Crash of a Swearingen SA226AC Metro II in Norway House

Date & Time: Nov 8, 2006 at 0834 LT
Type of aircraft:
Operator:
Registration:
C-FTNV
Survivors:
Yes
Schedule:
Winnipeg – Norway House
MSN:
TC-239E
YOM:
1977
Flight number:
PAG105
Country:
Crew on board:
2
Crew fatalities:
Pax on board:
7
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
6000
Captain / Total hours on type:
4500.00
Copilot / Total flying hours:
4000
Copilot / Total hours on type:
15
Circumstances:
The aircraft was on a flight from Winnipeg, Manitoba, to Norway House, Manitoba, with two crew members and seven passengers on board. After touchdown on Runway 05, when propeller reverse was selected, the aircraft veered to the left. The crew attempted to regain directional control; however, the aircraft departed the left side of the runway surface, entered an area of loose snow, traversed a shallow ditch, climbed a rocky embankment, and came to rest on its belly with all three landing gears collapsed. The crew and passengers exited the aircraft through the main door stairway and the over-wing exits. There were no reported injuries. The accident occurred during daylight hours at 0834 central standard time.
Probable cause:
Findings as to Causes and Contributing Factors:
1. The left engine fuel control support assembly failed in fatigue and released one of three attachment bolts, which resulted in a slight displacement of the fuel control and changed the propeller control dimension. As a result, Beta pressure was achieved and propeller reverse was available for the left engine before it was available for the right engine.
2. The pilot selected thrust reverse without confirmation that the Beta lights were on for both engines, and the aircraft veered from the runway, most likely as a result of temporary asymmetric thrust.
Finding as to Risk:
1. There is no requirement to include the Beta light call as part of the pre-landing briefing. Briefing this item would remind the pilots of the need to confirm Beta light activation for both engines before application of thrust reverse.
Final Report:

Crash of a Cessna 208B Super Cargomaster in Winnipeg: 1 killed

Date & Time: Oct 6, 2005 at 0543 LT
Type of aircraft:
Operator:
Registration:
C-FEXS
Flight Phase:
Flight Type:
Survivors:
No
Schedule:
Winnipeg – Thunder Bay
MSN:
208B-0542
YOM:
1996
Flight number:
FDX8060
Country:
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
1
Captain / Total flying hours:
4570
Captain / Total hours on type:
1500.00
Aircraft flight hours:
6724
Circumstances:
On the day before the occurrence, the accident aircraft arrived in Winnipeg, Manitoba, on a flight from Thunder Bay, Ontario. The aircraft was parked in a heated hangar overnight and was pulled outside at about 0410 central daylight time. The pilot reviewed the weather information and completed planning for the flight, which was estimated to take two hours and six minutes. The aircraft was refuelled and taxied to Apron V at the Winnipeg International Airport, where it was loaded with cargo. After loading was complete, the pilot obtained an instrument flight rules (IFR) clearance for the flight to Thunder Bay, taxied to Runway 36, received take-off clearance, and departed. The aircraft climbed on runway heading for about one minute to an altitude of 1300 feet above sea level (asl), 500 feet above ground level (agl). The flight was cleared to 9000 feet asl direct to Thunder Bay, and the pilot turned on course. The aircraft continued to climb, reaching a maximum altitude of 2400 feet asl about 2.5 minutes after take-off. The aircraft then started a gradual descent averaging about 400 feet per minute (fpm) until it descended below radar coverage. The accident occurred during hours of darkness at 0543. The Winnipeg Fire Paramedic Service were notified and responded from a nearby station.
Probable cause:
Findings as to Causes and Contributing Factors:
1. The aircraft departed at a weight exceeding the maximum take-off weight and the maximum weight for operation in icing conditions.
2. After departure from Winnipeg, the aircraft encountered in-flight icing conditions in which the aircraftís performance deteriorated until the aircraft was unable to maintain altitude.
3. During the attempt to return to the Winnipeg International Airport, the pilot lost control of the aircraft, likely with little or no warning, at an altitude from which recovery was not possible.
Findings as to Risk:
1. Aviation weather forecasts incorporate generic icing forecasts that may not accurately predict the effects of icing conditions on particular aircraft. As a result, specific aircraft types may experience more significant detrimental effects from icing than forecasts indicate.
2. Bulk loading prevented determining the cargo weight in each zone, resulting in a risk that the individual zone weight limits could have been exceeded.
3. The aircraftís centre of gravity (CG) could not be accurately determined, and may have been in the extrapolated shaded warning area on the CG limit chart. Although it was determined that the CG was likely forward of the maximum allowable aft CG, bulk loading increased the risk that the CG could have exceeded the maximum allowable aft CG.
4. The incorrect tare weight on the Toronto cargo container presented a risk that other aircraft carrying cargo from that container could have been inadvertently overloaded.
Other Findings:
1. The pilotís weather information package was incomplete and had to be updated by a telephone briefing.
2. The operatorís pilots were not pressured to avoid using aircraft de-icing facilities or to depart with aircraft unserviceabilities.
3. The aircraft departed Winnipeg without significant contamination of its critical surfaces.
4. The biological material on board the aircraft was disposed of after the accident, with no indication that any of the material had been released into the ground or the atmosphere.
5. The fact that the aircraft was not equipped with flight data recorder or cockpit voice recorder equipment limited the information available for the occurrence investigation and the scope of the investigation.
Final Report:

Crash of a Swearingen SA226TC Metro II in Thompson

Date & Time: May 10, 2005 at 1030 LT
Type of aircraft:
Operator:
Registration:
C-FKEX
Survivors:
Yes
Schedule:
York Landing – Thompson
MSN:
TC-332
YOM:
1980
Country:
Crew on board:
2
Crew fatalities:
Pax on board:
15
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
erimeter Aviation flight 914, a Metro II with 17 people on board, was on approach at Thompson, MB. The first officer flew the aircraft during the approach, and encountered turbulence and fluctuating airspeed. The captain took control at 200 feet agl. The aircraft was high and left of centreline. The captain added power, continued the approach and landed hard on runway 23 near the intersection with runway 32. After the aircraft arrived at the apron, a fuel leak was noted. The aircraft was inspected and damage was found in the wheel wells, wing leading edge, engine mounts and a wing-fuselage attachment point. No injuries were reported. Reported winds at 1400Z were 010 at 15-20 kts; 1500Z winds were 350 at 9 kts.

Crash of a Piper PA-31-350 Navajo Chieftain in Winnipeg: 1 killed

Date & Time: Jun 11, 2002 at 0920 LT
Operator:
Registration:
C-GPOW
Survivors:
Yes
Site:
Schedule:
Gunisao Lake - Winnipeg
MSN:
31-7305093
YOM:
1973
Country:
Crew on board:
1
Crew fatalities:
Pax on board:
6
Pax fatalities:
Other fatalities:
Total fatalities:
1
Captain / Total flying hours:
3000
Circumstances:
The aircraft was on an instrument flight rules flight from Gunisao Lake, Manitoba, to Winnipeg. One pilot and six passengers were on board. At 0913 central daylight time, KEE208 began an instrument landing system approach to Runway 13 at Winnipeg International Airport. The captain flew the approach at a higher-than-normal approach airspeed and well above the glide path. When the aircraft broke out of the cloud layer, it was not in position to land safely on the remaining runway. The captain executed a missed approach at 0916 and, after switching to the approach frequency from tower frequency, requested an expedited return to the airport. The approach controller issued instructions for a turn back to the airport. Almost immediately, at 0918, the captain declared a 'Mayday' for an engine failure. Less than 20 seconds later the captain transmitted that the aircraft had experienced a double engine failure. The aircraft crashed at a major traffic intersection at 0920, striking traffic signals and several vehicles. All seven of the aircraft passengers and several of the vehicle occupants were seriously injured; one passenger subsequently died of his injuries. The aircraft experienced extensive structural damage, with the wings and engines tearing off along the wreckage trail. There was a small post-crash fire in the right wing and engine area.
Probable cause:
Findings as to Causes and Contributing Factors:
1. The pilot did not correctly calculate the amount of fuel required to accomplish the flight from Winnipeg to Gunisao Lake and return, and did not ensure that the aircraft carried sufficient fuel for the flight.
2. The ILS approach was flown above the glideslope and beyond the missed approach point, which reduced the possibility of a safe landing at Winnipeg, and increased the risk of collision with terrain.
3. During the missed approach, the aircraft's engines lost power as a result of fuel exhaustion, and the pilot conducted a forced landing at a major city intersection.
4. The pilot did not ensure that the aircraft was equipped with an autopilot as specified by CARs.
Findings as to Risk:
1. The company did not provide an adequate level of supervision and allowed the flight to depart without an autopilot.
2. The company operations manual did not reflect current company procedures.
3. The company did not provide an adequate level of supervision and allowed the flight to depart without adequate fuel reserves. The company did not have a safety system in place to prevent a fuel exhaustion situation developing.
Other Findings:
1. The pilot did not advise air traffic control of his critical situation in a timely fashion.
Final Report:

Crash of a Swearingen SA226TC Metro II in Shamattawa: 2 killed

Date & Time: Oct 11, 2001 at 2333 LT
Type of aircraft:
Operator:
Registration:
C-GYPA
Flight Type:
Survivors:
Yes
Schedule:
Gods Lake Narrows – Shamattawa
MSN:
TC-250
YOM:
1978
Flight number:
PAG962
Country:
Crew on board:
2
Crew fatalities:
Pax on board:
1
Pax fatalities:
Other fatalities:
Total fatalities:
2
Captain / Total flying hours:
3100
Captain / Total hours on type:
1100.00
Copilot / Total flying hours:
1200
Copilot / Total hours on type:
900
Circumstances:
Perimeter Airlines Flight PAG962, a Fairchild SA226TC (Metroliner), with two pilots and a flight nurse on board, departed Gods Lake Narrows, Manitoba, at approximately 2300 central daylight time, on a MEDEVAC flight to Shamattawa. Approaching Shamattawa, the crew began a descent to the 100 nautical mile minimum safe altitude of 2300 feet above sea level (asl) and, when clear of an overcast cloud layer at about 3000 feet asl, attempted a night, visual approach to Runway 01. The aircraft was too high and too fast on final approach and the crew elected to carry out a missed approach. Approximately 30 seconds after the power was increased, at 2333, the aircraft flew into trees slightly to the left of the runway centreline and about 2600 feet from the departure end of Runway 01. The aircraft was equipped with a cockpit voice recorder (CVR) that indicated the crew were in control of the aircraft; they did not express any concern prior to impact. The aircraft broke apart along a wreckage trail of about 850 feet. Only the cabin aft of the cockpit retained some structural integrity. The captain and first officer were fatally injured on impact. The flight nurse was seriously injured but was able to exit the wreckage of the cabin. A post-crash fire was confined to the wings which had separated from the cabin and cockpit wreckage.
Probable cause:
Findings as to Causes and Contributing Factors:
1. The aircraft was flown into terrain during an overshoot because the required climb angle was not set and maintained to ensure a positive rate of climb.
2. During the go-around, conditions were present for somatogravic illusion, which most likely led to the captain losing situational awareness.
3. The first officer did not monitor the aircraft instruments during a critical stage of flight; it is possible that he was affected by somatogravic illusion and/or distracted by the non-directional
beacon to the extent that he lost situational awareness.
Other Findings:
1. The absence of approach aids likely decreased the crew=s ability to fly an approach from which a landing could be executed safely.
2. The company standard operating procedures (SOPs) did not define how positive rate is to be determined.
Final Report:

Crash of a De Havilland DHC-3 Otter in Lake Stevens

Date & Time: Aug 2, 2000
Type of aircraft:
Operator:
Registration:
C-FMAJ
Flight Phase:
Survivors:
Yes
MSN:
383
YOM:
1960
Country:
Crew on board:
1
Crew fatalities:
Pax on board:
2
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
A DHC-3 and a Cessna 185 (both float equipped aircraft) had been chartered to move equipment from an outpost camp which was being threatened by forest fires in the Tadoule Lake (Lac Brochet, MB) area. Takeoff was conducted in a westerly direction into light winds estimated to be 5 to 8 knots. Besides the pilot there were two passengers (the camp owner and his son), two 45 gallon drums of #2 gas, a propane cylinder, battery chargers plus other sundry items. It was reported that once the aircraft was airborne, a windshift occurred which may have resulted in rollover and a downdraft situation. The aircraft began to descend, despite the application of full engine power, and settled into the trees with little forward speed and the wings in a near level attitude. The aircraft was then consumed by fire, the pilot and his two passengers were able to escape with minor scrapes and bruises. The pilot of the Cessna 185 witnessed the accident while airborne and he then returned and landed and rendered assistance to the three occupants. The local temperature was 27 degrees C, and the aircraft was near its maximum gross weight. It was reported that the aircraft had a headwind in proximity to the forest fire on takeoff, and that it flew into the area of a tailwind during initial climb.

Crash of a Piper PA-31-350 Navajo Chieftain in Princess Harbor

Date & Time: Aug 29, 1999 at 1532 LT
Operator:
Registration:
C-GHMK
Flight Phase:
Survivors:
Yes
Schedule:
Saint Andrews - Berens River
MSN:
31-7952120
YOM:
1979
Country:
Crew on board:
1
Crew fatalities:
Pax on board:
10
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
The Piper PA-31-350 Navajo, C-GHMK, departed from St. Andrews, Manitoba, on a visual flight rules charter flight to Berens River. One pilot and ten passengers, including one infant, were on board, and a dog was stowed in the baggage compartment behind the right, rear seat. At approximately 1530 central daylight saving time (CDT), while the aircraft was at an altitude of about 2 500 feet and about 30 nautical miles south of Berens River, the pilot heard a loud sound from the left engine. He saw deformation of the left engine cowling and smoke coming from the engine, and the aircraft yawed to the left. Part of the engine cowling departed in flight. The pilot could not pull the left propeller lever beyond half of its normal travel, nor could he move it into the feather position. He set maximum power on the right engine, but the aircraft did not maintain altitude. The pilot advised company dispatch over the radio that he would attempt a forced landing, then force landed in a mossy marsh area. Everyone on board, including the dog, deplaned. Five of the passengers sustained minor injuries during the evacuation. A fire ensued, completely destroying the aircraft except for the empennage aft of the horizontal stabilizers.
Probable cause:
Findings as to Causes and Contributing Factors:
1. The number three cylinder lower forward through stud was missing its base nut, which allowed the lower rear base nut of the number two cylinder to loosen.
2. The missing base nut of the through stud indicates that the base nut did not have sufficient clamping force; however, it could not be determined if the base nut did not receive the required torque during installation or if the base nut lost its clamping force during engine operation.
3. The d-inch studs and the 2-inch through studs of the number two cylinder failed in fatigue, and the number two cylinder of the left engine separated from the crankcase.
4. The left propeller could not be feathered because of interference between the propeller governor control and the separated number two cylinder.
5. The drag from the unfeathered left propeller and the deformed left engine cowling resulted in the aircraft being incapable of maintaining its altitude.
Other Findings:
1. The pilot was certified and qualified for the accident flight.
2. The aircraft's weight and balance were within the specified limits at the time of the accident.
3. The ELT was not readily accessible without tools.
Final Report:

Crash of a De Havilland DHC-3 Otter in Long Haul Lake: 1 killed

Date & Time: Jun 25, 1999 at 1320 LT
Type of aircraft:
Operator:
Registration:
C-FIFP
Flight Phase:
Flight Type:
Survivors:
Yes
MSN:
73
YOM:
1955
Country:
Crew on board:
1
Crew fatalities:
Pax on board:
1
Pax fatalities:
Other fatalities:
Total fatalities:
1
Aircraft flight hours:
23960
Circumstances:
The Blue Water Aviation Services seaplane departed from Long Haul Lake, Manitoba, with a pilot and an aviation maintenance engineer on board. Shortly after take-off, at 1320 central daylight savings time, the aircraft's engine abruptly lost power. The pilot's attempts to restart the engine were unsuccessful, and the aircraft descended into a stand of trees and struck the ground. The engineer suffered fatal injuries, and the pilot was seriously injured. The aircraft was destroyed by impact forces.
Probable cause:
Findings as to Causes and Contributing Factors:
1. The most likely accident scenario during the second take-off is that water contamination migrated from the centre fuel tank to the engine, resulting in a loss of engine power.
2. The engine stopped at a point from which there was insufficient time for the engine to restart, nor from which a safe landing could be made.
3. Indications of water contamination were found in the fuel system after the occurrence; however, the source(s) of the water contamination could not be identified.
Other Findings:
1. Examination of the aircraft and testing of the engine and components did not identify any pre-occurrence structural, mechanical, or electrical defects or malfunctions that would have
contributed to this occurrence.
2. The post-crash fire in the carburettor most likely resulted from uncontaminated fuel brought forward by the windmilling engine and the pilot's efforts to clear contamination from the fuel
system.
3. The pilot's use of his shoulder harness likely prevented more serious injuries during the impact sequence.
4. The engineer's injuries likely would have been less severe had he been using both his seat belt and shoulder harness.
5. The pilot was certified and qualified for the flight.
6. The aircraft's weight and centre of gravity were within approved limits.
7. The aircraft's records indicated that the aircraft had been certified and maintained in accordance with existing regulations.
8. The aircraft's engine power loss during the first attempted take-off was likely due to water contamination in the fuel.
Final Report:

Crash of an Embraer EMB-110P1 Bandeirante in Little Grand Rapids: 4 killed

Date & Time: Dec 9, 1997 at 1526 LT
Operator:
Registration:
C-GVRO
Survivors:
Yes
Schedule:
Winnipeg - Little Grand Rapids
MSN:
110-285
YOM:
1980
Flight number:
4K301
Country:
Crew on board:
2
Crew fatalities:
Pax on board:
15
Pax fatalities:
Other fatalities:
Total fatalities:
4
Captain / Total flying hours:
15000
Captain / Total hours on type:
114.00
Copilot / Total flying hours:
700
Copilot / Total hours on type:
367
Aircraft flight hours:
13724
Circumstances:
The Sowind Air Ltd. Embraer EMB-110P1 Bandeirante aircraft departed the operator's base at St. Andrews, Manitoba, with a crew of 2 and 15 passengers, on a 40-minute, scheduled flight to Little Grand Rapids, Manitoba. The aircraft arrived at Little Grand Rapids, and the crew flew an instrument approach to the airport and executed a missed approach because the required visual reference was not established. A second instrument approach was attempted. Ground-based witnesses observed the aircraft very low over the lake to the south of the airport and to the east of the normal approach path. Passengers in the aircraft also reported being very low over the lake and to the east of the normal approach path. The passengers described an increase in engine power followed by a rapid series of steep banking manoeuvres after the aircraft crossed the shoreline to the southeast of the airport. During the manoeuvres, the aircraft descended into the trees and crashed approximately 400 feet south and 1 600 feet east of the approach to runway 36 at Little Grand Rapids. The captain and three passengers were fatally injured, and the first officer and the remaining 12 passengers were seriously injured.
Probable cause:
Findings as to Causes and Contributing Factors:
1. At the time of the occurrence, the base of the cloud at Little Grand Rapids was between 100 and 300 feet agl, with fog to the east of the airport, and the visibility was one to two miles.
2. The aircraft was flown in marginal weather at low level, below the minimum en route altitude for commuter operations and below the MDA for the NDB A approach at Little Grand Rapids. The MDA for the approach was 1 560 feet asl, 555 feet above the airport elevation.
3. While the aircraft was being manoeuvred at very low level in marginal weather, it descended after an abrupt turn, and flew, in controlled flight, into the terrain.
Other Findings:
1. At both take-off and landing, the aircraft was about 1 000 pounds heavier than the relevant maximum allowable weight.
2. The GPS installed in C-GVRO was not approved as a primary navigational aid. The available information indicates that the flight crew used the GPS as a primary navigational aid during the last approach to Little Grand Rapids.
3. The aircraft was not equipped with a GPWS, nor was it required to be by regulation.
4. The weight and balance report that was submitted to Transport Canada, required for the importation of C-GVRO, contained numerous discrepancies; the report was not reviewed for accuracy by Transport Canada.
5. The emergency locator transmitter (ELT) produced a very weak signal because the antenna cable had been installed with little slack, and it pulled out of the antenna fitting during impact.
6. It could not be determined whether the presence of carbon monoxide and diphenhydramine in the captain's body affected his decision making and level of alertness.
7. The company, which had been an air taxi operator, did not effectively manage either the addition of the more complex commuter operations or the introduction of the larger Bandeirante aircraft.
8. The difficulty that the company had in the transition to commuter operations and in the introduction of the Bandeirante aircraft was underestimated by Transport Canada.
9. There were inadequacies in TC=s oversight, whereby the post-certification audit of the company was not conducted, thus eliminating an important mechanism by which TC could have found, and addressed, the inadequate safety management practices, non-conformance with pilot training requirements, and related operating irregularities.
10. The pilots had passed their flying proficiency and medical tests, but they had not completed elements of pilot training requirements with respect to servicing and operational control and right seat conversion as prescribed by TC. Also, no company pilot had received required training in the use of onboard survival or emergency equipment.
11. There was no indication found of any pre-impact failure or malfunction of the airframe, flight controls, or engines.
12. The aircraft was not equipped with either a CVR or an FDR; TC had given the company an exemption to operate without a CVR until 01 August 1998, and the aircraft was not required to be equipped with an FDR.
13. The absence of recorders on this aircraft, which was configured to carry 20 people, left many of the otherwise ascertainable facts associated with the accident unknown and reduced the opportunity of uncovering risks to safety associated with the flight.
14. Conditions were conducive to the pilot experiencing a false sensation that the aircraft was climbing (somatogravic illusion) after increasing the engine power, and he may have been manoeuvring to avoid an abandoned fire tower.
Final Report:

Crash of a Swearingen SA226TC Metro II in Island Lake

Date & Time: Nov 2, 1997 at 1257 LT
Type of aircraft:
Operator:
Registration:
C-FNKN
Survivors:
Yes
Schedule:
Winnipeg - Island Lake
MSN:
TC-296
YOM:
1979
Country:
Crew on board:
2
Crew fatalities:
Pax on board:
9
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
Following a firm touchdown on a gravel airstrip at Island Lake Airport, the crew heard a noise when the left wing dropped. Suspecting a left main gear failure, the captain initiated a go-around procedure and decided to divert to another airport with better facilities. Shortly later, the hydraulic pressure was lost and fuel quantity began to drop rapidly. The crew decided to return to land at Island Lake. Upon touchdown, the left main gear collapsed and the aircraft veered off runway to the left before coming to rest. All 11 occupants escaped uninjured while the aircraft was damaged beyond repair. slid off the runway. The pilot reported a very strong cross wind and that he touched down with crab.
Probable cause:
The left main gear drag links may have failed in overload.