Crash of a Beechcraft 1900C-1 in Karachi: 21 killed

Date & Time: Nov 5, 2010 at 0706 LT
Type of aircraft:
Operator:
Registration:
AP-BJD
Flight Phase:
Survivors:
No
Schedule:
Karachi - Bhit Shah
MSN:
UC-157
YOM:
1991
Country:
Region:
Crew on board:
2
Crew fatalities:
Pax on board:
19
Pax fatalities:
Other fatalities:
Total fatalities:
21
Captain / Total flying hours:
8114
Captain / Total hours on type:
1820.00
Copilot / Total flying hours:
1746
Copilot / Total hours on type:
1338
Aircraft flight hours:
18545
Aircraft flight cycles:
24990
Circumstances:
0C-1 aircraft Reg # AP-BJD was scheduled to fly chartered flight from Jinnah International Airport (JIAP), Karachi to Bhit Shah Oil Fields to convey 17 employees of M/s Eni company including one foreign national from Italy. The flight crew included two cockpit crew ie Captain and First Officer (FO), one JS (Air) ground crew (technician) and one Airport Security Force staff. The Mishap Aircraft (MA) took off from JIAP, Karachi at 02:04:31 UTC. The reported weather was fit for the conduct of ill-fated flight to Bhit Shah Oil Fields. After takeoff aircraft experienced Engine No 2 abnormal operation and cockpit crew decided to land back at JIAP Karachi after calling right hand downwind for runway 25R. While joining for right hand downwind for 25R the mishap aircraft could not sustain flight and crashed at a distance of around 1 nm from runway 07R beginning JIAP, Karachi. All souls (21) onboard got fatally injured as a result of aircraft ground impact and extensive post impact ground fire.
Probable cause:
Detailed investigation and analyses of the examinable evidence confirmed that the aircraft had developed some problem with its Engine No.2 (Right) immediately after takeoff which was observed by the cockpit crew as propeller feathering on its own. No concrete evidence could be found which would have led to the engine’s propeller malfunction as observed. The only probable cause of propeller feathering on its own could be the wear & tear of the beta valve leading to beta system malfunction. However, this anomaly at the most could have led to the non availability of one engine and making a safe landing with a single engine since the aircraft was capable of landing with a single engine operation. Some of the actions by the cockpit crew before takeoff and subsequent to the observed anomaly in the Engine No.2 were not according to the QRH / FCOM which aggravated the situation and resulted into the catastrophic accident.
The following factors contributed to the accident:
The aircraft accident took place as a result of combination of various factors which directly and indirectly contributed towards the causation of accident.
The primary cause of accident includes, inappropriate skill level of Captain to handle abnormal operation of engine No 2 just after takeoff, failure of cockpit crew to raise the landing gears after experiencing the engine anomaly, execution of remedial actions by FO before the attainment of minimum safe altitude of 400 ft AGL resulted in non conformance and non compliance of cockpit crew to OEM recommended procedures to handle such situations.
The lack of situational awareness and CRM failure directly contributed towards ineffective management of the flight deck by the cockpit crew.
The contributory factors include inadequate cockpit crew simulator training monitoring mechanism both at operator and CAA Pakistan levels in respect of correlation of previous / current performance and skill level of cockpit crew during the simulator training sessions along with absence of conduct of recurrent / refresher simulator training between two annual simulator checks in accordance with ICAO Annex-6 guidelines and CAA Pakistan (applicable ANOs) requirements for specific type of aircraft in a year.
Final Report:

Crash of a Piper PA-46-500TP Malibu Meridian in Port Mansfield

Date & Time: Oct 29, 2010 at 1611 LT
Registration:
N234PM
Flight Phase:
Flight Type:
Survivors:
Yes
Schedule:
Port Mansfield – Sinton
MSN:
46-97200
YOM:
2005
Crew on board:
1
Crew fatalities:
Pax on board:
2
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
3500
Captain / Total hours on type:
5.00
Aircraft flight hours:
650
Circumstances:
The pilot reported that shortly after takeoff the engine lost power momentarily, just before losing power completely. The pilot performed an emergency landing in a nearby field. The airplane sustained substantial damage during the forced landing. The airframe, engine, and engine accessories were examined. Fuel was noted at the engine, and no anomalies were revealed that would have contributed to the accident. The cause of the loss of power could not be determined.
Probable cause:
The total loss of engine power for undetermined reasons because examination of the airframe and engine did not reveal any anomalies that would have contributed to the loss of engine power.
Final Report:

Crash of a Let L-410UVP near Bukavu: 2 killed

Date & Time: Oct 21, 2010
Type of aircraft:
Operator:
Registration:
9Q-CUA
Flight Phase:
Flight Type:
Survivors:
No
Schedule:
Bukavu – Shabunda
MSN:
X0101
YOM:
1977
Location:
Region:
Crew on board:
2
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
2
Circumstances:
The aircraft was completing a cargo flight from Bukavu to Shabunda, carrying two pilots and a load of 1,500 kilos of various goods. Few minutes after takeoff from Bukavu-Kavumu Airport, while climbing, the twin engine aircraft went out of control and crashed near the village of Bugulumisa located at the border of the Kahuzi-Biega National Park. The aircraft was totally destroyed and both pilots were killed.
Probable cause:
It is believed that the accident was the consequence of an engine failure.

Crash of a Cessna 501 Citation I/SP off Coatzacoalcos: 8 killed

Date & Time: Oct 6, 2010 at 0745 LT
Type of aircraft:
Registration:
XA-TKY
Flight Phase:
Survivors:
No
Schedule:
Culiacán – Puebla – Minatitlán – Veracruz
MSN:
501-0029
YOM:
1977
Country:
Crew on board:
2
Crew fatalities:
Pax on board:
6
Pax fatalities:
Other fatalities:
Total fatalities:
8
Circumstances:
The aircraft departed Culiacán on a round trip to Veracruz with intermediate stops in Puebla and Minatitlán, carrying two pilots and six employees of the Coppel Company. One minute after takeoff from Minatitlán Airport, while in initial climb, the aircraft entered an uncontrolled descent and crashed in the sea off Coatzacoalcos. A day later, few debris were found on beaches. The main wreckage was not found and all eight occupants were killed.
Crew:
Javier Montoya,
Bernardo Estrada.
Passengers:
Salvador Leyva,
David Jurado,
Norma Torres,
Brenda Camacho,
Alejandro Quintero,
Freddy Peraza.

Crash of a Cessna 402C in Nassau: 9 killed

Date & Time: Oct 5, 2010 at 1236 LT
Type of aircraft:
Operator:
Registration:
C6-NLH
Flight Phase:
Survivors:
No
Schedule:
Nassau – Cockburn Town
MSN:
402C-0458
YOM:
1981
Country:
Crew on board:
2
Crew fatalities:
Pax on board:
7
Pax fatalities:
Other fatalities:
Total fatalities:
9
Captain / Total flying hours:
12000
Captain / Total hours on type:
10000.00
Circumstances:
On October 5, 2010 about 1636 UTC / 12:36pm Eastern Daylight Time (EDT), C6-NLH a Cessna 402C aircraft registered to Lebocruise Air Limited and operated by Acklins Blue Air Charter/Nelson Hanna crashed into lake Killarney shortly after becoming airborne from runway 14 at Lynden Pindling International Airport, Nassau, New Providence, Bahamas. The airplane sustained substantial damages by impact forces. The pilot, copilot and seven (7) passengers aboard the airplane received fatal injuries. The aircraft was on a passenger carrying flight from Lynden Pindling Intl Airport (MYNN) to Cockburn Town, San Salvador, Bahamas (MYSM). The aircraft was on a visual flight rules flight plan. Visual meteorological conditions prevailed at the time of the accident. The official notification of the accident was made to the Manager of the Flight Standards Inspectorate at Lynden Pindling Intl Airport, Nassau, N. P., Bahamas shortly thereafter. The investigation began the same day at approximately 1655 UTC upon notification of the IIC. The investigation was conducted by the Bahamas Civil Aviation Department [BCAD], Inspector Delvin R. Major (Investigator-in-Charge) of the Air Accident Investigation and Prevention Unit (AAIPU), Management of BCAD and Flight Standards Inspectorate (FSI), Airworthiness Inspectors, Operations Inspectors, Human Factors and other administrative staff. Valuable assistance was also received from the National Transportation Safety Board (NTSB), the Federal Aviation Administration (FAA) and Manufacturers of the aircraft and engine components. Three (3) Air Operator Certificate (AOC) holders at the Domestic Section of Lynden Pindling Intl Airport stated that on the day of the accident flight; one of the victims of the accident aircraft approached each of them individually at different times, requesting a quote and their availability to conduct a charter flight to Cockburn Town, San Salvador, Bahamas. Each AOC holder reported that they declined to conduct the charter because by looking at the amount of luggage and other equipment that accompanied the passengers and the size of the passengers that wanted to travel, in their estimation the combined weight appeared to be in excess of the weight that their respective aircraft (Cessna 402C and Hawker Beechcraft B100) can accommodate. After the AOC holders declined to conduct the charter, sometime thereafter, the same individual that was arranging the flight with the previous AOC holders made contact with Nelson Hanna / Acklins Blue Air Charter where arrangements were made to conduct the charter flight. The aircraft type certificate allowed for the aircraft to be operated by one (1) pilot, but the fatal flight was operated by a crew of two (2) pilots (according to eyewitness reports). The aircraft actual weight and center of gravity was unknown. As far as could be determined, the takeoff weight exceeded the maximum weight allowed of 6,850 pounds by more than 500 pounds. This excess in weight also placed the center of gravity of the aircraft outside of the safe envelope / limits for flight allowed by the manufacturer. The flight crew was given instructions by ATC to taxi from the business aviation apron (Executive Flight Support) for a takeoff on Runway 14 at intersection Foxtrot. (Intersection Foxtrot is 2,000 feet beyond the threshold of Runway 14, with a take-off run available of 9,353 feet. (Runway 14 - 11,353 feet long by 150 feet wide, see Appendix 5.15). According to eyewitness reports, from the initiation of takeoff power up to the point when the aircraft lost control white smoke was observed trailing behind the left engine of the aircraft. Eyewitnesses also reported that the take off appeared normal with gear being retracted shortly after takeoff and the aircraft seemed to be struggling to climb. The aircraft was seen at a low height, turning in a left direction over the lake as if trying to return for a landing at the airport. The bank of the aircraft changed from shallow to very steep to almost perpendicular to the ground, gears were extended and almost immediately the aircraft lost control and nose dived into the lake inverted. It cart wheeled, coming to rest upright, approximately ¼ mile from the approach end of runway 27. The aircraft came to rest on an approximate heading of 210 degrees. Eyewitness also reported hearing the engine run for a few seconds after the aircraft made contact with the water of the lake. There were no reports from the pilot to ATC of an emergency or any abnormalities with the aircraft or its systems after takeoff. The flight plan form filed for this flight listed one (1) soul on board; however, there were 7 additional occupants including a “second pilot” discovered onboard the accident flight the day of the accident. The aircraft's recovery and search for luggage, equipment and additional victims commenced shortly after the accident. This effort however, was hampered by inclement weather, rough lake conditions and darkness. On October 6th, the day after the crash, aircraft recovery continued. Family members of an additional person believed to be on board, advised the authorities that there was a ninth (9th) person on board. Search to recover any additional bodies continued but search and recovery efforts proved fruitless. On October 7th, the second day after the crash, the body of the ninth (9th) victim was found in the marshes and recovered from the southwestern end of the lake in the vicinity of where the fatal crash occurred.
Probable cause:
The following findings were identified:
1. Acklins Blue Air Charter was advertising and operating as a Bahamas air taxi operator without having undergone the certification process in contravention of Bahamas Civil Aviation (Safety) Regulations Schedule 12.
2. The airplane was issued a Certificate of Airworthiness on May 19, 2010, by the Bahamas Flight Standards Inspectorate, and was being operated by Acklins Blue Air Charter.
3. The Cessna 402C aircraft is classified in the performance Group C. This requires rapid feathering of the propeller of a failed engine and the raising of flap and the landing gear in order to achieve maximum climb performance.
4. The airplane maintenance records were not located; therefore, no determination could be made whether the airplane was being maintained in accordance with Bahamas Civil Aviation Regulations.
5. The 12,000 hour pilot and second pilot were not qualified to operate in Bahamas commercial air taxi operations.
6. No determination could be made whether the pilot or second pilot had completed required training and had accomplished a satisfactory recurrent flight check of their flying ability as required by CASR Schedule 12 and 14 for aircraft operating in commercial air transportation as well as the stipulation by the insurance policy.
7. Post-accident weight and balance calculations indicate the airplane was being operated approximately 523 pounds over maximum certificated takeoff weight (6,850 lb)
8. The pilot was advised by an air traffic controller that white smoke was trailing the left engine during takeoff; the pilot did not declare an emergency or advise the controller of any engine failure or mechanical abnormality.
9. The airplane's left engine could not produce rated shaft horsepower during takeoff.
10. Several factors contributing to the degradation of the airplane's performance and its inability to maintain flight include the wind-milling propeller, the pilot's intentional initiation of a steep turn to return to the departure airport, and his intentional lowering of the landing gear during the turn to return.
11. While turning to return, the airplane stalled, pitched nose down, and impacted in a lake.
12. The search and rescue efforts were timely and appropriate; however, the lack of accurate information on the pilot submitted flight plan delayed recovery of all victims.
13. The left propeller was not feathered.
14. The No. 2 cylinder of the left engine failed due to fatigue that originated in the root of the cylinder head thread that was engaged with the first thread on the barrel.
15. Post-accident inspection of the cockpit revealed several switches for the right engine were secured; however, no determination could be made when the switches were placed / moved in those positions.
16. No evidence of failure of the airplane's structures or flight control system contributed to the accident.
17. Existing regulations did not require the aircraft to be fitted with flight recorders. The lack of any recorded data about the aircraft's performance or the flight crew conversations deprived the investigation team of essential factual information.
18. Current Civil Aviation Department personnel and budget resources may not be sufficient to ensure that the quality of surveillance for certified as well as uncertified air carrier operations will improve.
19. Airside access procedures are inadequate at Fixed Base Operators. Access to the secure airside occurring without any check of individuals to challenge whether they have a legitimate reason for accessing the secure airside. FBO door to access airside is not secured or locked continuously; persons observed walking in and out without being challenged.
20. Flight Plan Forms are being accepted and transmitted to ATC with incomplete information. This information is vital for search and rescue purposes.
21. Weather was not a factor in the accident.
22. ATC was not a factor in the accident.
23. Currently flight plans for private flights are only required for international operations.
24. The pilot was aware of discrepancy associated with the manifold pressure reading of the left engine prior to takeoff. This discrepancy was brought to his attention by a client from the flight immediately preceding the accident flight.
25. The exact center of gravity of the accident airplane could not be calculated accurately as no indication of what seat each passenger occupied in the airplane and no indication of where luggage or equipment were placed on the aircraft could be determined. However, due to the exceedance of weight limits the aircraft was already outside the allowable center of gravity envelope developed by the manufacturer.
26. The pilot had insufficient time to prepare for the approach to runway 27 before beginning the approach. The airplane pitched up quickly into a stall, after extension of gear, recovery before ground impact was unlikely once the stall began.
27. Post accident inspection did not reveal any mechanical evidence or problems with the right hand engine.
28. The pilot's decision to return to the airfield was reasonable. Once the aircraft began to lose height a return to the airfield became impractical and a forced landing in the direction of flight should have been attempted.
29. The right propeller was never recovered from the lake.
The following causal factors were identified:
1. The left engine suffered a mechanical failure of the #2 cylinder, and therefore could not produce rated shaft horsepower. No indication of total loss of power with the left engine reported.
2. Right Engine electrical and engine control switches were found in the “OFF” position, therefore the aircraft was incapable of climbing on the power of one engine alone.
3. The excess weight above the maximum weight allowed for takeoff may have been an important factor in the aircraft's inability to gain adequate altitude after takeoff.
4. The pilot secured the right engine which was mechanically capable of producing power resulting in a total loss of thrust. He then sometime thereafter initiated a steep turn with gear down and the left engine already not developing sufficient shaft horsepower to sustain lift.
5. The pilot attempted to return to the departure airfield but lost control of the aircraft during a turn to the left.
Final Report:

Crash of a Beechcraft B100 King Air in Montmagny

Date & Time: Sep 22, 2010 at 1700 LT
Type of aircraft:
Operator:
Registration:
C-FSIK
Flight Phase:
Survivors:
Yes
Schedule:
Montmagny - Montreal
MSN:
BE-39
YOM:
1978
Country:
Crew on board:
2
Crew fatalities:
Pax on board:
4
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
4500
Captain / Total hours on type:
2500.00
Copilot / Total flying hours:
7800
Copilot / Total hours on type:
675
Circumstances:
The aircraft was operating as flight MAX100 on an instrument flight rules flight from Montmagny to Montreal/St-Hubert, Quebec, with 2 pilots and 4 passengers on board. At approximately 1700 Eastern Daylight Time, the aircraft moved into position on the threshold of 3010-foot-long runway 26 and initiated the take-off. On the rotation, at approximately 100 knots, the flight crew saw numerous birds in the last quarter of the runway. While getting airborne, the aircraft struck the birds and the left engine lost power, causing the aircraft to yaw and roll to the left. The aircraft lost altitude and touched the runway to the left of the centre line and less than 100 feet from the runway end. The take-off was aborted and the aircraft overran the runway, coming to rest in a field 885 feet from the runway end. All occupants evacuated the aircraft via the main door. There were no injuries. The aircraft was substantially damaged.
Probable cause:
Findings As To Causes and Contributing Factors:
The bird strike occurred on take-off at an altitude of less than 50 feet. Gulls were ingested in the left engine, which then lost power.
After the loss of engine power, the flight crew had difficulty controlling the aircraft. The aircraft touched the ground, forcing the pilot flying to abort the take-off when the runway remaining was insufficient to stop the aircraft, resulting in the runway overrun.
Findings As To Risks:
Although a cannon was in place, it was not working on the day of the accident, which increased the risk of a bird strike.
The presence of a goose and duck farm outside the airport perimeter but near a runway increases the risk of attracting gulls.
Operators subject to Canadian Aviation Regulations Subpart 703 are not prohibited from having an aircraft take off from a runway that is shorter than the accelerate-stop distance of that aircraft as determined from the performance diagrams. Consequently, travellers carried by these operators are exposed to the risks associated with a runway overrun when a take-off is aborted.
The absence of a CVR makes it harder to ascertain material facts. Consequently, investigations can take more time, resulting in delays which compromise public safety.
Final Report:

Crash of a Fletcher FU-24-954 in Fox Glacier: 9 killed

Date & Time: Sep 4, 2010 at 1327 LT
Type of aircraft:
Registration:
ZK-EUF
Flight Phase:
Survivors:
No
Schedule:
Fox Glacier - Fox Glacier
MSN:
281
YOM:
1981
Country:
Region:
Crew on board:
1
Crew fatalities:
Pax on board:
8
Pax fatalities:
Other fatalities:
Total fatalities:
9
Captain / Total flying hours:
4554
Captain / Total hours on type:
41.00
Circumstances:
Shortly after take off from Fox Glacier aerodrome, while climbing, aircraft stalled and crashed in flames in a paddock near the airfield. All nine occupants, the pilot and 8 skydivers, were killed. The new owner and operator of the aeroplane had not completed any weight and balance calculations on the aeroplane before it entered service, nor at any time before the accident. As a result the aeroplane was being flown outside its loading limits every time it carried a full load of 8 parachutists. On the accident flight the centre of gravity of the aeroplane was well rear of its aft limit and it became airborne at too low a speed to be controllable. The pilot was unable to regain control and the aeroplane continued to pitch up, then rolled left before striking the ground nearly vertically.
Probable cause:
Findings:
- There were no technical defects identified that may have contributed to the accident and the aeroplane was considered controllable during the take-off roll, with the engine able to deliver power during the short flight.
- The aeroplane’s centre of gravity was at least 0.122m rear of the maximum permissible limit, which created a tendency for the nose to pitch up. The most likely reason for the crash was the aeroplane being excessively out of balance. In addition, the aeroplane probably became airborne early and at too low an airspeed to prevent uncontrollable nose-up pitch.
- The aeroplane reached a pitch angle that would have made it highly improbable for the unrestrained parachutists to prevent themselves sliding back towards the tail. Any shift in weight rearward would have made the aeroplane more unstable.
- The engineering company that modified ZK-EUF for parachuting operations did not follow proper processes required by civil aviation rules and guidance. Two of the modifications had been approved for a different aircraft type, one modification belonged to another design holder and a fourth was not referred to in the aircraft maintenance logbook.
- The flight manual for ZK-EUF had not been updated to reflect the new role of the aeroplane and was limited in its usefulness to the aeroplane owner for calculating weight and balance.
- Regardless of the procedural issues with the project to modify ZK-EUF, the engineering work conducted on ZK-EUF to convert it from agricultural to parachuting operations in the standard category was by all accounts appropriately carried out.
- The weight and balance of the aeroplane, with its centre of gravity at least 0.122m outside the maximum aft limit, would have caused serious handling issues for the pilot and was the most significant factor contributing to the accident.
- ZK-EUF was 17 kg over its maximum permissible weight on the accident flight, but was still 242 kg lighter than the maximum all-up weight for which the aeroplane was certified in its previous agricultural role. Had the aeroplane not been out of balance it is considered the excess weight in itself would have been unlikely to cause the accident. Nevertheless, the pilots should have made a full weight and balance calculation before each flight.
- The aeroplane owner and their pilots did not comply with civil aviation rules and did not follow good, sound aviation practice by failing to conduct weight and balance calculations on the aeroplane. This resulted in the aeroplane being routinely flown overweight and outside the aft centre of gravity allowable limit whenever it carried 8 parachutists.
- The empty weight and balance for ZK-EUF was properly recorded in the flight manual, but the stability information in that manual had not been appropriately amended to reflect its new role of a parachute aeroplane. Nevertheless, it was still possible for the aeroplane operator to initially have calculated the weight and balance of the aeroplane for the predicted operational loads before entering the aeroplane into service.
- The aeroplane owner did not comply with civil aviation rules and did not follow good, sound aviation practice when they: used the incorrect amount of fuel reserves; removed the flight manual from the aeroplane; and did not formulate their own standard operating procedures before using the aeroplane for commercial parachuting operations.
- The Director of Civil Aviation delegated the task of assessing and overseeing major modifications to Rule Part 146 design organisations and individual holders of “inspection authorisations”. The delegations did not absolve the Director of his responsibility to monitor compliance with civil aviation rules and guidance.
Page 38 | Report 10-009
- The delegations increased the risk that unless properly managed the CAA could lose control of 2 safety-critical functions: design and inspection. The Director had not appropriately managed that risk with the current oversight programme.
- The CAA had adhered strictly to its normal practice and was acting in accordance with civil aviation rules when approving the change in airworthiness category from special to standard. However, knowing the scope, size and complexity of the modifications required to change ZK-EUF from an agricultural to a parachuting aeroplane, it should have had greater participation in the process to help ensure there were no safety implications.
- There was a flaw in the regulatory system that allowed an engineering company undertaking major modification work on an aircraft to have little or no CAA involvement by using an internal or contracted design delegation holder and a person with the inspection authorisation to oversee and sign off the work.
- The level of parachuting activity in New Zealand warranted a stronger level of regulatory oversight than had been applied in recent years.
- The CAA’s oversight and surveillance of commercial parachuting were not adequate to ensure that operators were functioning in a safe manner.
- The CAA had mechanisms through the Director’s powers under the Civil Aviation Act and his designated powers under the HSE Act to effectively regulate the parachuting industry pending the introduction of Rule Part 115.
- An alcohol and drug testing regime needs to be initiated for persons performing activities critical to flight safety, to detect and deter the use of performance-impairing substances.
- In this case the impact was not survivable and the passengers wearing safety restraints would not have prevented their deaths, but in other circumstances the wearing of safety restraints might reduce injuries and save lives.
- Safety harnesses or restraints would help to prevent passengers sliding rearward and altering the centre of gravity of the aircraft. It could not be established if this was a factor in this accident.
Final Report:

Crash of a Cessna 207A Skywagon in Tuluksak

Date & Time: Sep 3, 2010 at 1830 LT
Operator:
Registration:
N9942M
Flight Phase:
Survivors:
Yes
Schedule:
Tuluksak - Bethel
MSN:
207-0756
YOM:
1983
Location:
Crew on board:
1
Crew fatalities:
Pax on board:
2
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
4545
Captain / Total hours on type:
245.00
Aircraft flight hours:
29550
Circumstances:
Shortly after take off from runway 20, aircraft hit tree tops, stalled and crashed in a wooded area near the airport. Both passenger were slightly injured while the pilot was seriously injured. Aircraft was damaged beyond repair. The director of operations for the operator stated that soft field conditions and standing water on the runway slowed the airplane during the takeoff roll. The airplane did not lift off in time to clear trees at the end of the runway and sustained substantial damage to both wings and the fuselage when it collided with the trees. The pilot reported that he used partial power at the beginning of the takeoff roll to avoid hitting standing water on the runway with full power. After passing most of the water, he applied full power, but the airplane did not accelerate like he thought it would. He recalled the airplane being in a nose-high attitude and the main wheels bouncing several times before the airplane impacted the trees at the end of the runway.
Probable cause:
The pilot's delayed application of full power during a soft/wet field takeoff, resulting in a collision with trees during takeoff.
Final Report:

Crash of a Beechcraft 65 Queen Air off San Carlos: 3 killed

Date & Time: Sep 2, 2010 at 1151 LT
Type of aircraft:
Operator:
Registration:
N832B
Flight Phase:
Flight Type:
Survivors:
No
Schedule:
San Carlos - Santa Clara
MSN:
LC-112
YOM:
1961
Crew on board:
1
Crew fatalities:
Pax on board:
2
Pax fatalities:
Other fatalities:
Total fatalities:
3
Captain / Total flying hours:
18000
Captain / Total hours on type:
6000.00
Circumstances:
Shortly after takeoff for a repositioning flight for the airplane’s upcoming annual inspection, numerous witnesses, including the two air traffic controllers, reported observing the airplane climbing out normally until it was about 1/2 mile beyond the runway. The witnesses stated that the airplane then underwent a short series of attitude excursions, rolled right, and descended steeply into a lagoon. All radio communications between the airplane and the air traffic controllers were normal. Ground-based radar tracking data indicated that the airplane's climb to about 500 feet was normal and that it was airborne for about 40 seconds. Postaccident examination of the airframe, systems, and engines did not reveal any mechanical failures that would have precluded continued normal operation. Damage to both engines’ propeller blades suggested low or moderate power at the time of impact; however, the right propeller blades exhibited less damage than the left. The propeller damage, witness-observed airplane dynamics, and the airplane’s trajectory were consistent with a loss of power in the right engine and a subsequent loss of control due to airspeed decay below the minimum control speed (referred to as VMC). Although required by the Federal Aviation Administration (FAA)-approved Airplane Flight Manual, no evidence of a cockpit placard to designate the single engine operating speeds, including VMC, was found in the wreckage. The underlying reason for the loss of power in the right engine could not be determined. The airplane's certification basis (Civil Air Regulation [CAR] 3) did not require either a red radial line denoting VMC or a blue radial line denoting the single engine climb speed (VYSE) on the airspeed indicators; no such markings were observed on the airspeed indicators in the wreckage. Those markings were only mandated for airplanes certificated under Federal Aviation Regulation Part 23, which became effective about 3 years after the accident airplane was manufactured. Neither the Federal Aviation Administration (FAA) nor the airplane manufacturer mandated or recommended such VMC or VYSE markings on the airspeed indicators of the accident airplane make and model. In addition, a cursory search did not reveal any such retroactive guidance for any twin-engine airplane models certificated under CAR 3. Follow-up communication from the FAA Small Airplane Directorate stated that the FAA has "not discussed this as a possible retroactive action... Our take from the accident studies is that because of the accident record with light/reciprocating engine twins, the insurance industry has restricted them to a select group of pilot/owners…" Toxicology testing revealed evidence consistent with previous use of marijuana by the pilot; however, it was not possible to determine when that usage occurred or whether the pilot might have been impaired by its use during the accident flight.
Probable cause:
A loss of power in the right engine for undetermined reasons and the pilot’s subsequent failure to maintain adequate airspeed, which resulted in a loss of control. Contributing to the loss of control was the regulatory certification basis of the airplane that does not require airspeed indicator markings that are critical to maintaining airplane control with one engine inoperative.
Final Report:

Crash of an Antonovv AN-26B in Tallinn

Date & Time: Aug 25, 2010 at 1747 LT
Type of aircraft:
Operator:
Registration:
SP-FDP
Flight Phase:
Flight Type:
Survivors:
Yes
Schedule:
EXN3788
MSN:
119 03
YOM:
1982
Flight number:
Tallinn - Helsinki
Country:
Region:
Crew on board:
4
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
5569
Captain / Total hours on type:
4432.00
Copilot / Total flying hours:
738
Copilot / Total hours on type:
485
Aircraft flight hours:
21510
Circumstances:
On 25th August 2010 cargo aircraft An-26B, registration SP-FDP started from Tallinn-Lennart Meri-Ülemiste Airport to Helsinki. After uneventful flight preparations, the aircraft started its take-off roll on runway 08. Based on pilots statements and FDR/CVR recordings the aircraft entered runway 08 from taxiway B on the West end of the runway and lined up for takeoff. On 16:47:22 the aircraft started its takeoff roll. The calculated V1 was 182 and Vr was 201 km/h. 10 seconds later PF started rotation without Vr callout at 123 km/h. The aircraft pitch angle increased to 4.6˚ 2 seconds later. At 16:47:38 the navigator made V1 call-out at 160.5 km/h. 1 second later flight engineer called “Retracting” in Polish. The aircraft started to pitch down and 3 seconds later it contacted the runway and continued on its belly for 1,228 m before coming to its rest position 3 m right from the runway centerline. No persons were injured and no fire broke up. The occurrence was classified as an accident due to the substantial damage to the aircraft structures.
Probable cause:
The investigation determined the inadequate action of the flight engineer, consisting in early and uncommanded landing gear retraction, as a cause of the accident.
Contributing factors to the accident were:
1. Inadequate crew recourse management and insufficient experience in cooperation and coordination between crewmembers.
2. Start of aircraft rotation at low speed and with fast elevator movement to 17˚, which resulted in:
Lifting the aircraft sufficiently to close the WOW switch and allow the retraction of the landing gear at the speed not sufficient for the climb.
Providing misleading information to FE about the aerodynamic status of the aircraft.
3. Inadequate adjustment of the WOW switch, which allowed the gear retraction to be activated before the aircraft was airborne. The position of the landing gear selector on the central console is not considered as a contributing factor to the accident. However, investigation finds necessary to point it out as a safety concern, specifically in situations, where crewmembers are trained and/or used to operate the aircrafts with gear selector location according to the EASA Certification Standards CS-25. Positioning of the gear lever to the location which is compliant to EASA document CS-25, would create additional safety barrier to avoid similar occurrences, specifically in aircrafts where landing gear is operated by FE.
Final Report: