Crash of a Cessna 207A Stationair 8-II in Dillingham

Date & Time: Jul 20, 1992 at 0922 LT
Operator:
Registration:
N9975M
Flight Phase:
Flight Type:
Survivors:
Yes
Site:
Schedule:
Dillingham - New Koliganek
MSN:
207-0772
YOM:
1984
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
2800
Captain / Total hours on type:
200.00
Circumstances:
The pilot bent down to retrieve the fire extinguisher between his feet and to replace it in the bracket located under the pilot's seat. When he looked up he saw a hill in front of the airplane. He pulled up and the airplane struck the hill but continued to fly. He pulled back on the yoke and added full power and the airplane entered the clouds. He noticed he was about to stall the airplane so he lowered the nose and the airplane immediately struck the hill again and nosed over.
Probable cause:
The pilot in command's failure to maintain visual lookout and clearance from terrain. A factor was the pilot diverted his attention to secure a loose fire extinguisher.
Final Report:

Crash of a Short JC-23A Sherpa in Colquitt: 3 killed

Date & Time: Jul 16, 1992 at 0930 LT
Type of aircraft:
Operator:
Registration:
84-0466
Flight Phase:
Flight Type:
Survivors:
No
Schedule:
Cairns AAF - Cairns AAF
MSN:
3113
YOM:
1985
Crew on board:
3
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
3
Circumstances:
The Sherpa departed Fort Rucker-Cairns AAF on a training flight, carrying three crew members who were supposed to test the aircraft in special configuration. Two hours and 45 minutes into the flight, while cruising at an altitude of 5,336 feet in good weather conditions, the aircraft became unstable and rolled to the right to an angle of 12° then to the left to an angle of 35°. It entered an uncontrolled descent before crashing in an open field located 4 miles north of Colquitt, bursting into flames. All three occupants were killed. It was determined that control was lost while the aircraft' speed was 89 knots. Originally, the crew was supposed to simulate an engine failure at the altitude of 10,000 feet but apparently encountered problems as the aircraft' speed was dropping by the order of one knot per second before it became unstable. At the time of the accident, the total weight of the aircraft and its CofG were within limits.
Probable cause:
The exact cause of the stall at a speed of 89 knots remains unclear.

Crash of a Short SC.7 Skyvan 3A Variant 200 in Bethel: 1 killed

Date & Time: Jul 13, 1992 at 1230 LT
Type of aircraft:
Operator:
Registration:
N20086
Flight Phase:
Flight Type:
Survivors:
No
Schedule:
Bethel - Chevak
MSN:
1918
YOM:
1973
Location:
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
1
Captain / Total flying hours:
5000
Captain / Total hours on type:
2000.00
Aircraft flight hours:
6390
Circumstances:
The airplane rolled 200-300 feet before becoming airborne in a very nose high attitude. It maintained this attitude, made a right, then a left bank, and fell to the ground in a nose high attitude. The cargo consisted of eight 55-gallons drums of fuel, laid on their side and secured by one cargo strap running fore and aft and another cargo strap running diagonally across the barrels. The tie down ring ultimate strength rating was 1,600 pounds. The weight of the cargo was 2,863 pounds. Three of the cargo hooks associated with the cargo straps were found still attached to the tie down rings, and one hook and tie down ring were not located. Post-impact fire destroyed the cargo straps, and the barrels were strewn randomly through the cabin/cargo area. According to the manufacturer, the davis tie down ring installation is not approved by the manufacturer. The modification should have been accomplished under a supplemental type certificate. The logbooks showed only an entry. The certificated max gross weight was calculated to have been exceeded by 324.8 lbs. The pilot, sole on board, was killed.
Probable cause:
Inadequate security of the cargo which shifted rearward during the takeoff roll. Factors which contributed to the accident were: the over gross weight condition, and the improper alteration of the tie down rings by the overhauling maintenance facility.
Final Report:

Crash of a Mitsubishi MU-2B-40 Solitaire in Concord: 2 killed

Date & Time: Jul 9, 1992 at 0730 LT
Type of aircraft:
Registration:
N220MA
Flight Phase:
Flight Type:
Survivors:
No
Schedule:
Concord - Yucata - Trenton
MSN:
441
YOM:
1981
Crew on board:
1
Crew fatalities:
Pax on board:
1
Pax fatalities:
Other fatalities:
Total fatalities:
2
Captain / Total flying hours:
6452
Aircraft flight hours:
2706
Circumstances:
The 74 year old pilot and his wife were on a trip to attend a funeral. A witness, who heard the airplane overhead, reported that it sounded low and at least one engine was operating. He reported that when he looked up, the airplane was in a dive, spinning slowly; however, the airplane did not make a complete revolution. Radar data showed the airplane in a left descending turn at approximately 2000 feet per minute. The airplane impacted the ground about 3 miles west of the airport in a near vertical descent, and much of the forward section had penetrated the ground. There was a post-crash fire. Examination of the airplane and various actuators confirmed that the landing gear was retracted, flaps were extended 5°, elevator and aileron trim were neutral, and the rudder was positioned 3° left. Examination of the engine confirmed internal/rotational damage. Both occupants were killed.
Probable cause:
Loss of control during flight for undetermined reason(s).
Final Report:

Crash of a Cessna 421B Golden Eagle II in Shelter Cove

Date & Time: Jul 4, 1992 at 1709 LT
Registration:
N929DB
Flight Phase:
Survivors:
Yes
Schedule:
Shelter Cove - Oakland
MSN:
421B-0864
YOM:
1974
Crew on board:
1
Crew fatalities:
Pax on board:
3
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
2479
Captain / Total hours on type:
218.00
Aircraft flight hours:
2198
Circumstances:
The pilot said he was on the takeoff ground roll at about 100 knots when he discovered that the control lock was still in place. The pilot said he attempted to remove the control lock but could not prior to the aircraft over running the departure end of the 3,400 foot long runway. The aircraft collided with a county sewage treatment building, separating the wings from the fuselage. The aircraft fuselage continued through the building and came to rest on rocks near the beach. All four occupants were seriously injured.
Probable cause:
The pilot's inadequate preflight inspection of the aircraft and his failure to ensure that the control surface locks were removed prior to flight.
Final Report:

Crash of a Piper PA-60 Aerostar (Ted Smith 602P) in Lancaster

Date & Time: Jun 25, 1992 at 1734 LT
Operator:
Registration:
N700MM
Flight Phase:
Flight Type:
Survivors:
Yes
Schedule:
Lancaster - Lancaster
MSN:
60-8265-031
YOM:
1982
Crew on board:
1
Crew fatalities:
Pax on board:
1
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
4980
Aircraft flight hours:
2313
Circumstances:
During the takeoff ground run, witnesses observed the airplane at a slow speed, using the full length of the 4,102-ft runway before it became airborne briefly. The left wing dipped, struck some power lines, and the airplane crashed on a highway striking a car. Metallurgical teardown examinations of the two left engine turbochargers disclosed evidence of extreme wear in the bearings from the turbine wheel shafts which resulted in obstructed oil ports. Both occupants were injured.
Probable cause:
The failure of the left engine turbochargers bearings, which resulted in a loss of power and subsequent degradation of climb performance.
Final Report:

Crash of a Rockwell Grand Commander 690B in Konawa: 1 killed

Date & Time: Jun 25, 1992 at 0833 LT
Registration:
N690JC
Flight Phase:
Flight Type:
Survivors:
No
Schedule:
Norman - Fort Lauderdale
MSN:
690-11479
YOM:
1978
Location:
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
1
Captain / Total flying hours:
8857
Captain / Total hours on type:
98.00
Aircraft flight hours:
3355
Circumstances:
As the airplane was deviating around low intensity weather returns, and passing through 20,500 feet during climb out, it departed controlled flight and entered a right spiral. Descent rates exceeded 16,600 fpm during the descent from 18,300 feet to 3,900 feet and then slowed. Witnesses stated they saw the airplane descend from the clouds in a right flap spin. The empennage had separated from the airplane in pieces. Pieces of the wreckage were found up to 1.5 mile from the primary impact point. Both wings remained attached. The right engine was flamed out, and the propeller was feathered at impact. No mechanical reason for the flameout could be determined. At no time did the pilot indicate he was having difficulties. The NTSB weather study indicated that moderate turbulence was present in the area. The pilot's toxicology tests found 0.151 ug/ml of chlorpheniramine in the blood; normal therapeutic concentration is 0.01 to 0.04. Effects of overdosage include sedation, diminished mental alertness, and cardiovascular collapse to stimulation. The pilot, sole on board, was killed.
Probable cause:
The pilot's failure to maintain control of the airplane which resulted in an inadvertent spiral and subsequent rapid descent. The design stress limits of the airframe were exceeded resulting in an overload failure of the empennage. Factors related to the accident were: turbulence and the pilot's physical impairment due to drugs.
Final Report:

Crash of a Mitsubishi MU-2B-30 Marquise in Alamogordo: 6 killed

Date & Time: Jun 24, 1992 at 2325 LT
Type of aircraft:
Registration:
N108SC
Flight Phase:
Flight Type:
Survivors:
No
Site:
Schedule:
Alamogordo - Burnet
MSN:
545
YOM:
1971
Crew on board:
1
Crew fatalities:
Pax on board:
5
Pax fatalities:
Other fatalities:
Total fatalities:
6
Captain / Total flying hours:
10072
Captain / Total hours on type:
1095.00
Aircraft flight hours:
4251
Circumstances:
The flight had departed the Alamogordo-White Sands Regional Airport after a fuel stop. The pilot had earlier indicated to ATC that he was unfamiliar with the area. Prior to departure at 2321 the pilot was informed that departure radar was out of service. The flight departed with a VFR departure. At 2324 the pilot was advised that radar was back in service, and confirmed that the aircraft was climbing thru 5,300 feet. Discussion ensued between the pilot and controller concerning terrain clearance. At 2324 the pilot indicated he was turning left due to not being sure if a hill was in his path. The airplane impacted a mountain at 6,100 feet msl, 1,500 feet below the summit. The minimum vectoring altitude in the area was 11,000 feet. The aircraft disintegrated on impact and all six occupants were killed.
Probable cause:
The failure of the pilot to exercise adequate VFR departure terrain avoidance procedures, and the failure of the controller to issue a safety alert to the pilot. Factors which contributed to the accident were: the pilot's lack of familiarity with the geographic area, the dark night, and the mountainous terrain.
Final Report:

Crash of a Cessna 421B Golden Eagle II in Monterey: 3 killed

Date & Time: Jun 24, 1992 at 1030 LT
Registration:
N628RJ
Flight Phase:
Flight Type:
Survivors:
No
Schedule:
Monterey - Tucson
MSN:
421B-0028
YOM:
1970
Crew on board:
1
Crew fatalities:
Pax on board:
2
Pax fatalities:
Other fatalities:
Total fatalities:
3
Captain / Total flying hours:
75
Captain / Total hours on type:
10.00
Circumstances:
The 3 occupants aboard were: the owner in the left front seat, his wife in the right front seat, and a man hired by the owner to fly the airplane (seat location could not be determined). Prior to takeoff a man telephoned FSS for a weather briefing and to file an IFR flight plan. He told FSS the pilot's name was J. Hamlett; a J. Hamlett was not aboard (it was found later that Hamlett was the maiden name of the wife of the man hired to fly the airplane). Two minutes after takeoff the pilot was told to contact departure; the pilot acknowledged. This was the last recorded radio contact. The airplane collided with a hill obscured by ground fog about 3 miles east of the airport. The man hired to fly the airplane did not possess an airman certificate; his certificate was revoked 2 years prior to the accident. The owner had obtained his private certificate for airplane single-engine land about 1 month prior to the accident, and had not received any multi-engine instruction. All three occupants were killed.
Probable cause:
The owner/pilot's poor judgement in attempting an operation beyond his experience and ability, which resulted in his failure to attain an adequate climb profile necessary for terrain clearance. Also, the owner/pilot lacked instrument experience, and was overconfident in his ability. Factors in the accident were: the hilly terrain and weather conditions.
Final Report:

Crash of a Grumman TS-2F Tracker in Columbia: 1 killed

Date & Time: Jun 19, 1992 at 1613 LT
Type of aircraft:
Operator:
Registration:
N451DF
Flight Phase:
Flight Type:
Survivors:
No
Site:
Schedule:
Columbia - Columbia
MSN:
548
YOM:
1958
Flight number:
Tanker 92
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
1
Circumstances:
The pilot departed Columbia Airport on a fire fighting mission. After the retardant was dropped on the fire zone, the pilot increased engine power to gain height when the aircraft, flying in reduced visibility due to smoke, collided with trees. It rolled to the left and crashed inverted, bursting into flames. The pilot, sole on board, was killed.
Probable cause:
The pilot was approaching the fire area at an insufficient altitude according to the published procedures of the operator. The pilot's field of vision was probably reduced by the presence of smoke and that when starting the resource, the pilot failed to see the trees struck by the airplane a few seconds later. Despite the fact that no technical failure was found on the aircraft, this assumption was not ruled out.