Crash of a Rockwell Shrike Commander 500S off Horn Island: 1 killed

Date & Time: Feb 24, 2011 at 0800 LT
Operator:
Registration:
VH-WZU
Flight Type:
Survivors:
No
Schedule:
Cairns - Horn Island
MSN:
3060
YOM:
1970
Country:
Region:
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
1
Captain / Total flying hours:
4154
Captain / Total hours on type:
209.00
Aircraft flight hours:
17545
Circumstances:
At 0445 Eastern Standard Time on 24 February 2011, the pilot of an Aero Commander 500S, registered VH-WZU, commenced a freight charter flight from Cairns to Horn Island, Queensland under the instrument flight rules. The aircraft arrived in the Horn Island area at about 0720 and the pilot advised air traffic control that he intended holding east of the island due to low cloud and rain. At about 0750 he advised pilots in the area that he was north of Horn Island and was intending to commence a visual approach. When the aircraft did not arrive a search was commenced but the pilot and aircraft were not found. On about 10 October 2011, the wreckage was located on the seabed about 26 km north-north-west of Horn Island.
Probable cause:
The ATSB found that the aircraft had not broken up in flight and that it impacted the water at a relatively low speed and a near wings-level attitude, consistent with it being under control at impact. It is likely that the pilot encountered rain and reduced visibility when manoeuvring to commence a visual approach. However, there was insufficient evidence available to determine why the aircraft impacted the water.
Several aspects of the flight increased risk. The pilot had less than 4 hours sleep during the night before the flight and the operator did not have any procedures or guidance in place to minimize the fatigue risk associated with early starts. In addition, the pilot, who was also the operator’s chief pilot, had either not met the recency requirements or did not have an endorsement to conduct the types of instrument approaches available at Horn Island and several other locations frequently used by the operator.
Final Report:

Crash of a Pilatus PC-12/47 off Plettenberg Bay: 9 killed

Date & Time: Feb 8, 2011 at 1633 LT
Type of aircraft:
Registration:
ZS-GAA
Survivors:
No
Schedule:
Queenstown - Plettenberg Bay
MSN:
858
YOM:
2007
Country:
Region:
Crew on board:
2
Crew fatalities:
Pax on board:
7
Pax fatalities:
Other fatalities:
Total fatalities:
9
Captain / Total flying hours:
2662
Captain / Total hours on type:
582.00
Copilot / Total flying hours:
351
Copilot / Total hours on type:
112
Aircraft flight hours:
1096
Circumstances:
The aircraft, which was operated under the provisions of Part 91 of the Civil Aviation Regulations (CARs), departed from Queenstown Aerodrome (FAQT) at 1329Z on an instrument flight plan for Plettenberg Bay Aerodrome (FAPG). On board the aircraft were two (2) crew members and seven (7) passengers. The estimated time of arrival for the aircraft to land at FAPG was 1430Z, however the aircraft never arrived at its intended destination, nor did the crew cancel their search and rescue as per flight plan/air navigation requirements. At ±1600Z an official search for the missing aircraft commenced. The search was coordinated by the Aeronautical Rescue Co-ordination Centre (ARCC). The first phase of the search, which was land based, was conducted in the Robberg Nature Reserve area. Progress was slow due to poor visibility associated with dense mist and night time. A sea search was not possible following activation of the official search during the late afternoon and night time, but vessels from the National Sea Rescue Institute (NSRI) were able to launch at first light the next morning. Floating debris (light weight material) was picked up from the sea and along the western shoreline of the Robberg Nature Reserve where foot patrols were conducted. On 11 February 2011 the South African Navy joined the search for the missing wreckage by utilizing side scan sonar equipment to scan the sea bed for the wreckage. All the occupants on board the aircraft were fatally injured in the accident.
Probable cause:
The aircraft crashed into the sea following a possible in flight upset associated with a loss of control during IMC conditions.
The following contributory factors were identified:
- Deviation from standard operating procedures by the crew not flying the published cloud-break procedure for runway 30 at FAPG, but instead opted to attempt to remain visual with the ground/sea (comply with VMC requirements) by descending over the sea and approaching the aerodrome from the southeast (Robberg Nature Reserve side).
- Inclement weather conditions prevailed in the area, which was below the minima to comply with the approved cloud-break procedure for runway 30 at FAPG (minimum safety altitude of 844 feet according to cloud-break procedure) as published at the time of the accident.
- Judgement and decision making lacking by the crew. (The crew continued from the seaward side with the approach during IMC conditions and not diverting to an alternative aerodrome with proper approach facilities timeously although a cell phone call in this regard indicate such an intention).
- The possibility that the pilot-flying at the time became spatially disorientated during the right turn while encountering / entering IMC conditions in an attempt to divert to FAGG should be regarded as a significant contributory factor to this accident.
- This was the first time as far as it could be determined that the two crew members flew together.
Final Report:

Crash of a Piper PA-61 Aerostar (Ted Smith 601) in Falaise Lake

Date & Time: Dec 22, 2010 at 1350 LT
Operator:
Registration:
C-FMLI
Flight Phase:
Flight Type:
Survivors:
Yes
Schedule:
Yellowknife – Fort Saint John
MSN:
61-0589-7963259
YOM:
1979
Country:
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
The twin engine aircraft was en route from Yellowknife, NT to Fort St. John, BC. The pilot noticed fumes and smoke coming from behind the rear cabin wall. The cabin was depressurized and the door opened to clear the smoke. A forced landing was conducted onto the frozen surface of Falaise Lake, NT. The pilot immediately egressed, however, the aircraft was soon engulfed in flames and was completely consumed. The pilot was not injured and was flown out by helicopter.

Crash of a Beechcraft C-45 Expeditor off Nassau: 2 killed

Date & Time: Dec 14, 2010 at 1510 LT
Type of aircraft:
Operator:
Registration:
N38L
Flight Type:
Survivors:
No
Schedule:
Fort Lauderdale – Nassau
MSN:
6323
YOM:
1944
Country:
Crew on board:
2
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
2
Circumstances:
While approaching Nassau-Lynden Pindling Airport runway 27 in poor weather conditions (cold front), the twin engine aircraft crashed into the sea few km offshore. Some debris were found floating on water north of Nassau. Both pilots were killed.

Crash of a Piper PA-46-350P Malibu Mirage in the Gulf of Mexico

Date & Time: Dec 4, 2010 at 1430 LT
Operator:
Registration:
N350MM
Flight Phase:
Flight Type:
Survivors:
Yes
Schedule:
Cozumel – New Orleans
MSN:
46-22105
YOM:
1990
Country:
Region:
Crew on board:
2
Crew fatalities:
Pax on board:
2
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
1593
Captain / Total hours on type:
516.00
Copilot / Total flying hours:
7000
Copilot / Total hours on type:
750
Aircraft flight hours:
2936
Circumstances:
About 2 hours into a cross-country flight over water, the pilot heard a noticeable change in engine noise and observed erratic engine torque readings. Moments later the airplane experienced a complete loss of engine power. After declaring an emergency, the pilot attempted to diagnose the problem and restart the engine to no avail. The airplane ditched 175 miles from land, in water over 5,000 feet deep. The airplane was not recovered and the reason for the loss of engine power could not be determined.
Probable cause:
A total loss of engine power for undetermined reasons.
Final Report:

Crash of a Beechcraft A65 Queen Air near Tuguegarao

Date & Time: Nov 29, 2010 at 1330 LT
Type of aircraft:
Registration:
RP-C1111
Flight Phase:
Flight Type:
Survivors:
Yes
Schedule:
Basco – Tuguegarao
MSN:
LC-270
YOM:
1968
Country:
Region:
Crew on board:
2
Crew fatalities:
Pax on board:
11
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
En route from Basco to Tuguegarao, the crew encountered technical problems and elected to divert to the nearest airport for an emergency landing. The twin engine aircraft stalled and crashed in a river. All 13 occupants, among them two children, evacuated safely. The aircraft damaged beyond repair.

Crash of a Piper PA-46-350P Malibu Mirage off Destin: 3 killed

Date & Time: Nov 23, 2010 at 1930 LT
Registration:
N548C
Flight Type:
Survivors:
No
Schedule:
New Orleans – Destin
MSN:
46-36322
YOM:
2001
Crew on board:
1
Crew fatalities:
Pax on board:
2
Pax fatalities:
Other fatalities:
Total fatalities:
3
Captain / Total flying hours:
408
Captain / Total hours on type:
34.00
Aircraft flight hours:
761
Circumstances:
The instrument-rated pilot was executing a night instrument approach when the airplane impacted the water. The published approach minimums for the area navigation/global positioning system approach were 460-foot ceiling and one-mile visibility. Recorded air traffic control voice and radar data indicated that prior to the approach the pilot had turned to an approximately 180-degree heading and appeared to be heading in the direction of another airport. The controller reassigned the pilot a heading in order to intercept the final approach. The airplane was located in the water approximately 5,000 feet from the runway threshold. A postaccident examination of the airplane revealed that the left main landing gear was in the retracted position and the right main and nose landing gear were in the extended position. Examination of the left main landing gear actuator revealed no mechanical anomalies. The pilot had likely just commanded the landing gear to the down position and the landing gear was in transit. It is further possible that, as the gear was in transit, the airplane impacted the water in a left-wing and nose-down attitude and the left gear was forced to a gear-up position.
Probable cause:
Controlled flight into water due to the pilot's improper descent below the published minimum descent altitude.
Final Report:

Crash of a Piper PA-31-350 Navajo Chieftain off Aguadilla

Date & Time: Oct 27, 2010 at 1740 LT
Operator:
Registration:
N350RL
Flight Phase:
Flight Type:
Survivors:
Yes
Schedule:
Punta Cana - San Juan
MSN:
31-8252049
YOM:
1982
Country:
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
1902
Captain / Total hours on type:
38.00
Aircraft flight hours:
4736
Circumstances:
The pilot stated he experienced a high temperature in the right engine and a partial loss of engine rpm while at 9,000 feet mean sea level in cruise flight. He requested and received clearance from air traffic control to descend and divert to another airport. He leveled the airplane at 2,500 feet and both engines were operating; however, the right engine experienced a loss of rpm which made it difficult to maintain altitude. The pilot reduced power in both engines, turned the fuel boost pump on, opened the cowl flaps and the engine continued to run with a low rpm. The pilot elected to ditch the airplane in the ocean, instead of landing as soon as practical at the nearest suitable airport, as instructed in the Pilot's Operating Handbook (POH). Additionally, he shut down the right engine before performing the troubleshooting items listed in the POH. He attributed his decision to ditch the airplane to poor single-engine performance and windy conditions. The wind at the destination airport was from 060 degrees at 6 knots and runway 8 was in use at the time of the accident. The airplane was not recovered.
Probable cause:
The pilot's improper decision to ditch the airplane after a reported partial loss of engine power and overheat on one engine for undetermined reasons.
Final Report:

Crash of a Cessna 501 Citation I/SP off Coatzacoalcos: 8 killed

Date & Time: Oct 6, 2010 at 0745 LT
Type of aircraft:
Registration:
XA-TKY
Flight Phase:
Survivors:
No
Schedule:
Culiacán – Puebla – Minatitlán – Veracruz
MSN:
501-0029
YOM:
1977
Country:
Crew on board:
2
Crew fatalities:
Pax on board:
6
Pax fatalities:
Other fatalities:
Total fatalities:
8
Circumstances:
The aircraft departed Culiacán on a round trip to Veracruz with intermediate stops in Puebla and Minatitlán, carrying two pilots and six employees of the Coppel Company. One minute after takeoff from Minatitlán Airport, while in initial climb, the aircraft entered an uncontrolled descent and crashed in the sea off Coatzacoalcos. A day later, few debris were found on beaches. The main wreckage was not found and all eight occupants were killed.
Crew:
Javier Montoya,
Bernardo Estrada.
Passengers:
Salvador Leyva,
David Jurado,
Norma Torres,
Brenda Camacho,
Alejandro Quintero,
Freddy Peraza.

Crash of a Cessna 402C in Nassau: 9 killed

Date & Time: Oct 5, 2010 at 1236 LT
Type of aircraft:
Operator:
Registration:
C6-NLH
Flight Phase:
Survivors:
No
Schedule:
Nassau – Cockburn Town
MSN:
402C-0458
YOM:
1981
Country:
Crew on board:
2
Crew fatalities:
Pax on board:
7
Pax fatalities:
Other fatalities:
Total fatalities:
9
Captain / Total flying hours:
12000
Captain / Total hours on type:
10000.00
Circumstances:
On October 5, 2010 about 1636 UTC / 12:36pm Eastern Daylight Time (EDT), C6-NLH a Cessna 402C aircraft registered to Lebocruise Air Limited and operated by Acklins Blue Air Charter/Nelson Hanna crashed into lake Killarney shortly after becoming airborne from runway 14 at Lynden Pindling International Airport, Nassau, New Providence, Bahamas. The airplane sustained substantial damages by impact forces. The pilot, copilot and seven (7) passengers aboard the airplane received fatal injuries. The aircraft was on a passenger carrying flight from Lynden Pindling Intl Airport (MYNN) to Cockburn Town, San Salvador, Bahamas (MYSM). The aircraft was on a visual flight rules flight plan. Visual meteorological conditions prevailed at the time of the accident. The official notification of the accident was made to the Manager of the Flight Standards Inspectorate at Lynden Pindling Intl Airport, Nassau, N. P., Bahamas shortly thereafter. The investigation began the same day at approximately 1655 UTC upon notification of the IIC. The investigation was conducted by the Bahamas Civil Aviation Department [BCAD], Inspector Delvin R. Major (Investigator-in-Charge) of the Air Accident Investigation and Prevention Unit (AAIPU), Management of BCAD and Flight Standards Inspectorate (FSI), Airworthiness Inspectors, Operations Inspectors, Human Factors and other administrative staff. Valuable assistance was also received from the National Transportation Safety Board (NTSB), the Federal Aviation Administration (FAA) and Manufacturers of the aircraft and engine components. Three (3) Air Operator Certificate (AOC) holders at the Domestic Section of Lynden Pindling Intl Airport stated that on the day of the accident flight; one of the victims of the accident aircraft approached each of them individually at different times, requesting a quote and their availability to conduct a charter flight to Cockburn Town, San Salvador, Bahamas. Each AOC holder reported that they declined to conduct the charter because by looking at the amount of luggage and other equipment that accompanied the passengers and the size of the passengers that wanted to travel, in their estimation the combined weight appeared to be in excess of the weight that their respective aircraft (Cessna 402C and Hawker Beechcraft B100) can accommodate. After the AOC holders declined to conduct the charter, sometime thereafter, the same individual that was arranging the flight with the previous AOC holders made contact with Nelson Hanna / Acklins Blue Air Charter where arrangements were made to conduct the charter flight. The aircraft type certificate allowed for the aircraft to be operated by one (1) pilot, but the fatal flight was operated by a crew of two (2) pilots (according to eyewitness reports). The aircraft actual weight and center of gravity was unknown. As far as could be determined, the takeoff weight exceeded the maximum weight allowed of 6,850 pounds by more than 500 pounds. This excess in weight also placed the center of gravity of the aircraft outside of the safe envelope / limits for flight allowed by the manufacturer. The flight crew was given instructions by ATC to taxi from the business aviation apron (Executive Flight Support) for a takeoff on Runway 14 at intersection Foxtrot. (Intersection Foxtrot is 2,000 feet beyond the threshold of Runway 14, with a take-off run available of 9,353 feet. (Runway 14 - 11,353 feet long by 150 feet wide, see Appendix 5.15). According to eyewitness reports, from the initiation of takeoff power up to the point when the aircraft lost control white smoke was observed trailing behind the left engine of the aircraft. Eyewitnesses also reported that the take off appeared normal with gear being retracted shortly after takeoff and the aircraft seemed to be struggling to climb. The aircraft was seen at a low height, turning in a left direction over the lake as if trying to return for a landing at the airport. The bank of the aircraft changed from shallow to very steep to almost perpendicular to the ground, gears were extended and almost immediately the aircraft lost control and nose dived into the lake inverted. It cart wheeled, coming to rest upright, approximately ¼ mile from the approach end of runway 27. The aircraft came to rest on an approximate heading of 210 degrees. Eyewitness also reported hearing the engine run for a few seconds after the aircraft made contact with the water of the lake. There were no reports from the pilot to ATC of an emergency or any abnormalities with the aircraft or its systems after takeoff. The flight plan form filed for this flight listed one (1) soul on board; however, there were 7 additional occupants including a “second pilot” discovered onboard the accident flight the day of the accident. The aircraft's recovery and search for luggage, equipment and additional victims commenced shortly after the accident. This effort however, was hampered by inclement weather, rough lake conditions and darkness. On October 6th, the day after the crash, aircraft recovery continued. Family members of an additional person believed to be on board, advised the authorities that there was a ninth (9th) person on board. Search to recover any additional bodies continued but search and recovery efforts proved fruitless. On October 7th, the second day after the crash, the body of the ninth (9th) victim was found in the marshes and recovered from the southwestern end of the lake in the vicinity of where the fatal crash occurred.
Probable cause:
The following findings were identified:
1. Acklins Blue Air Charter was advertising and operating as a Bahamas air taxi operator without having undergone the certification process in contravention of Bahamas Civil Aviation (Safety) Regulations Schedule 12.
2. The airplane was issued a Certificate of Airworthiness on May 19, 2010, by the Bahamas Flight Standards Inspectorate, and was being operated by Acklins Blue Air Charter.
3. The Cessna 402C aircraft is classified in the performance Group C. This requires rapid feathering of the propeller of a failed engine and the raising of flap and the landing gear in order to achieve maximum climb performance.
4. The airplane maintenance records were not located; therefore, no determination could be made whether the airplane was being maintained in accordance with Bahamas Civil Aviation Regulations.
5. The 12,000 hour pilot and second pilot were not qualified to operate in Bahamas commercial air taxi operations.
6. No determination could be made whether the pilot or second pilot had completed required training and had accomplished a satisfactory recurrent flight check of their flying ability as required by CASR Schedule 12 and 14 for aircraft operating in commercial air transportation as well as the stipulation by the insurance policy.
7. Post-accident weight and balance calculations indicate the airplane was being operated approximately 523 pounds over maximum certificated takeoff weight (6,850 lb)
8. The pilot was advised by an air traffic controller that white smoke was trailing the left engine during takeoff; the pilot did not declare an emergency or advise the controller of any engine failure or mechanical abnormality.
9. The airplane's left engine could not produce rated shaft horsepower during takeoff.
10. Several factors contributing to the degradation of the airplane's performance and its inability to maintain flight include the wind-milling propeller, the pilot's intentional initiation of a steep turn to return to the departure airport, and his intentional lowering of the landing gear during the turn to return.
11. While turning to return, the airplane stalled, pitched nose down, and impacted in a lake.
12. The search and rescue efforts were timely and appropriate; however, the lack of accurate information on the pilot submitted flight plan delayed recovery of all victims.
13. The left propeller was not feathered.
14. The No. 2 cylinder of the left engine failed due to fatigue that originated in the root of the cylinder head thread that was engaged with the first thread on the barrel.
15. Post-accident inspection of the cockpit revealed several switches for the right engine were secured; however, no determination could be made when the switches were placed / moved in those positions.
16. No evidence of failure of the airplane's structures or flight control system contributed to the accident.
17. Existing regulations did not require the aircraft to be fitted with flight recorders. The lack of any recorded data about the aircraft's performance or the flight crew conversations deprived the investigation team of essential factual information.
18. Current Civil Aviation Department personnel and budget resources may not be sufficient to ensure that the quality of surveillance for certified as well as uncertified air carrier operations will improve.
19. Airside access procedures are inadequate at Fixed Base Operators. Access to the secure airside occurring without any check of individuals to challenge whether they have a legitimate reason for accessing the secure airside. FBO door to access airside is not secured or locked continuously; persons observed walking in and out without being challenged.
20. Flight Plan Forms are being accepted and transmitted to ATC with incomplete information. This information is vital for search and rescue purposes.
21. Weather was not a factor in the accident.
22. ATC was not a factor in the accident.
23. Currently flight plans for private flights are only required for international operations.
24. The pilot was aware of discrepancy associated with the manifold pressure reading of the left engine prior to takeoff. This discrepancy was brought to his attention by a client from the flight immediately preceding the accident flight.
25. The exact center of gravity of the accident airplane could not be calculated accurately as no indication of what seat each passenger occupied in the airplane and no indication of where luggage or equipment were placed on the aircraft could be determined. However, due to the exceedance of weight limits the aircraft was already outside the allowable center of gravity envelope developed by the manufacturer.
26. The pilot had insufficient time to prepare for the approach to runway 27 before beginning the approach. The airplane pitched up quickly into a stall, after extension of gear, recovery before ground impact was unlikely once the stall began.
27. Post accident inspection did not reveal any mechanical evidence or problems with the right hand engine.
28. The pilot's decision to return to the airfield was reasonable. Once the aircraft began to lose height a return to the airfield became impractical and a forced landing in the direction of flight should have been attempted.
29. The right propeller was never recovered from the lake.
The following causal factors were identified:
1. The left engine suffered a mechanical failure of the #2 cylinder, and therefore could not produce rated shaft horsepower. No indication of total loss of power with the left engine reported.
2. Right Engine electrical and engine control switches were found in the “OFF” position, therefore the aircraft was incapable of climbing on the power of one engine alone.
3. The excess weight above the maximum weight allowed for takeoff may have been an important factor in the aircraft's inability to gain adequate altitude after takeoff.
4. The pilot secured the right engine which was mechanically capable of producing power resulting in a total loss of thrust. He then sometime thereafter initiated a steep turn with gear down and the left engine already not developing sufficient shaft horsepower to sustain lift.
5. The pilot attempted to return to the departure airfield but lost control of the aircraft during a turn to the left.
Final Report: