Crash of a Douglas DC-8-53 in Tokyo

Date & Time: Apr 18, 1977 at 1522 LT
Type of aircraft:
Operator:
Registration:
RP-C803
Flight Phase:
Survivors:
Yes
Schedule:
Tokyo - Manila
MSN:
45937
YOM:
1967
Flight number:
PR421
Country:
Region:
Crew on board:
13
Crew fatalities:
Pax on board:
127
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
10750
Captain / Total hours on type:
601.00
Copilot / Total flying hours:
8030
Copilot / Total hours on type:
194
Aircraft flight hours:
35862
Circumstances:
The crew was cleared to takeoff from runway 15L and started the takeoff procedure. After a course of about 1,000 meters, the airplane lifted off prematurely. It banked left, causing the left wing to struck the ground. Out of control, the airplane landed back onto the runway then went out of control. It veered off runway to the left and while contacting soft ground, all landing gear were torn off as well as all four engines. The airplane slid for about 800 meters before coming to rest. All 140 occupants were evacuated, three of them were injured. The aircraft was written off.
Probable cause:
The left elevator geared tab drive arm assemblies and the elevator gust lock crank assembly failed during the takeoff roll, causing the aircraft to liftoff prematurely and to be uncontrollable.
Final Report:

Crash of a Douglas DC-8-62AF in Anchorage: 5 killed

Date & Time: Jan 13, 1977 at 0635 LT
Type of aircraft:
Operator:
Registration:
JA8054
Flight Phase:
Flight Type:
Survivors:
No
Schedule:
Moses Lake - Anchorage - Tokyo
MSN:
46148/553
YOM:
1971
Flight number:
JL8054
Crew on board:
5
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
5
Captain / Total flying hours:
23252
Captain / Total hours on type:
4040.00
Copilot / Total flying hours:
1603
Copilot / Total hours on type:
1207
Aircraft flight hours:
19744
Circumstances:
On January 13, 1977, a Japan Air Line (JAL) McDonnell-Douglas DC-8-62F, JA 8054, operated as an international charter cargo flight from Moses Lake, Washington, U.S.A., to Tokyo, Japan. An en route stop and crew change were scheduled at Anchorage, Alaska. The aircraft arrived at Anchorage at 0503. The incoming flightcrew reported that the only weather they encountered en route was a layer of fog on the final approach at 800 feet, and that they did not encounter any precipitation or icing. The aircraft was serviced and a walk-around inspection was performed by JAL maintenance personnel and contract mechanics. The two contract mechanics stated that there was ice on the inlet guide vanes, the engine cowlings, and the engine bullet noses, but no ice was reported on the airfoil surfaces. The JAL personnel stated that they did not see any ice on the aircraft. One contract mechanic advised the JAL representative that the engine anti-icing system should be used by the next crew to clear the ice in the engine inlets. No maintenance was performed on the aircraft. The outbound flightcrew was wakened about 0330, left the hotel by taxi about 0430, and arrived at the JAL dispatch office about 0 0500. The taxicab driver who brought the outbound crew to the airport stated that he became concerned by the captain's actions in the taxi and called his dispatcher to report his impressions. He stated that the captain's movements were uncoordinated; that his face was flushed and his eyes were glazed; that his conversation was garbled and incoherent; that his movements were jerky and unstable; and that he had trouble getting out of the cab and had to steady himself on the car door. About 0450 the taxi dispatcher called the operations agent for the contract maintenance company and reported that one of her drivers had taken an "intoxicated" JAL captain to the airport. The operations agent stated that "...it seemed logical that JAL would detect anything unusual and act accordingly." He further stated that a 0620, he notified his line manager of the conversation with the taxi dispatcher and that "I felt that if the captain was intoxicated JAL OPS...or his first officer would have stopped the flight immediately." The JAL dispatch personnel and the inbound JAL crew stated that they noted nothing unusual about the outbound crew. The dispatch briefing proceeded smoothly and no significant questions were asked by the outbound crew. The outbound crew consisted of an American captain and a Japanese first officer and flight engineer. They went to the aircraft about 0515 and boarded the aircraft with the two cattle handlers. The driver of the crew car, a friend of the captain, stated that "...he was in good condition as far as way's I've seen him sometimes and I made that statement before I ever heard any rumors that he was supposedly drunk or had been partying or whatever." A review of the cockpit voice recorder (CVR) indicated that about 0603 the captain and first officer were checking the inputs to the inertial navigation system. They also checked the Automatic Terminal Information Service (ATIS) for local visibility, received their clearance, and began their prestart checklists about 0609. The weather on the ATIS report was in part: "...sky partially obscured, visibility one-quarter mile, fog...". The checklists were completed and the takeoff data reviewed. About 0615 the engines were started and the stickshaker (stall warning system) was tested. The after-start checklist was completed and the aircraft was cleared to taxi to runway 24L. During the taxi, the flight engineer requested and received permission from the captain to turn the engine anti-ice system on because of the ice on the inlet guide vanes. The flight controls and spoilers were checked while taxiing and the flaps were extended to 23°. The taxi checklist was completed and the takeoff data, the flap settings, and the trim settings were again reviewed. The captain, in response to the challenge "anti-ice, de-ice, and rain removal," said, "Ok, we will use engine anti-ice." The de-ice system was reported "off'' by the flight engineer. The captain briefed the crew on the takeoff and abort procedures he would use. He commented that the runway was slippery and he didn't think they would abort. The captain taxied the aircraft southeast on the ramp, past the terminal toward runway 24L. He stopped on the ramp after being instructed to hold short of runway 24R. After several communications with the controller, the aircraft taxied onto runway 24R, and reported ''...ready for takeoff." The tower advised the captain that he was on runway 24R which the captain contradicted. The controller then issued taxi instructions to get the aircraft to runway 24L. The captain made a 180° turn on runway 24R before he finally taxied to the taxiway which leads to the approach end of runway 24L. The crew again reported that they were ready for takeoff at 0633:37. Takeoff was initiated and at 0634:32 the captain called "maximum power". At 0634:50 the captain announced, "I have" and at 0634:52, "80" (knots) was called by the copilot. At 0635:10, "Vee one" was called by the copilot and at 0635:16 rotation was called and acknowledged by the captain. At 0635:19.5 the captain called "Ten degrees" and at 0635:21.4 the first officer called V2. At 0635:26.2 a sound similar to aircraft buffet was recorded. This sound became more frequent and continued until the sounds of impact. At 0635:32 the first officer called "Gear up" and at 0635:33 the flight engineer said "Too much speed (steep)".' At 0635: 38 the engineer called "stall" simultaneously the stickshaker sounded and continued until 0635:39.3, when impact was recorded. A witness near the departure end of the runway saw the aircraft climb to an estimated altitude of about 100 feet above the ground, veer to the left, and then slide '... out of the air." The aircraft was totally destroyed upon impact and all five occupants were killed as well as the 56 cows.
Probable cause:
The probable cause of the accident was a stall that resulted from the pilot's control inputs aggravated by airframe icing while the pilot was under the influence of alcohol. Contributing to the cause of this accident was the failure of the other flightcrew members to prevent the captain from attempting the flight.
Final Report:

Crash of a Douglas DC-8-62 in Moscow: 61 killed

Date & Time: Nov 28, 1972 at 1951 LT
Type of aircraft:
Operator:
Registration:
JA8040
Flight Phase:
Survivors:
Yes
Schedule:
Copenhagen - Moscow - Tokyo
MSN:
46057
YOM:
1969
Flight number:
JL446
Country:
Region:
Crew on board:
14
Crew fatalities:
Pax on board:
62
Pax fatalities:
Other fatalities:
Total fatalities:
61
Circumstances:
A McDonnell Douglas DC-8-62 passenger plane, JA8040, was destroyed when it crashed on takeoff from Moscow's -Sheremetyevo Airport (SVO), Russia. Five of the 14 crew members and ten of the 62 passengers survived the accident. JAL flight JL446 was a scheduled international flight from Copenhagen (CPH), Denmark to Tokyo-Haneda (HND), Japan with an en route stop in Moscow. The flight to Moscow was uneventful and the airplane landed at 18:17. After servicing of the aircraft startup and taxi clearance was received at 19:38. JL446 was cleared for takeoff from runway 25 at 19:49. On takeoff the DC-8 climbed to 100 m with a supercritical angle of attack and lost height abruptly. It hit the ground and burst into flames.
Probable cause:
The cause of the disaster to aircraft DC-8-62 JA-8040 resided in the fact that during take-off and following attainment of the safety speed V2, the crew put the aircraft into a supercritical angle of attack which resulted in loss of speed and altitude. The aircraft's assumption of supercritical angles of attack was the consequence of one of the following circumstances:
- Inadvertent extension of the spoilers in flight, leading to a fall in the maximum value of the lift ratio and an increase in drag;
- Loss of control of the aircraft by the crew in conditions associated with malfunctioning of the No. 1 or No. 2 engine consequent upon possible ice formation on the engine intake at a time when the de-icing system was switched off.
The anomalies in the functioning of the engines observed by the crew and other witnesses may have arisen after the aircraft had assumed a supercritical angle of attack with the spoilers extended.
Final Report:

Crash of a Convair CV-880-22M-3 in Tokyo: 5 killed

Date & Time: Aug 26, 1966 at 1428 LT
Type of aircraft:
Operator:
Registration:
JA8030
Flight Phase:
Flight Type:
Survivors:
No
Schedule:
Tokyo - Tokyo
MSN:
22-00-45M
YOM:
1961
Country:
Region:
Crew on board:
5
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
5
Captain / Total flying hours:
8446
Captain / Total hours on type:
1265.00
Copilot / Total flying hours:
2618
Copilot / Total hours on type:
25
Aircraft flight hours:
5290
Circumstances:
JA8030 started a take-off run on runway 33R of Tokyo International Airport under VFR conditions at approximately 1428 hours with the pilot-in-command Manshichi Harano, examinees Yoshiomi Motouchi and Shuji Daikoku, flight engineer Terumitsu Fujimaki, and Chief Examiner of the Civil Aviation Bureau of Ministry of Transport Yukiaki Kawata, on board for the purpose of conducting a practical examination necessary for change in type rating to Convair 880-22M. About the time the aircraft took a nose-up attitude, it began to yaw left and entered into a right side-slip. At approximately 1 500 m from the runway threshold marking, the right main landing gear started to go off the ground, and while the yaw and side-slip further increased, the under-surface of No. 1 engine began to contact the runway at approximately 1 600 m from the marking. The aircraft continued to side-slip with the nose coming down and deviated from the runway at approximately 1 700 m from the marking. The aircraft moved on the lawn area, crossed taxiway C-4, then while proceeding in the direction of approximately 35O left in reference to the runway bearing, moved the heading to approximately 145O left in reference to the runway bearing, thence yawed right and continued the side-slip. Although the aircraft was in a slight nose-up attitude during this period, it went abruptly into a nose-down and almost at that time a fire started near No. 3 engine. During this period the aircraft further proceeded with the left main landing gear, nose landing gear and Nos. 3, 2, 1 and 4 engines separated in this sequence, and came to a stop at a point approximately 2 100 m from runway 33R threshold marking and approximately 200 m from the runway centre line with a heading of 90° in reference to runway 33L. The fire expanded explosively and the aircraft was damaged by fire or burnt except for the aft fuselage, empennage and a portion of the main wings. All five persons on board died. The flight was performed on behalf of Japan Air Lines.
Probable cause:
The reason for the uncontrollable left yaw was not determined. The following findings were reported:
- No evidence related to the cause of the accident could be found from qualifications, working conditions and others of the flight crew,
- No evidence related to the cause of the accident could be found from investigation of the aircraft wreckage,
- It was recognized that JA 8030 was flown by pilot Daikoku in the left-hand seat,
- It was estimated that the aircraft was taking off with left rudder and right wing down to counteract a cross-wind from the right,
- It was estimated that No. 1 engine was idled around the time VR was reached,
- Although it was estimated that the left rudder was in operation around the time No. 1 engine was idled, it was not clear why and when the rudder came to operation,
- It was estimated that the aircraft was in a right side-slip conditions at the time the tire trace of the right main landing gear started to be marked. It was estimated that, at the time the tire trace of the right main landing gear had disappeared, it became impossible for the crew to counteract by control the rolling moment to the left due to the right side-slip. It is also estimated that the rolling moment produced to a considerable extent resulted from an abrupt increase in side-slip angle due to yawing acceleration after the time the tire trace of the right main landing gear started to be marked.
Final Report:

Crash of a Boeing 707-436 on Mt Fuji: 124 killed

Date & Time: Mar 5, 1966 at 1415 LT
Type of aircraft:
Operator:
Registration:
G-APFE
Flight Phase:
Survivors:
No
Site:
Schedule:
San Francisco – Honolulu – Tokyo – Hong Kong – London
MSN:
17706
YOM:
1960
Flight number:
BA911
Location:
Country:
Region:
Crew on board:
11
Crew fatalities:
Pax on board:
113
Pax fatalities:
Other fatalities:
Total fatalities:
124
Captain / Total flying hours:
14724
Captain / Total hours on type:
2155.00
Copilot / Total flying hours:
3663
Copilot / Total hours on type:
2073
Aircraft flight hours:
19523
Aircraft flight cycles:
6744
Circumstances:
BOAC Flight 911 was a scheduled service from San Francisco (SFO) to Hong Kong (HKG) via Honolulu (HNL) and Tokyo (HND). The Boeing 707 was expected to arrive at Tokyo Airport at 16:45 on 4 March. However, due to poor meteorological conditions at Tokyo and because the precision approach radar (PAR) of the GCA was out of service, it diverted to Fukuoka (FUK) and landed there at 18:00. After staying overnight at Fukuoka, Flight 911 left for Tokyo at 11:25 and landed there at 12:43. The aircraft was prepared for the next leg to Hong Kong and a flight plan was filed for a flight in accordance with the instrument flight rules via Oshima on airway JG6 to Hong Kong at FL310. At 13:42 hours the crew contacted ATC requesting permission to start the engines and clearance for a VMC climb via Fuji-Rebel-Kushimoto. The aircraft left the ramp at 13:50. It was instructed to make "a right turn after take off", and departed Tokyo Airport at 13:58. After takeoff the aircraft flew over Gotemba City on a heading of approximately 298 deg at an altitude of approximately 4900 m and indicated airspeed of 320 to 370 knots. The aircraft, trailing white vapor, then suddenly lost altitude over the Takigahara area, and parts of the aircraft began to break away over Tsuchiyadai and Ichirimatsu. Finally over Tarobo at an altitude of approx. 2000 m, the forward fuselage broke away. The mid-aft fuselage together with the wing, making a slow flat spin to the right, crashed into a forest at the foot of Mount Fuji. The forward fuselage crashed into the forest approx. 300 m to the west of the above site and caught fire. All 124 occupants were killed.
Probable cause:
The aircraft suddenly encountered abnormally severe turbulence over Gotemba City which imposed a gust load considerably in excess of the design limit.
Final Report:

Crash of a Douglas DC-8-43 in Tokyo: 64 killed

Date & Time: Mar 4, 1966 at 2015 LT
Type of aircraft:
Operator:
Registration:
CF-CPK
Survivors:
Yes
Schedule:
Hong Kong – Tokyo – Vancouver
MSN:
45761
YOM:
1965
Flight number:
CP402
Country:
Region:
Crew on board:
10
Crew fatalities:
Pax on board:
62
Pax fatalities:
Other fatalities:
Total fatalities:
64
Captain / Total flying hours:
26564
Captain / Total hours on type:
4089.00
Copilot / Total flying hours:
19789
Copilot / Total hours on type:
3071
Aircraft flight hours:
1792
Circumstances:
Flight 402 was a scheduled international flight from Hong Kong to Tokyo and Vancouver. It took off from Hong Kong at 1614 hours Japan Standard Time and was routed via Taipei, Kagoshima and Ohshima. At 1908 hours it flew over "Spencer Victor" at 25 000 ft and started to descend gradually; at 1912 hours it crossed "Rice Victor" at 18 000 it and two minutes later entered the Kisarazu holding pattern at 14 000 ft where it waited for an improvement of the weather conditions at Tokyo International Airport (TIA). At 1942 hours the flight notified Tokyo air traffic control that if the weather conditions failed to improve within 15 minutes, it would divert to Taipei (alternate airport). Ten minutes later, at 1952 hours the flight was advised by Tokyo ATC that the RVR was 2 400 ft and the pilot then asked for a clearance for approach and landing. The approach clearance was given and the aircraft proceeded to descend to 3 000 ft, in the holding pattern. However, the weather conditions at TIA worsened and the aircraft did not proceed with the approach. The pilot requested a clearance to divert to Taipei at 1958 hours and commenced climbing. At 2005 hours, while heading for Tateyama en route to Taipei the flight was advised by Tokyo air traffic control that visibility at TIA had improved to 4 mile with RVR 3 000 ft. Consequently, the pilot requested a clearance to return to Kisarazu and began descending from 11 500 ft. At 2011 hours the aircraft arrived over Kisarazu at 3 000 ft and began another approach under instructions of the GCA. At this time the flight was quite normal. When the aircraft was 8 NM from touchdown at an altitude of 1 500 ft, it was advised that there was a light tailwind 150015 kt and was cleared to land on runway 33R. The rate of descent for final approach was begun about 5.3 NM from touchdown at approximately 2012:58 hours. The aircraft was on course and on the glide path with a ground speed of approximately 174 kt, gradually decreasing to approximately 140 kt at 2 NM and 114 kt after passing 1 NM. When the aircraft reached one mile from touchdown, the GCA final controller noted that the aircraft was slightly below the GCA glide path and advised "20 ft low, level off momentarily". Nevertheless, the aircraft continued its approach 20 ft below and in parallel with the GCA glide path. After the aircraft passed the P.M. (precision minimum), the aircraft requested the intensity of the lights to be reduced. Shortly thereafter, the aircraft made a sharp descent and its main landing gear wheel struck No. 14 approach light 2 800 ft from touch- down point approximately in an attitude of level flight. Following this first contact, the aircraft struck the approach lights one by one until No. 3 damaging or destroying them, and at approximately 2015 hours crashed against the sea wall with the bottom of the fore-fuselage. Then, the aircraft was thrown over near the end of runway 33R, destroyed and caught fire. All 10 crew members and 54 passengers were killed while eight others were injured.
Probable cause:
The pilot misjudged landing approach under unusually difficult weather conditions. The visibility at Tokyo International Airport was reduced at the time of landing to less than half a mile by fog and smoke, RVR was in the order of 3 000 it. The aircraft carried out a GCA approach to runway 33R under very difficult conditions. It was considered that the approach was normal until a point located between 3 900 and 3 600 ft before the touchdown point. It then entered a steep rate of descent between 3 900 and 3 600 it before the touchdown point, it first struck an approach light 2 800 ft from the touchdown point in an attitude of level flight, then broke several approach light piers and crashed against the sea wall of the airport. The wreckage was thrown over the sea wall near the runway threshold and completely destroyed by the ensuing fire. The steep rate of descent was considered to be the result of an intentional manoeuvre of the aircraft by the pilot-in-command with a view to executing a final approach at a lower altitude than normal. Although no certain cause for the excessive descent which led to striking the approach lights could be determined, it was considered that the poor visibility due to illusive fog conditions that night misled the pilot-in-command in his judgement.
Final Report:

Crash of a Boeing 727-81 off Tokyo: 133 killed

Date & Time: Feb 4, 1966 at 1900 LT
Type of aircraft:
Operator:
Registration:
JA8302
Survivors:
No
Schedule:
Sapporo – Tokyo
MSN:
18822
YOM:
1965
Flight number:
NH060
Country:
Region:
Crew on board:
7
Crew fatalities:
Pax on board:
126
Pax fatalities:
Other fatalities:
Total fatalities:
133
Circumstances:
While approaching Tokyo-Haneda Airport by night and in good weather conditions, at an altitude of about 2,000 feet, the three engine aircraft went out of control and crashed into the Tokyo Bay, about 12 km southeast of the airport. Lots of debris were quickly recovered as well as the tail that sank by a depth of 20 meters. The aircraft disintegrated on impact and none of the 133 occupants survived the crash, which was the worst in Aviation History to date. At the time of the accident, the crew was approaching the airport under VFR mode in good weather conditions and did not report any issues on the frequency.
Probable cause:
The exact cause of the accident could not be determined with certainty. It was reported that the pilot was in contact with ATC during the final approach and did not report any anomalies. Investigations did not reveal any technical issues with instruments or engines or any kind of explosion prior to the accident.

Crash of a Douglas DC-3 on Mt Nakanoone: 2 killed

Date & Time: Feb 14, 1965
Type of aircraft:
Operator:
Registration:
JA5080
Flight Phase:
Flight Type:
Survivors:
No
Site:
Schedule:
Osaka – Tokyo
MSN:
4436
YOM:
1942
Country:
Region:
Crew on board:
2
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
2
Circumstances:
While cruising at an altitude of 2,200 meters in marginal weather conditions, the airplane struck the slope of Mt Nakanoone located some 65 km northeast of Hamamatsu. SAR operations were conducted but eventually suspended few days as no trace of the aircraft nor the crew was found. The wreckage was found on 29 December 1966 in an isolated area. Both pilots were killed.

Crash of a Curtiss C-46D-15-CU Commando in Tokyo

Date & Time: Nov 30, 1964
Type of aircraft:
Operator:
Registration:
51-1107
Flight Type:
Survivors:
Yes
MSN:
33503
YOM:
1945
Country:
Region:
Crew on board:
4
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
The aircraft belly landed at Tokyo-Haneda Airport for unknown reason. All four crew members who were completing a training flight were uninjured while the aircraft was damaged beyond repair.

Crash of a De Havilland DH.114 Heron 1B in Hachijō-jima: 19 killed

Date & Time: Aug 17, 1963 at 1411 LT
Type of aircraft:
Operator:
Registration:
JA6155
Flight Phase:
Survivors:
No
Site:
Schedule:
Hachijō-jima – Tokyo
MSN:
14026
YOM:
1954
Country:
Region:
Crew on board:
3
Crew fatalities:
Pax on board:
16
Pax fatalities:
Other fatalities:
Total fatalities:
19
Circumstances:
Shortly after takeoff from Hachijō-jima Airport, en route to Tokyo-Haneda Airport, the crew climbed in limited visibility due to foggy conditions when the airplane struck the slope of a mountain. As the airplane failed to arrive at destination, SAR were initiated at 1630LT and the wreckage was later found on the slope of a mountain located some 10 km from the airport. The aircraft was destroyed by impact forces and all 19 occupants were killed.
Probable cause:
Investigations were not able to determine the exact cause of the accident. However, the following assumptions were not ruled out:
- A navigation error on part of the crew who followed a wrong departure route in low visibility,
- An engine failure which forced the crew to modify his route in an attempt to return to the airport for an emergency landing.