Crash of a Pilatus PC-12/47 off Plettenberg Bay: 9 killed

Date & Time: Feb 8, 2011 at 1633 LT
Type of aircraft:
Registration:
ZS-GAA
Survivors:
No
Schedule:
Queenstown - Plettenberg Bay
MSN:
858
YOM:
2007
Country:
Region:
Crew on board:
2
Crew fatalities:
Pax on board:
7
Pax fatalities:
Other fatalities:
Total fatalities:
9
Captain / Total flying hours:
2662
Captain / Total hours on type:
582.00
Copilot / Total flying hours:
351
Copilot / Total hours on type:
112
Aircraft flight hours:
1096
Circumstances:
The aircraft, which was operated under the provisions of Part 91 of the Civil Aviation Regulations (CARs), departed from Queenstown Aerodrome (FAQT) at 1329Z on an instrument flight plan for Plettenberg Bay Aerodrome (FAPG). On board the aircraft were two (2) crew members and seven (7) passengers. The estimated time of arrival for the aircraft to land at FAPG was 1430Z, however the aircraft never arrived at its intended destination, nor did the crew cancel their search and rescue as per flight plan/air navigation requirements. At ±1600Z an official search for the missing aircraft commenced. The search was coordinated by the Aeronautical Rescue Co-ordination Centre (ARCC). The first phase of the search, which was land based, was conducted in the Robberg Nature Reserve area. Progress was slow due to poor visibility associated with dense mist and night time. A sea search was not possible following activation of the official search during the late afternoon and night time, but vessels from the National Sea Rescue Institute (NSRI) were able to launch at first light the next morning. Floating debris (light weight material) was picked up from the sea and along the western shoreline of the Robberg Nature Reserve where foot patrols were conducted. On 11 February 2011 the South African Navy joined the search for the missing wreckage by utilizing side scan sonar equipment to scan the sea bed for the wreckage. All the occupants on board the aircraft were fatally injured in the accident.
Probable cause:
The aircraft crashed into the sea following a possible in flight upset associated with a loss of control during IMC conditions.
The following contributory factors were identified:
- Deviation from standard operating procedures by the crew not flying the published cloud-break procedure for runway 30 at FAPG, but instead opted to attempt to remain visual with the ground/sea (comply with VMC requirements) by descending over the sea and approaching the aerodrome from the southeast (Robberg Nature Reserve side).
- Inclement weather conditions prevailed in the area, which was below the minima to comply with the approved cloud-break procedure for runway 30 at FAPG (minimum safety altitude of 844 feet according to cloud-break procedure) as published at the time of the accident.
- Judgement and decision making lacking by the crew. (The crew continued from the seaward side with the approach during IMC conditions and not diverting to an alternative aerodrome with proper approach facilities timeously although a cell phone call in this regard indicate such an intention).
- The possibility that the pilot-flying at the time became spatially disorientated during the right turn while encountering / entering IMC conditions in an attempt to divert to FAGG should be regarded as a significant contributory factor to this accident.
- This was the first time as far as it could be determined that the two crew members flew together.
Final Report:

Crash of a Hawker 850XP in Sulaymaniyah: 7 killed

Date & Time: Feb 4, 2011 at 1749 LT
Type of aircraft:
Operator:
Registration:
OD-SKY
Flight Phase:
Survivors:
No
Schedule:
Sulaymānīyah - Ankara
MSN:
258804
YOM:
2006
Country:
Region:
Crew on board:
3
Crew fatalities:
Pax on board:
4
Pax fatalities:
Other fatalities:
Total fatalities:
7
Circumstances:
Shortly after take off from Sulaymaniyah Airport runway 31, while in initial climb, the aircraft stalled and crashed 2,100 metres from the airport, bursting into flames. The aircraft was totally destroyed by a post crash fire and all seven occupants were killed, among them four employees of the Iraqi communications company Asiacell. Weather conditions at the time of the accident were as follow: 1,500 metres visibility in snow falls, overcast 3,500 feet.
Probable cause:
The following findings were identified:
- The wings, elevator and horizontal stabilizer top surface were contaminated with ice and snow.
- The crew was in a hurry due to early passenger arrival.
- The crew didn’t remove the snow and ice contamination from the control surfaces nor did he call for de-icing actions.
- Ice and snow contamination on tail section most likely cause sluggish rotation during the takeoff; this will resulting in over rotation and wing stall.
- Snow and ice contamination on the wing, fuselage and tail will compromise the normal takeoff characteristics.
- A combination of snow and ice causing disruptive air flow, heaver actual weights and over rotation, the combination of which most likely didn’t activate the stall warning safety design. The aircraft could stall asymmetrical without warning during takeoff.
- That was the probable cause of the accident.
Final Report:

Crash of a Learjet 35A in Springfield

Date & Time: Jan 6, 2011 at 1100 LT
Type of aircraft:
Operator:
Registration:
N800GP
Survivors:
Yes
Schedule:
Chicago - Springfield
MSN:
35A-158
YOM:
1978
Flight number:
PWA800
Crew on board:
2
Crew fatalities:
Pax on board:
4
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
5932
Captain / Total hours on type:
827.00
Aircraft flight hours:
16506
Circumstances:
The flight encountered light rime icing during an instrument approach to the destination airport. The copilot was the pilot flying at the time of the accident. He reported that the airframe anti-icing system was turned off upon intercepting the instrument approach glide slope, which was shortly before the airplane descended below the cloud layer. He recalled observing light frost on the outboard wing and tip tank during the approach. The stick shaker activated on short final, and the airplane impacted left of the runway centerline before it ultimately departed the right side of the runway pavement and crossed a slight rise before coming to rest in the grass. The cockpit voice recorder transcript indicated that the pilots were operating in icing conditions without the wing anti- ice system activated for about 4 1/2 minutes prior to activation of the stick shaker. A postaccident examination of the airplane did not reveal any anomalies consistent with a preimpact failure of the flight control system or a loss of anti-ice system functionality. A performance study determined that the airplane’s airspeed during the final 30 seconds of the flight was about 114 knots and that the angle of attack ultimately met the stick shaker threshold. The expected stall speed for the airplane was about 93 knots. The airplane flight manual stated that anti-ice systems should be turned on prior to operation in icing conditions during normal operations. The manual warned that even small accumulations of ice on the wing leading edge can cause an aerodynamic stall prior to activation of the stick shaker and/or stick pusher.
Probable cause:
The pilot’s decision to conduct an instrument approach in icing conditions without the anti-ice system activated, contrary to the airplane flight manual guidance, which resulted in an inadvertent aerodynamic stall due to an in-flight accumulation of airframe icing.
Final Report:

Crash of a Beechcraft 1900C-1 in Karachi: 21 killed

Date & Time: Nov 5, 2010 at 0706 LT
Type of aircraft:
Operator:
Registration:
AP-BJD
Flight Phase:
Survivors:
No
Schedule:
Karachi - Bhit Shah
MSN:
UC-157
YOM:
1991
Country:
Region:
Crew on board:
2
Crew fatalities:
Pax on board:
19
Pax fatalities:
Other fatalities:
Total fatalities:
21
Captain / Total flying hours:
8114
Captain / Total hours on type:
1820.00
Copilot / Total flying hours:
1746
Copilot / Total hours on type:
1338
Aircraft flight hours:
18545
Aircraft flight cycles:
24990
Circumstances:
0C-1 aircraft Reg # AP-BJD was scheduled to fly chartered flight from Jinnah International Airport (JIAP), Karachi to Bhit Shah Oil Fields to convey 17 employees of M/s Eni company including one foreign national from Italy. The flight crew included two cockpit crew ie Captain and First Officer (FO), one JS (Air) ground crew (technician) and one Airport Security Force staff. The Mishap Aircraft (MA) took off from JIAP, Karachi at 02:04:31 UTC. The reported weather was fit for the conduct of ill-fated flight to Bhit Shah Oil Fields. After takeoff aircraft experienced Engine No 2 abnormal operation and cockpit crew decided to land back at JIAP Karachi after calling right hand downwind for runway 25R. While joining for right hand downwind for 25R the mishap aircraft could not sustain flight and crashed at a distance of around 1 nm from runway 07R beginning JIAP, Karachi. All souls (21) onboard got fatally injured as a result of aircraft ground impact and extensive post impact ground fire.
Probable cause:
Detailed investigation and analyses of the examinable evidence confirmed that the aircraft had developed some problem with its Engine No.2 (Right) immediately after takeoff which was observed by the cockpit crew as propeller feathering on its own. No concrete evidence could be found which would have led to the engine’s propeller malfunction as observed. The only probable cause of propeller feathering on its own could be the wear & tear of the beta valve leading to beta system malfunction. However, this anomaly at the most could have led to the non availability of one engine and making a safe landing with a single engine since the aircraft was capable of landing with a single engine operation. Some of the actions by the cockpit crew before takeoff and subsequent to the observed anomaly in the Engine No.2 were not according to the QRH / FCOM which aggravated the situation and resulted into the catastrophic accident.
The following factors contributed to the accident:
The aircraft accident took place as a result of combination of various factors which directly and indirectly contributed towards the causation of accident.
The primary cause of accident includes, inappropriate skill level of Captain to handle abnormal operation of engine No 2 just after takeoff, failure of cockpit crew to raise the landing gears after experiencing the engine anomaly, execution of remedial actions by FO before the attainment of minimum safe altitude of 400 ft AGL resulted in non conformance and non compliance of cockpit crew to OEM recommended procedures to handle such situations.
The lack of situational awareness and CRM failure directly contributed towards ineffective management of the flight deck by the cockpit crew.
The contributory factors include inadequate cockpit crew simulator training monitoring mechanism both at operator and CAA Pakistan levels in respect of correlation of previous / current performance and skill level of cockpit crew during the simulator training sessions along with absence of conduct of recurrent / refresher simulator training between two annual simulator checks in accordance with ICAO Annex-6 guidelines and CAA Pakistan (applicable ANOs) requirements for specific type of aircraft in a year.
Final Report:

Crash of a Beechcraft 100 King Air in Kirby Lake: 1 killed

Date & Time: Oct 25, 2010 at 1120 LT
Type of aircraft:
Operator:
Registration:
C-FAFD
Survivors:
Yes
Schedule:
Calgary - Edmonton - Kirby Lake
MSN:
B-42
YOM:
1970
Flight number:
KBA103
Country:
Crew on board:
2
Crew fatalities:
Pax on board:
8
Pax fatalities:
Other fatalities:
Total fatalities:
1
Circumstances:
The aircraft was on an instrument flight rules flight from the Edmonton City Centre Airport to Kirby Lake, Alberta. At approximately 1114 Mountain Daylight Time, during the approach to Runway 08 at the Kirby Lake Airport, the aircraft struck the ground, 174 feet short of the threshold. The aircraft bounced and came to rest off the edge of the runway. There were 2 flight crew members and 8 passengers on board. The captain sustained fatal injuries. Four occupants, including the co-pilot, sustained serious injuries. The 5 remaining passengers received minor injuries. The aircraft was substantially damaged. A small, post-impact, electrical fire in the cockpit was extinguished by survivors and first responders. The emergency locator transmitter was activated on impact. All passengers were BP employees.
Probable cause:
Findings as to Causes and Contributing Factors:
1. The conduct of the flight crew members during the instrument approach prevented them from effectively monitoring the performance of the aircraft.
2. During the descent below the minimum descent altitude, the airspeed reduced to a point where the aircraft experienced an aerodynamic stall and loss of control. There was insufficient altitude to effect recovery prior to ground impact.
3. For unknown reasons, the stall warning horn did not activate; this may have provided the crew with an opportunity to avoid the impending stall.
Findings as to Risk:
1. The use of company standard weights and a non-current aircraft weight and balance report resulted in the flight departing at an inaccurate weight. This could result in a performance regime that may not be anticipated by the pilot.
2. Flying an instrument approach using a navigational display that is outside the normal scan of the pilot increases the workload during a critical phase of flight.
3. Flying an abbreviated approach profile without applying the proper transition altitudes increases the risk of controlled flight into obstacles or terrain.
4. Not applying cold temperature correction values to the approach altitudes decreases the built-in obstacle clearance parameters of an instrument approach.
Final Report:

Crash of a Gippsland GA8 Airvan in Lady Barron

Date & Time: Oct 15, 2010 at 1715 LT
Type of aircraft:
Operator:
Registration:
VH-DQP
Survivors:
Yes
Site:
Schedule:
Lady Barron - Bridport
MSN:
GA8-05-075
YOM:
2005
Country:
Region:
Crew on board:
1
Crew fatalities:
Pax on board:
6
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
2590
Captain / Total hours on type:
1355.00
Circumstances:
The pilot was conducting a charter flight from Lady Barron, Flinders Island to Bridport, Tasmania with six passengers on board. The aircraft departed Lady Barron Aerodrome at about 1700 Australian Eastern Daylight-saving Time and entered instrument meteorological conditions (IMC) several minutes afterwards while climbing to the intended cruising altitude of about 1,500 ft. The pilot did not hold a command instrument rating and the aircraft was not equipped for flight in IMC. He attempted to turn the aircraft to return to Lady Barron Aerodrome but became lost, steering instead towards high ground in the Strzelecki National Park in the south-east of Flinders Island. At about 1715, the aircraft exited cloud in the Strzelecki National Park, very close to the ground. The pilot turned to the left, entering a small valley in which he could neither turn the aircraft nor out climb the terrain. He elected to slow the aircraft to its stalling speed for a forced landing and, moments later, it impacted the tree tops and then the ground. The first passenger to exit the aircraft used the aircraft fire extinguisher to put out a small fire that had begun beneath the engine. The other passengers and the pilot then exited the aircraft safely. One passenger was slightly injured during the impact; the pilot and other passengers were uninjured. During the night, all of the occupants of the aircraft were rescued by helicopter and taken to the hospital in Whitemark, Flinders Island.
Probable cause:
Contributing safety factors:
• The weather was marginal for flight under the visual flight rules, with broken cloud forecast down to 500 ft above mean sea level in the area.
• The pilot, who did not hold a command instrument rating, entered instrument meteorological conditions because he was adhering to an un-written operator rule not to fly below 1,000 ft above ground level.
• The pilot became lost in cloud and flew the aircraft towards the Mt Strzelecki Range, exiting the cloud in very close proximity to the terrain.
• The aircraft exited the cloud in a small valley, within which the pilot could neither turn round nor out-climb the terrain.
Other key findings:
• The aircraft exited cloud before impacting terrain and with sufficient time for the pilot to execute a forced landing.
• The design of the aircraft’s seats, and the provision to passengers in the GA-8 Airvan of three-point automotive-type restraint harnesses with inertia reel shoulder straps contributed to the passengers’ survival, almost without injury.
Final Report:

Crash of a Cessna 501 Citation I/SP off Coatzacoalcos: 8 killed

Date & Time: Oct 6, 2010 at 0745 LT
Type of aircraft:
Registration:
XA-TKY
Flight Phase:
Survivors:
No
Schedule:
Culiacán – Puebla – Minatitlán – Veracruz
MSN:
501-0029
YOM:
1977
Country:
Crew on board:
2
Crew fatalities:
Pax on board:
6
Pax fatalities:
Other fatalities:
Total fatalities:
8
Circumstances:
The aircraft departed Culiacán on a round trip to Veracruz with intermediate stops in Puebla and Minatitlán, carrying two pilots and six employees of the Coppel Company. One minute after takeoff from Minatitlán Airport, while in initial climb, the aircraft entered an uncontrolled descent and crashed in the sea off Coatzacoalcos. A day later, few debris were found on beaches. The main wreckage was not found and all eight occupants were killed.
Crew:
Javier Montoya,
Bernardo Estrada.
Passengers:
Salvador Leyva,
David Jurado,
Norma Torres,
Brenda Camacho,
Alejandro Quintero,
Freddy Peraza.

Crash of a Cessna 402C in Nassau: 9 killed

Date & Time: Oct 5, 2010 at 1236 LT
Type of aircraft:
Operator:
Registration:
C6-NLH
Flight Phase:
Survivors:
No
Schedule:
Nassau – Cockburn Town
MSN:
402C-0458
YOM:
1981
Country:
Crew on board:
2
Crew fatalities:
Pax on board:
7
Pax fatalities:
Other fatalities:
Total fatalities:
9
Captain / Total flying hours:
12000
Captain / Total hours on type:
10000.00
Circumstances:
On October 5, 2010 about 1636 UTC / 12:36pm Eastern Daylight Time (EDT), C6-NLH a Cessna 402C aircraft registered to Lebocruise Air Limited and operated by Acklins Blue Air Charter/Nelson Hanna crashed into lake Killarney shortly after becoming airborne from runway 14 at Lynden Pindling International Airport, Nassau, New Providence, Bahamas. The airplane sustained substantial damages by impact forces. The pilot, copilot and seven (7) passengers aboard the airplane received fatal injuries. The aircraft was on a passenger carrying flight from Lynden Pindling Intl Airport (MYNN) to Cockburn Town, San Salvador, Bahamas (MYSM). The aircraft was on a visual flight rules flight plan. Visual meteorological conditions prevailed at the time of the accident. The official notification of the accident was made to the Manager of the Flight Standards Inspectorate at Lynden Pindling Intl Airport, Nassau, N. P., Bahamas shortly thereafter. The investigation began the same day at approximately 1655 UTC upon notification of the IIC. The investigation was conducted by the Bahamas Civil Aviation Department [BCAD], Inspector Delvin R. Major (Investigator-in-Charge) of the Air Accident Investigation and Prevention Unit (AAIPU), Management of BCAD and Flight Standards Inspectorate (FSI), Airworthiness Inspectors, Operations Inspectors, Human Factors and other administrative staff. Valuable assistance was also received from the National Transportation Safety Board (NTSB), the Federal Aviation Administration (FAA) and Manufacturers of the aircraft and engine components. Three (3) Air Operator Certificate (AOC) holders at the Domestic Section of Lynden Pindling Intl Airport stated that on the day of the accident flight; one of the victims of the accident aircraft approached each of them individually at different times, requesting a quote and their availability to conduct a charter flight to Cockburn Town, San Salvador, Bahamas. Each AOC holder reported that they declined to conduct the charter because by looking at the amount of luggage and other equipment that accompanied the passengers and the size of the passengers that wanted to travel, in their estimation the combined weight appeared to be in excess of the weight that their respective aircraft (Cessna 402C and Hawker Beechcraft B100) can accommodate. After the AOC holders declined to conduct the charter, sometime thereafter, the same individual that was arranging the flight with the previous AOC holders made contact with Nelson Hanna / Acklins Blue Air Charter where arrangements were made to conduct the charter flight. The aircraft type certificate allowed for the aircraft to be operated by one (1) pilot, but the fatal flight was operated by a crew of two (2) pilots (according to eyewitness reports). The aircraft actual weight and center of gravity was unknown. As far as could be determined, the takeoff weight exceeded the maximum weight allowed of 6,850 pounds by more than 500 pounds. This excess in weight also placed the center of gravity of the aircraft outside of the safe envelope / limits for flight allowed by the manufacturer. The flight crew was given instructions by ATC to taxi from the business aviation apron (Executive Flight Support) for a takeoff on Runway 14 at intersection Foxtrot. (Intersection Foxtrot is 2,000 feet beyond the threshold of Runway 14, with a take-off run available of 9,353 feet. (Runway 14 - 11,353 feet long by 150 feet wide, see Appendix 5.15). According to eyewitness reports, from the initiation of takeoff power up to the point when the aircraft lost control white smoke was observed trailing behind the left engine of the aircraft. Eyewitnesses also reported that the take off appeared normal with gear being retracted shortly after takeoff and the aircraft seemed to be struggling to climb. The aircraft was seen at a low height, turning in a left direction over the lake as if trying to return for a landing at the airport. The bank of the aircraft changed from shallow to very steep to almost perpendicular to the ground, gears were extended and almost immediately the aircraft lost control and nose dived into the lake inverted. It cart wheeled, coming to rest upright, approximately ¼ mile from the approach end of runway 27. The aircraft came to rest on an approximate heading of 210 degrees. Eyewitness also reported hearing the engine run for a few seconds after the aircraft made contact with the water of the lake. There were no reports from the pilot to ATC of an emergency or any abnormalities with the aircraft or its systems after takeoff. The flight plan form filed for this flight listed one (1) soul on board; however, there were 7 additional occupants including a “second pilot” discovered onboard the accident flight the day of the accident. The aircraft's recovery and search for luggage, equipment and additional victims commenced shortly after the accident. This effort however, was hampered by inclement weather, rough lake conditions and darkness. On October 6th, the day after the crash, aircraft recovery continued. Family members of an additional person believed to be on board, advised the authorities that there was a ninth (9th) person on board. Search to recover any additional bodies continued but search and recovery efforts proved fruitless. On October 7th, the second day after the crash, the body of the ninth (9th) victim was found in the marshes and recovered from the southwestern end of the lake in the vicinity of where the fatal crash occurred.
Probable cause:
The following findings were identified:
1. Acklins Blue Air Charter was advertising and operating as a Bahamas air taxi operator without having undergone the certification process in contravention of Bahamas Civil Aviation (Safety) Regulations Schedule 12.
2. The airplane was issued a Certificate of Airworthiness on May 19, 2010, by the Bahamas Flight Standards Inspectorate, and was being operated by Acklins Blue Air Charter.
3. The Cessna 402C aircraft is classified in the performance Group C. This requires rapid feathering of the propeller of a failed engine and the raising of flap and the landing gear in order to achieve maximum climb performance.
4. The airplane maintenance records were not located; therefore, no determination could be made whether the airplane was being maintained in accordance with Bahamas Civil Aviation Regulations.
5. The 12,000 hour pilot and second pilot were not qualified to operate in Bahamas commercial air taxi operations.
6. No determination could be made whether the pilot or second pilot had completed required training and had accomplished a satisfactory recurrent flight check of their flying ability as required by CASR Schedule 12 and 14 for aircraft operating in commercial air transportation as well as the stipulation by the insurance policy.
7. Post-accident weight and balance calculations indicate the airplane was being operated approximately 523 pounds over maximum certificated takeoff weight (6,850 lb)
8. The pilot was advised by an air traffic controller that white smoke was trailing the left engine during takeoff; the pilot did not declare an emergency or advise the controller of any engine failure or mechanical abnormality.
9. The airplane's left engine could not produce rated shaft horsepower during takeoff.
10. Several factors contributing to the degradation of the airplane's performance and its inability to maintain flight include the wind-milling propeller, the pilot's intentional initiation of a steep turn to return to the departure airport, and his intentional lowering of the landing gear during the turn to return.
11. While turning to return, the airplane stalled, pitched nose down, and impacted in a lake.
12. The search and rescue efforts were timely and appropriate; however, the lack of accurate information on the pilot submitted flight plan delayed recovery of all victims.
13. The left propeller was not feathered.
14. The No. 2 cylinder of the left engine failed due to fatigue that originated in the root of the cylinder head thread that was engaged with the first thread on the barrel.
15. Post-accident inspection of the cockpit revealed several switches for the right engine were secured; however, no determination could be made when the switches were placed / moved in those positions.
16. No evidence of failure of the airplane's structures or flight control system contributed to the accident.
17. Existing regulations did not require the aircraft to be fitted with flight recorders. The lack of any recorded data about the aircraft's performance or the flight crew conversations deprived the investigation team of essential factual information.
18. Current Civil Aviation Department personnel and budget resources may not be sufficient to ensure that the quality of surveillance for certified as well as uncertified air carrier operations will improve.
19. Airside access procedures are inadequate at Fixed Base Operators. Access to the secure airside occurring without any check of individuals to challenge whether they have a legitimate reason for accessing the secure airside. FBO door to access airside is not secured or locked continuously; persons observed walking in and out without being challenged.
20. Flight Plan Forms are being accepted and transmitted to ATC with incomplete information. This information is vital for search and rescue purposes.
21. Weather was not a factor in the accident.
22. ATC was not a factor in the accident.
23. Currently flight plans for private flights are only required for international operations.
24. The pilot was aware of discrepancy associated with the manifold pressure reading of the left engine prior to takeoff. This discrepancy was brought to his attention by a client from the flight immediately preceding the accident flight.
25. The exact center of gravity of the accident airplane could not be calculated accurately as no indication of what seat each passenger occupied in the airplane and no indication of where luggage or equipment were placed on the aircraft could be determined. However, due to the exceedance of weight limits the aircraft was already outside the allowable center of gravity envelope developed by the manufacturer.
26. The pilot had insufficient time to prepare for the approach to runway 27 before beginning the approach. The airplane pitched up quickly into a stall, after extension of gear, recovery before ground impact was unlikely once the stall began.
27. Post accident inspection did not reveal any mechanical evidence or problems with the right hand engine.
28. The pilot's decision to return to the airfield was reasonable. Once the aircraft began to lose height a return to the airfield became impractical and a forced landing in the direction of flight should have been attempted.
29. The right propeller was never recovered from the lake.
The following causal factors were identified:
1. The left engine suffered a mechanical failure of the #2 cylinder, and therefore could not produce rated shaft horsepower. No indication of total loss of power with the left engine reported.
2. Right Engine electrical and engine control switches were found in the “OFF” position, therefore the aircraft was incapable of climbing on the power of one engine alone.
3. The excess weight above the maximum weight allowed for takeoff may have been an important factor in the aircraft's inability to gain adequate altitude after takeoff.
4. The pilot secured the right engine which was mechanically capable of producing power resulting in a total loss of thrust. He then sometime thereafter initiated a steep turn with gear down and the left engine already not developing sufficient shaft horsepower to sustain lift.
5. The pilot attempted to return to the departure airfield but lost control of the aircraft during a turn to the left.
Final Report:

Crash of a Beechcraft B100 King Air in Montmagny

Date & Time: Sep 22, 2010 at 1700 LT
Type of aircraft:
Operator:
Registration:
C-FSIK
Flight Phase:
Survivors:
Yes
Schedule:
Montmagny - Montreal
MSN:
BE-39
YOM:
1978
Country:
Crew on board:
2
Crew fatalities:
Pax on board:
4
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
4500
Captain / Total hours on type:
2500.00
Copilot / Total flying hours:
7800
Copilot / Total hours on type:
675
Circumstances:
The aircraft was operating as flight MAX100 on an instrument flight rules flight from Montmagny to Montreal/St-Hubert, Quebec, with 2 pilots and 4 passengers on board. At approximately 1700 Eastern Daylight Time, the aircraft moved into position on the threshold of 3010-foot-long runway 26 and initiated the take-off. On the rotation, at approximately 100 knots, the flight crew saw numerous birds in the last quarter of the runway. While getting airborne, the aircraft struck the birds and the left engine lost power, causing the aircraft to yaw and roll to the left. The aircraft lost altitude and touched the runway to the left of the centre line and less than 100 feet from the runway end. The take-off was aborted and the aircraft overran the runway, coming to rest in a field 885 feet from the runway end. All occupants evacuated the aircraft via the main door. There were no injuries. The aircraft was substantially damaged.
Probable cause:
Findings As To Causes and Contributing Factors:
The bird strike occurred on take-off at an altitude of less than 50 feet. Gulls were ingested in the left engine, which then lost power.
After the loss of engine power, the flight crew had difficulty controlling the aircraft. The aircraft touched the ground, forcing the pilot flying to abort the take-off when the runway remaining was insufficient to stop the aircraft, resulting in the runway overrun.
Findings As To Risks:
Although a cannon was in place, it was not working on the day of the accident, which increased the risk of a bird strike.
The presence of a goose and duck farm outside the airport perimeter but near a runway increases the risk of attracting gulls.
Operators subject to Canadian Aviation Regulations Subpart 703 are not prohibited from having an aircraft take off from a runway that is shorter than the accelerate-stop distance of that aircraft as determined from the performance diagrams. Consequently, travellers carried by these operators are exposed to the risks associated with a runway overrun when a take-off is aborted.
The absence of a CVR makes it harder to ascertain material facts. Consequently, investigations can take more time, resulting in delays which compromise public safety.
Final Report:

Crash of a Piper PA-31-350 Navajo Chieftain in South Bimini

Date & Time: Sep 19, 2010 at 1440 LT
Operator:
Registration:
N84859
Survivors:
Yes
Schedule:
South Bimini - Fort Lauderdale
MSN:
31-7305043
YOM:
1973
Country:
Crew on board:
1
Crew fatalities:
Pax on board:
6
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
On September 19, 2010, at 1440 eastern daylight time, a Piper PA31-350, N84859, registered to Spirit Air Inc, and operated by Pioneer Air Service was on initial climb out when the lower half of the main cabin door came open. The pilot reversed his course and returned to the departure airport, landing on runway 27. The right main landing gear tire blew out on the landing roll. The airplane went off the right side of the runway, struck a tree, caught fire and came to a complete stop. Visual meteorological conditions prevailed and an instrument flight plan was filed. The commercial pilot and five passengers were not injured and the airplane received substantial damage. The flight originated from Bimini Airport, South Bimini Island, Bahamas, at 1435, and was operated in accordance with 14 Code of Federal Regulations Part 135.