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Crash of a GippsAero GA10 Airvan near Mojave

Date & Time: Jun 4, 2018 at 1152 LT
Type of aircraft:
Operator:
Registration:
VH-XMH
Flight Phase:
Flight Type:
Survivors:
Yes
Schedule:
Mojave - Mojave
MSN:
GA10-TP450-16-101
YOM:
2016
Crew on board:
2
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
9767
Captain / Total hours on type:
46.00
Copilot / Total flying hours:
10980
Copilot / Total hours on type:
287
Aircraft flight hours:
113
Circumstances:
The airplane manufacturer was conducting spin flight testing for the installation of a cargo pod when the airplane exhibited aberrant behavior and the testing was halted. The chief design engineer (CDE) was consulted, and, to provide a margin of safety for further flights, a forward center of gravity position was authorized for flaps up and flaps takeoff entries to gain more insight into the airplane's behavior on the previous flight. At the final briefing, before the next flight, the flight crew added spins with flaps in the landing configuration (flaps landing) into the test plan without the CDE's consultation or authorization. According to the pilot flying, after two wings-level, power on, flaps landing spins with left rudder and right aileron, a third spin entry was flown in the same configuration except that the entry was from a 30° left-bank turn. The airplane entered a normal spin, and, at one turn, flight controls were inputted for a normal recovery; however, the airplane settled into a fully developed spin. When recovery attempts failed, the decision was made to deploy the anti-spin parachute. After repeated unsuccessful attempts to deploy the anti-spin parachute, and when the airplane's altitude reached about 500 ft above the briefed minimum bailout altitude, both pilots called for and executed a bailout. The airplane impacted the ground and was destroyed. A postaccident examination of the anti-spin parachute system revealed that half of the connector hook had opened, which allowed the activation pin lanyard for the anti-spin parachute to become disengaged. Based on the airplane's previous aberrant behavior and the conservative parameters that the CDE had previously set, it is not likely that the CDE would have authorized abused spin entries without a prior testing buildup to those entries. Thus, the flight crew made an inappropriate decision to introduce flaps landing entry spin testing, and the failure of the anti-spin parachute contributed to the accident.
Probable cause:
The flight crew's inappropriate decision, without authorization or consultation from the manufacturer's chief design engineer, to introduce flaps in the landing configuration into the entry spin testing, which resulted in an unrecoverable spin and impact with the ground. Contributing to the accident was the failure of the anti-spin parachute.
Final Report:

Crash of an AMI Turbo DC-3-65TP in Mojave

Date & Time: Feb 4, 2009 at 0852 LT
Type of aircraft:
Operator:
Registration:
N834TP
Flight Phase:
Flight Type:
Survivors:
Yes
Schedule:
Mojave - Mojave
MSN:
12590
YOM:
1947
Crew on board:
2
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
18000
Captain / Total hours on type:
1326.00
Aircraft flight hours:
17277
Circumstances:
During the takeoff roll, the airplane began to drift to the right. Despite the certified flight instructor's and student's attempts, they were unable to stop the yaw and drift. As the airplane was about to depart the runway, the pilots did not reduce the throttles or apply brakes as they felt that it would be safer to attempt to get airborne. After departing the runway surface, the airplane collided with a series of berms, which sheared off the left landing gear and left engine. The right landing gear collapsed, and the airplane came to rest in a nose down attitude. Post accident e examination revealed that the student pilot had inadvertently set the rudder trim to the full right position when he adjusted the rudder pedals during the prestart checks. The rudder trim was in the full right position for the takeoff, and found in the same position upon post accident inspection.
Probable cause:
The student pilot failed to follow the checklist and set the takeoff trim properly prior to takeoff resulting in a loss of directional control. Contributing to the accident were the certified flight instructor's inadequate supervision and delayed remedial action.
Final Report:

Crash of a Canadair CL-600-1A11 Challenger 600 in California City: 1 killed

Date & Time: Apr 3, 1980 at 0910 LT
Type of aircraft:
Operator:
Registration:
C-GCGR-X
Flight Phase:
Flight Type:
Survivors:
Yes
Site:
Schedule:
Mojave - Mojave
MSN:
1001
YOM:
1978
Crew on board:
3
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
1
Captain / Total flying hours:
7782
Captain / Total hours on type:
468.00
Circumstances:
The crew departed Mojave-Kern County Airport in the morning on a series of tests on this new Bombardier prototype. While in cruising altitude, the crew initiated an unscheduled stall when the airplane reached an angle of attack of 34°. Control was lost and the airplane entered a dive. All three crew members bailed out and the airplane crashed in a desert area. Two crew members were injured while the third occupant was killed as his parachute failed to open.
Probable cause:
Uncontrolled collision with ground following an emergency descent due to technical problems with instruments/equipment. The following contributing factors were reported:
- Flight and navigation instruments: angle of attack indicator,
- Binding,
- Hydraulic system: seals, deteriorated,
- Unknown failure in emergency chute jettison system.
Final Report:

Crash of a Douglas A-26A Invader in Chino

Date & Time: Feb 9, 1978 at 1300 LT
Type of aircraft:
Operator:
Registration:
N99218
Flight Type:
Survivors:
Yes
Schedule:
Mojave - Chino
MSN:
18796
YOM:
1943
Crew on board:
2
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
10000
Captain / Total hours on type:
1200.00
Circumstances:
On final approach to Chino Airport, the crew lost control of the airplane that crashed short of runway threshold. The aircraft was destroyed and both pilots were seriously injured. They were completing a ferry flight from Mojave.
Probable cause:
Loss of control on final approach after the n°2 propeller went into reverse thrust for undetermined reasons. The following contributing factors were reported:
- Thrust reversal unwanted,
- Material failure.
Final Report: