities:
Pax on board:
1
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
At approximately 1809, (23 minutes before last light) during final approach to landing at Carnarvon, the pilot noticed that the landing gear had not extended correctly. The aircraft remained in the circuit area whilst the pilot attempted to lower the landing gear using both manual and emergency methods. He also sought assistance from the company's, Perth based, duty pilot and Carnarvon based engineers. After exhausting all possible methods of lowering the gear the pilot decided to land with the landing gear and flaps retracted. The pilot rejected a landing on the sealed runways because he was apprehensive that it would cause unnecessary damage to the aircraft and could result in a fire. He considered landing in a riverbed (rejected by the Senior Operational Controller), alongside one of the sealed runways (the surface was unsuitable) and on one of the dirt strips. The pilot was offered a flare path on dirt runway 27 however, he declined and indicated that he would try to land using the available light. At 1856 (last light was at 1832) the pilot attempted a landing on runway 27. On late final approach the aircraft collided with a one and a half metre high levy bank, 270 metres short and 115 metres to the right of the threshold. The pilot was trapped in the wreckage for some time after the aircraft came to a stop. While the passenger was slightly injured, the pilot was seriously wounded.
Probable cause:
The landing gear problem arose when the left main landing gear would not lower. Examination of the aircraft revealed that both hinges fitted to the inboard landing gear door had fractured. The forward hinge had fractured as a result of fatigue and the rear hinge as a result of overload. The fatigue crack initiation had occurred at a sharp edged, prominent forging flash on the inner radius of the hinge and had grown over approximately 4000 load cycles. A similar fatigue problem had been identified on an earlier version of the hinge (part number 46653-00), however, regular inspections for fatigue cracking were discontinued when hinges with part number 47529-32 (as fitted to VH-DEG) were introduced in 1980. Similar fatigue cracking was found in the forward door hinge of another PA31 during the investigation. The fractured hinges jammed the left main landing gear mechanism and neither the normal or emergency extension systems could extend the gear. The pilot was apprehensive about wheels up landings. Much of his decision making was aimed at reducing the risk of fire and minimising the damage the aircraft would sustain during the landing. eg. Selection of a dirt runway instead of the sealed strip, landing with flaps retracted etc. During the pilot's attempts to rectify the landing gear problem, and up until the time of his touchdown, he was subjected to considerable radio transmission traffic involving questions, directions and suggestions which distracted him from his primary tasks. The pilot indicated on at least two occasions that he was ready to land, however, each time advice and questions from the ground personnel involved overrode his intentions. When the pilot was asked if he wanted a flare path on runway 27 there was still some natural light available and he was intending to land. However, by the time he was able to make his final approach it was dark and he was unable to see the ground. Studies have shown that aircrew subjected to high levels of stress can suffer skill fatigue and cognitive task saturation, which in turn can lead to a breakdown in the decision making process. It was apparent from the pilot's radio transmissions and the quality of the decisions made in the latter part of the flight that his information processing and decision making abilities had been degraded by the stress of continuous radio transmissions and continuous, and sometimes conflicting, instructions. As a result, what should have been a relatively simple wheels up landing in daylight was turned into an extremely difficult wheels up landing at night. With the landing gear retracted the aircraft's taxi and landing lights were not available to the pilot.
The following factors were considered relevant to the development of the accident:
1. Manufacturing defect. A forging flash created a stress concentration which led to fatigue cracking.
2. Inadequate inspection procedures. Previous inspection procedures introduced to disclose similar cracking were withdrawn on the introduction of later part numbered hinges.
3. Apprehension of the pilot. The pilot was apprehensive about apparently significant dangers of landing an aircraft, wheels up, on a sealed runway.
4. Inordinate interference in aircraft operations by ground based advisors. The ground advisors input overrode the pilot's decision on a number of occasions with the result that a simple exercise became very complicated.
5. Cognitive task saturation and skill fatigue. The amount of information, advice and suggestions being passed via the radio communications system overloaded the pilot decision making abilities.
6. Improper in-flight decisions. As a result of task saturation the final decision made by the pilot to attempt a night landing on an unlighted strip was incorrect.
7. The pilot did not see and therefore was unable to avoid the levy bank.
Final Report:

Crash of a Britten-Norman BN-2A-26 Islander near Milford Sound: 10 killed

Date & Time: Aug 8, 1989 at 1035 LT
Type of aircraft:
Operator:
Registration:
ZK-EVK
Flight Phase:
Survivors:
No
Site:
Schedule:
Wanaka - Milford Sound
MSN:
583
YOM:
1977
Country:
Region:
Crew on board:
1
Crew fatalities:
Pax on board:
9
Pax fatalities:
Other fatalities:
Total fatalities:
10
Captain / Total flying hours:
1063
Captain / Total hours on type:
12.00
Aircraft flight hours:
8350
Circumstances:
The twin engine aircraft was completing an on-demand scenic flight from Wanaka to Milford Sound, carrying nine tourists and one pilot. En route, in unknown circumstances, the aircraft crashed on the Blue Duck Glacier located near Milford Sound. The wreckage was found few hours later at the altitude of 5,400 feet. All 10 occupants were killed.
Probable cause:
The lack of direct evidence to account, operationally or structurally, for the manner in which the aircraft struck the mountain slope, the remoteness of the site which provided no witness observation to describe the aircraft’s flight path prior to the event and the absence of any survivor, combined to preclude a determination of the accident’s probable cause.
Final Report:

Crash of a Convair CV-580 in Auckland: 3 killed

Date & Time: Jul 31, 1989 at 2200 LT
Type of aircraft:
Operator:
Registration:
ZK-FTB
Flight Phase:
Flight Type:
Survivors:
No
Schedule:
Palmerston North – Auckland – Christchurch
MSN:
180
YOM:
1968
Flight number:
AFZ001
Country:
Region:
Crew on board:
3
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
3
Captain / Total flying hours:
3760
Captain / Total hours on type:
140.00
Copilot / Total flying hours:
1086
Copilot / Total hours on type:
6
Aircraft flight hours:
29999
Circumstances:
Flight Air Freight 1 was a scheduled night freight flight between Palmerston North, Auckland and Christchurch. The crew consisted of a training captain and two new co-pilots who were to fly alternate legs as co-pilot and observer. The co-pilot’s ADI of the Convair CV-580 in question had a known intermittent defect, but had been retained in service. The aircraft’s MEL however did not permit this flight to be undertaken with an unserviceable ADI. The aircraft nevertheless departed Palmerston North and arrived at Auckland at about 20:30. It was unloaded and reloaded with 11 pallets of cargo. On the next leg, to Christchurch, the handling pilot was to be the other co-pilot. Although she had completed her type rating on the Convair 580 this was her first line flight as a crew member. The flight was cleared to taxi to runway 23 for departure. Takeoff was commenced at 21:59. The aircraft climbed to a height of approx. 400 feet when it pitched down. It entered a gradual descent until it contacted the ground 387 m beyond the end of runway 23 and 91 m left of the extended centreline. The aircraft then crashed and broke up in the tidal waters of Manukau Harbour. The aircraft disintegrated on impact and all three crew members were killed.
Probable cause:
The probable cause of this accident was the training captain’s failure to monitor the aircraft’s climb flightpath during the critical stage of the climb after take-off.
Final Report: