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Crash of a Rockwell Shrike Commander 500S in Eden Prairie

Date & Time: Apr 8, 2011 at 1730 LT
Operator:
Registration:
N51RF
Flight Type:
Survivors:
Yes
Schedule:
Eden Prairie - Eden Prairie
MSN:
500-3298
YOM:
1976
Crew on board:
2
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
473
Captain / Total hours on type:
217.00
Copilot / Total flying hours:
4659
Copilot / Total hours on type:
2480
Aircraft flight hours:
11298
Circumstances:
The pilot reported that he performed a stabilized visual approach with a right crosswind. The airplane touched down on the centerline and subsequently drifted to the right. The pilot overcorrected for the drift and the airplane veered hard to the left. The airplane continued off the left side of the runway and skidded to a complete stop. The right main landing gear collapsed and the right wingtip hit the ground, which resulted in substantial damage to the fuselage and wing. A postaccident inspection of the airplane revealed no preimpact anomalies. The pilot additionally reported that there was no mechanical malfunction or failure.
Probable cause:
The pilot's inadequate compensation for the crosswind while landing, which resulted in a loss of directional control.
Final Report:

Crash of a Beechcraft E18S in Eden Prairie: 2 killed

Date & Time: Aug 12, 2009 at 1145 LT
Type of aircraft:
Registration:
N3038C
Flight Phase:
Flight Type:
Survivors:
No
Schedule:
Eden Prairie - Osceola
MSN:
BA-374
YOM:
1958
Crew on board:
1
Crew fatalities:
Pax on board:
1
Pax fatalities:
Other fatalities:
Total fatalities:
2
Captain / Total flying hours:
1150
Captain / Total hours on type:
0.00
Aircraft flight hours:
10626
Circumstances:
The pilot purchased the airplane approximately one year prior to the accident with the intention of restoring it for flight. The airplane had not been flown for approximately five years and had been used for spare parts. The pilot was flying the airplane to another airport to pick up passengers prior to returning. The pilot was cleared for takeoff and to circle the airport at 2,500 feet prior to departing the area. Witnesses reported that after taking off the airplane seemed to “wobble” at a slow airspeed in a nose-high attitude and that it never got higher than 500 feet. Some witnesses reported the engine(s) sputtering, and another stated that the airplane was loud and "didn't sound good," although other witnesses reported that the engines sounded normal. One witness reported seeing white smoke coming from the left engine and hearing the engine "popping" as the airplane took off. The airplane made three left turns and it appeared as if the pilot was attempting to return to land. Witnesses described the left wing rising prior to the airplane banking hard to the left and the nose dropping straight down. The airplane impacted the ground just northeast of the airport property and a postimpact fire ensued. Flight control continuity was established. The right side of the elevator/tailcone structure exhibited black rub marks and scrapes. Grass and nesting material was found inside the left wing. The left fuel valve was found in the OFF position and the right fuel valve was positioned to the rear auxiliary tank. Neither the fuel crossfeed valve nor the fuel boost pump switch was located. The left engine sustained substantial fire and impact damage. The right engine sustained heavy impact damage. The airplane was last fueled one month prior to the accident with 120 gallons of fuel. About 20 engine test runs in addition to high-speed taxi tests had been conducted since then. A Special Flight Permit had been obtained but had not been signed by the mechanic, who did not know that the pilot was going to fly the airplane on the day of the accident. The pilot reportedly did not have any Beech 18 flight experience.
Probable cause:
The pilot’s lack of experience flying the accident make and model of airplane, which led to a loss of control while maneuvering to return to the airport. Contributing to the accident was a partial loss of engine power for undetermined reasons.
Final Report:

Crash of a Beechcraft A100 King Air in Colorado Springs: 2 killed

Date & Time: Dec 21, 1997 at 0626 LT
Type of aircraft:
Operator:
Registration:
N100BE
Survivors:
Yes
Schedule:
Eden Prairie - Colorado Springs
MSN:
BB-221
YOM:
1976
Crew on board:
1
Crew fatalities:
Pax on board:
2
Pax fatalities:
Other fatalities:
Total fatalities:
2
Captain / Total flying hours:
3400
Captain / Total hours on type:
65.00
Aircraft flight hours:
8651
Circumstances:
The pilot was cleared for an ILS DME approach to runway 17L. During the final stage of the approach, the aircraft entered fog and disappeared from view of the control tower personnel. Radar and radio communications were lost also. After searching for 31 minutes, the aircraft was found by airport operations personnel over half way down the runway and 600 feet east of the runway. There was no evidence the aircraft touched down on the runway. The aircraft was configured with the landing gear up and the flaps deployed. Missed approach procedures require the flaps and landing gear to be retracted after initiating the procedure. The decision
height for the approach is 6,384 feet msl (200 feet above ground level) and the required RVR for a 14 CFR Part 135 flight to commence and approach is 2400 (1/2 mile). When on the glide slope, the decision height is 0.4 miles from the runway touchdown zone. Examination of the airplane did not disclose evidence of mechanical malfunction.
Probable cause:
Failure of the pilot to follow IFR Procedures and maintain the minimum descent altitude (MDA). A related factor was fog.
Final Report: