Crash of a Mitsubishi MU-300 Diamond in Anderson

Date & Time: Mar 25, 2002 at 0901 LT
Type of aircraft:
Registration:
N617BG
Survivors:
Yes
Schedule:
Memphis – Anderson
MSN:
067
YOM:
1983
Crew on board:
2
Crew fatalities:
Pax on board:
4
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
10500
Captain / Total hours on type:
1000.00
Copilot / Total flying hours:
1575
Copilot / Total hours on type:
275
Aircraft flight hours:
4078
Circumstances:
The MU-300 on-demand passenger charter flight sustained substantial damage during a landing overrun on a snow/ice contaminated runway. The captain, who was also the company chief pilot and check airman, was the flying pilot, and the first officer was the non flying pilot. Instrument meteorological conditions prevailed at the time of the accident. Area weather reporting stations reported the presence of freezing rain and snow for a time period beginning several hours before the accident. The captain did not obtain the destination airport weather observation until the flight was approximately 30 nautical miles from the airport. The flight received radar vectors for a instrument landing system approach to runway 30 (5,401 feet by 100 feet, grooved asphalt). The company's training manual states the MU-300's intermediate and final approach speeds as 140 knots indicated airspeed (KIAS) and Vref, respectively. Vref was reported by the flight crew as 106 KIAS. During the approach, the tower controller (LC) gave the option for the flight to circle to land or continue straight in to runway 30. LC advised that the winds were from 050-070 degrees at 10 knots gusting to 20 knots, and runway braking action was reported as fair to poor by a snow plow. Radar data indicates that the airplane had a ground speed in excess of 200 knots between the final approach fix and runway threshold and a full-scale localizer deviation 5.5 nm from the localizer antenna. The company did not have stabilized approach criteria establishing when a missed approach or go-around is to be executed. The captain stated that he was unaware that there was 0.7 percent downslope on runway 30. The company provided a page from their airport directory which did not indicate a slope present for runway 30. The publisher of the airport directory provided a page valid at the time of the accident showing a 0.7 percent runway slope. Runway slope is used in the determination of runway performance for transport category aircraft such as the MU-300. The airplane operating manual states that MU-300 landing performance on ice or snow covered runways has not been determined. The airplane was equipped with a cockpit voice recorder with a remote cockpit erasure control. Readout of the cockpit voice recorder indicated a repetitive thumping noise consistent with manual erasure. No notices to airman pertaining to runway conditions were issued by the airport prior to the accident.
Probable cause:
Missed approach not executed and flight to a destination alternate not performed by the flight crew. The tail wind and snow/ice covered runway were contributing factors.
Final Report:

Crash of a Mitsubishi MU-2B-35 Marquise in Smyrna

Date & Time: Sep 21, 1995 at 0425 LT
Type of aircraft:
Registration:
N309MA
Flight Phase:
Flight Type:
Survivors:
Yes
Schedule:
Smyrna - Louisville
MSN:
602
YOM:
1973
Crew on board:
1
Crew fatalities:
Pax on board:
1
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
2140
Captain / Total hours on type:
112.00
Aircraft flight hours:
4304
Circumstances:
A witness stated he observed the airplane on climbout from runway 32. The airplane started a right turn estimated at about 30 to 45° angle of bank. The airplane stopped climbing and began descending. Subsequently, it collided with a tree line, while in a right bank, and then it impacted the ground. Weather conditions at the time of accident were described by the witness as very dark, with no ambient light or visible horizon. Examination of the airframe, flight control system, engine assembly, and propeller assembly revealed no evidence of a precrash failure or malfunction. The autopilot was found in the off position, and the autopilot circuit breakers were not tripped. The pilot and passenger were seriously injured and had no memory of the flight. A radio transcript revealed that after taking off, the flight had made one radio transmission to request an ifr clearance.
Probable cause:
Failure of the pilot to maintain a proper climb rate after takeoff, and his inadvertent entry in a descending spiral, which he failed to correct. Factors relating to the accident were: darkness, and the pilot becoming spatially disoriented during the initial climb while attempting to obtain an ifr clearance.
Final Report: