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Crash of a Cirrus Vision SF50 in Kissimmee

Date & Time: Sep 9, 2022 at 1502 LT
Type of aircraft:
Operator:
Registration:
N77VJ
Flight Type:
Survivors:
Yes
Schedule:
Miami - Kissimmee
MSN:
88
YOM:
2018
Crew on board:
1
Crew fatalities:
Pax on board:
2
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
982
Captain / Total hours on type:
325.00
Aircraft flight hours:
645
Circumstances:
The pilot obtained multiple preflight weather briefings that resulted in him delaying the flight’s departure until the afternoon. After departure, while near his intended destination, the pilot was twice advised by air traffic controllers of adverse weather, including heavy to extreme precipitation along the intended final approach. While in visual meteorological conditions the pilot requested an RNAV approach to his destination airport. While flying towards the final approach fix at a low thrust setting the autopilot attempted to maintain 2,000 ft while pitching up and slowing to about 100 knots, causing an airspeed aural warning. The pilot applied partial thrust and while in instrument meteorological conditions the flight encountered extreme precipitation and turbulence associated with the previously reported thunderstorm. The pilot turned off the autopilot; the airplane then climbed at a rate that was well beyond the performance capability of the airplane, likely caused by updrafts from the mature thunderstorm and application of takeoff thrust. The High Electronic Stability & Protection (ESP) engaged, pitching the airplane nose-down coupled with the pilot pushing the control stick forward. The airplane then began descending followed by pitching up and climbing again. The pilot pulled the Cirrus Airframe Parachute System (CAPS) and descended under canopy into a marsh but the airplane was dragged a short distance from wind that inflated the CAPS canopy. Post accident examination of the recovered airplane revealed substantial damage to the front pressure bulkhead and to both sides of the fuselage immediately behind the front pressure bulkhead. There was no evidence of preimpact failure or malfunction of the flight controls for roll, pitch, or yaw. Data downloaded from the Recoverable Data Module (RDM) revealed no faults with the autopilot or stability protection systems until the CAPS system was activated, when those recorded faults would have been expected. Further, there were no discrepancies with the engine. Although the pilot perceived a malfunction of the autopilot at several times during the final portion of the flight, the perceived autopilot discrepancies were likely normal system responses based on the autopilot mode changes.
Probable cause:
The pilot’s continuation of the instrument approach into known extreme precipitation and turbulence associated with a thunderstorm, resulting in excessive altitude deviations that required him to activate the Cirrus Airframe Parachute System.
Final Report:

Crash of a Piper PA-46-350P Malibu off Mayport: 2 killed

Date & Time: Dec 20, 2018 at 0904 LT
Registration:
N307JM
Flight Phase:
Flight Type:
Survivors:
No
Schedule:
Kissimmee - Princeton
MSN:
46-36253
YOM:
2000
Location:
Crew on board:
1
Crew fatalities:
Pax on board:
1
Pax fatalities:
Other fatalities:
Total fatalities:
2
Captain / Total flying hours:
390
Captain / Total hours on type:
30.00
Aircraft flight hours:
3785
Circumstances:
The aircraft impacted the Atlantic Ocean near Mayport, Florida. The private pilot and pilot-rated passenger were fatally injured. The airplane was destroyed. The airplane was privately owned and operated under the provisions of Title 14 Code of Federal Regulations Part 91. Instrument meteorological conditions prevailed at the time and the flight was operating on an instrument flight rules (IFR) flight plan. The personal flight originated from Kissimmee Gateway Airport, Orlando, Florida, about 0821, and was destined for Princeton Airport, Princeton/Rocky Hill, NJ. According to preliminary air traffic control radar and voice data provided by the Federal Aviation Administration (FAA), at 0859:02, one of the airplane's occupants contacted the Jacksonville Air Route Traffic Control Center (ZJX ARTCC) R-73 sector controller and reported passing through Flight Level (FL) 220 for FL230. The controller advised the pilot there were moderate and some heavy precipitation along the route of flight extending for 200 nautical miles. The occupant acknowledged the controller and advised they would be watching the weather. FAA radar data indicated at 0900:22 the flight reached FL227. Preliminary review of weather data revealed that this altitude was above the freezing level, and at that time the flight entered an area of weather radar returns with intensities between 10 to 30 dBZ (which equated to light to moderate precipitation). While in the weather radar-indicated precipitation, the flight climbed to FL230. At 0902:14, while at the edge of the precipitation, the airplane started a slight left turn before entering a right turn at 0902:28 at FL226. The turn had not been directed by the controller or announced by either occupant. Between 0902:28 and 0903:10, the airplane descended from FL226 to FL202. At 0903:10, the airplane was descending through FL202 when the controller attempted to contact the flight, but there was no reply. The controller attempted to communicate with the flight several more times, and at 0903:27 in response to one attempt, while at 14,500 feet mean sea level (msl), an occupant advised, "were not ok we need help." The controller asked the pilot if he was declaring an emergency and "whats going on." At 0903:35, while at 12,600 feet msl an occupant stated, "I'm not sure whats happening", followed by, "I have anti-ice and everything." At 0903:40 the controller asked the flight if it could maintain altitude, an occupant responded that they could not maintain altitude. The controller provided vectors to a nearby airport west of their position, but the flight did not reply to that transmission or a subsequent query. At about 0904:32 (which was the last communication from the airplane), while at 3,300 feet msl, an occupant advised the controller that the airplane was inverted and asked for assistance. The last radar recorded position with altitude read-out of the flight was at 0904:40, at an altitude of 1,700 feet msl, and 30.40069° north latitude and -81.3844° west longitude. The U.S. Coast Guard initiated a search for the missing airplane, but the wreckage was not located and the search was suspended on December 22, 2018. A privately-funded search for the airplane was initiated and the wreckage was located and recovered on February 6, 2019. The recovered wreckage was retained for further investigation.
Probable cause:
An in-flight loss of control following an encounter with supercooled large droplet icing conditions, which ultimately resulted in an uncontrolled descent and subsequent inflight breakup. Also causal was the pilot’s failure to maintain an appropriate airspeed for flight in icing conditions.
Final Report:

Crash of a Beechcraft C90 King Air in Rockford

Date & Time: Dec 5, 2017 at 1802 LT
Type of aircraft:
Registration:
N500KR
Flight Type:
Survivors:
Yes
Schedule:
Kissimmee - Rockford
MSN:
LJ-708
YOM:
1977
Crew on board:
1
Crew fatalities:
Pax on board:
3
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
2500
Aircraft flight hours:
9856
Circumstances:
The private pilot departed on a cross-country flight in his high-performance, turbine-powered airplane with full tanks of fuel. He landed and had the airplane serviced with 150 gallons of fuel. He subsequently departed on the return flight. As the airplane approached the destination airport, the pilot asked for priority handling and reported that the airplane "lost a transfer pump and had a little less fuel than he thought," and he did not want to come in with a single engine. When asked if he needed assistance, he replied "negative." The pilot was cleared to perform a visual approach to runway 19 during night conditions. As the airplane approached the airport, the pilot requested the runway lights for runway 25 be turned on and reported that the airplane lost engine power in one engine. The controller advised that the lights on runway 25 were being turned on and issued a landing clearance. The airplane impacted terrain before the threshold for runway 25. During examination of the recovered wreckage, flight control continuity was established. No useable amount of fuel was found in any of the airplane's fuel tanks; however, fuel was observed in the fuel lines. All transfer pumps and boost pumps were operational. The engine-driven fuel pumps on both engines contained fuel in their respective fuel filter bowls. Both pumps were able to rotate when their input shafts were manipulated by hand. Disassembly of both pumps revealed that their inlet filters were free of obstructions. Bearing surfaces in both pumps exhibited pitting consistent with pump operation with inadequate fuel lubrication and fuel not reaching the pump. The examination revealed no evidence of airframe or engine preimpact malfunctions or failures that would have precluded normal operation of the airplane. Performance calculations using a flight planning method described in the airplane flight manual indicated that the airplane could have made the return flight with about 18 gallons (119 lbs) of fuel remaining. However, performance calculations using a fuel burn simulation method developed from the fuel burn and data from the airplane flight manual indicated that the airplane would have run out of fuel on approach. Regulations require that a flight depart with enough fuel to fly to the first point of intended landing and, assuming normal cruising speed, at night, to fly after that for at least 45 minutes. The calculated 45-minute night reserves required about 56 gallons (366 lbs) of fuel using a maximum recommended cruise power setting or about 37.8 gallons (246 lbs) of fuel using a maximum range power setting. Regardless of the flight planning method he could have used, the pilot did not depart on the accident flight with the required fuel reserves and exhausted all useable fuel while on approach to the destination. The airplane was owned by Edward B. Noakes III.
Probable cause:
The pilot's inadequate preflight planning and his decision to depart without the required fuel reserve, which resulted in fuel exhaustion during a night approach and subsequent loss of engine power.
Final Report:

Crash of a Piper PA-31-325 Navajo C/R in Tuscaloosa: 6 killed

Date & Time: Aug 14, 2016 at 1115 LT
Type of aircraft:
Registration:
N447SA
Flight Type:
Survivors:
No
Schedule:
Kissimmee – Oxford
MSN:
31-8312016
YOM:
1983
Crew on board:
1
Crew fatalities:
Pax on board:
5
Pax fatalities:
Other fatalities:
Total fatalities:
6
Captain / Total flying hours:
749
Captain / Total hours on type:
48.00
Aircraft flight hours:
3447
Circumstances:
The private pilot and five passengers departed on a day instrument flight rules cross-country flight in the multiengine airplane. Before departure, the airplane was serviced to capacity with fuel, which corresponded to an endurance of about 5 hours. About 1 hour 45 minutes after reaching the flight's cruise altitude of 12,000 ft mean sea level, the pilot reported a failure of the right engine fuel pump and requested to divert to the nearest airport. About 7 minutes later, the pilot reported that he "lost both fuel pumps" and stated that the airplane had no engine power. The pilot continued toward the diversion airport and the airplane descended until it impacted trees about 1,650 ft short of the approach end of the runway; a postimpact fire ensued. Postaccident examination of the airframe and engines revealed no preimpact failures or malfunctions that would have precluded normal operation. The propellers of both engines were found in the unfeathered position. All six of the fuel pumps on the airplane were functionally tested or disassembled, and none exhibited any anomalies that would have precluded normal operation before the accident. Corrosion was noted in the right fuel boost pump, which was likely the result of water contamination during firefighting efforts by first responders. The airplane was equipped with 4 fuel tanks, comprising an outboard and an inboard fuel tank in each wing. The left and right engine fuel selector valves and corresponding fuel selector handles were found in the outboard tank positions. Given the airplane's fuel state upon departure and review of fuel consumption notes in the flight log from the day of the accident, the airplane's outboard tanks contained sufficient fuel for about 1 hour 45 minutes of flight, which corresponds to when the pilot first reported a fuel pump anomaly to air traffic control. The data downloaded from the engine data monitor was consistent with both engines losing fuel pressure due to fuel starvation. According to the pilot's operating handbook, after reaching cruise flight, fuel should be consumed from the outboard tanks before switching to the inboard tanks. Two fuel quantity gauges were located in the cockpit overhead switch panel to help identify when the pilot should return the fuel selectors from the outboard fuel tanks to the inboard fuel tanks. A flight instructor who previously flew with the pilot stated that this was their normal practice. He also stated that the pilot had not received any training in the accident airplane to include single engine operations and emergency procedures. It is likely that the pilot failed to return the fuel selectors from the outboard to the inboard tank positions once the outboard tanks were exhausted of fuel; however, the pilot misdiagnosed the situation as a fuel pump anomaly.
Probable cause:
A total loss of power in both engines due to fuel starvation as a result of the pilot's fuel mismanagement, and his subsequent failure to follow the emergency checklist. Contributing to the pilot's failure to follow the emergency checklist was his lack of emergency procedures training in the accident airplane.
Final Report:

Crash of a De Havilland DHC-6 Twin Otter 200 in Palm Beach

Date & Time: Apr 5, 1999 at 0945 LT
Operator:
Registration:
N838MA
Survivors:
Yes
Schedule:
Palm Beach - Kissimmee
MSN:
188
YOM:
1968
Crew on board:
1
Crew fatalities:
Pax on board:
9
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
8000
Captain / Total hours on type:
200.00
Aircraft flight hours:
16659
Circumstances:
The pilot reported that prior to takeoff, he completed a preflight inspection of the airplane that included checking the engine oil quantity. The line personnel topped off the oil reservoirs, and reportedly secured the engine oil reservoir filler caps. Approximately two minutes into the flight, the right engine oil pressure warning light illuminated. The pilot informed Palm Beach Approach Control of the engine oil pressure problem, shut down the right engine, and returned to Lantana. As the flight approached runway 03, the pilot heard a radio transmission from another airplane taxiing for takeoff. As the pilot continued the approach, with full flaps extended, he elected to go-around 1500 feet from the approach end of the 3000-foot runway. The airplane collided with the ground during the go-around maneuver to runway 15. The wreckage examination also disclosed that the right cowling showed oil streaming back from behind the engine and onto the wing strut. Inspection of the oil filler cap revealed that it had not been properly installed.
Probable cause:
The pilot's failure to secure the engine oil filler cap during the preflight inspection that resulted the subsequent loss of engine power, and his in-flight decision to attempt a single engine go-around with full wing flaps extended.
Final Report:

Crash of a Beechcraft C90 King Air near Okeechobee: 10 killed

Date & Time: Jan 5, 1994 at 1829 LT
Type of aircraft:
Registration:
N230TW
Flight Type:
Survivors:
No
Schedule:
Kissimmee - Miami
MSN:
LJ-445
YOM:
1969
Crew on board:
1
Crew fatalities:
Pax on board:
9
Pax fatalities:
Other fatalities:
Total fatalities:
10
Captain / Total flying hours:
12000
Captain / Total hours on type:
130.00
Aircraft flight hours:
7072
Circumstances:
The pilot (or pilot-rated passenger) reported an 'indication' problem and said they intended to land at Okeechobee, but couldn't find the airport. They then reported engine trouble and said that they would try to land on a road. They circled the area and approached a dirt road with landing lights on. A car was proceeding on the road in the opposite direction. The plane began to climb, and it entered a left turn. It then rolled into a steep right bank, descended nose down, crashed and was consumed by fire. An exam revealed indications that both engines were operating at high rpm. A teardown revealed a right engine fuel control bearing had failed, which would have allowed improper movement of the fuel control drive shaft. The plane was last inspected on 11/25/92 and was 13 hours over a required 150 hour inspection. A service bulletin for maintenance of the fuel control bearings had not been complied with. The owner/pilot had not completed formal ground school instruction on the airplane systems and operation. The plane had 9 seats; 10 occupants were aboard.
Probable cause:
The pilot's improper remedial action concerning a right engine power anomaly, and his failure to maintain adequate airspeed during go-around from an aborted precautionary landing, which resulted in a loss of aircraft control and an uncontrolled descent. Factors related to the accident were: failure of the owner/operator/pilot to assure proper maintenance inspection of the aircraft, failure to comply with a service bulletin concerning the engine fuel controls, subsequent bearing failure in the right engine fuel control, and the pilot's lack of familiarity with this make and model of aircraft.
Final Report: