Crash of a Mitsubishi MU-2B-35 Marquise in Hilton Head: 1 killed

Date & Time: Aug 1, 2001 at 0751 LT
Type of aircraft:
Operator:
Registration:
N1VY
Flight Type:
Survivors:
No
Schedule:
Columbia – Savannah – Hilton Head
MSN:
567
YOM:
1972
Flight number:
BKA170
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
1
Captain / Total flying hours:
4184
Captain / Total hours on type:
483.00
Aircraft flight hours:
11612
Circumstances:
The airplane was on final approach to land at Hilton Head Airport, when according to witnesses, it suddenly rolled to the right, and descended, initially impacting trees at about the 70-foot level, and then impacting the ground. A fire then ensued upon ground impact, and the debris field spanned about 370 feet along an azimuth of about 082 degrees. Examination of the airplane wreckage revealed that left wing flap actuator and jack nut measurements were consistent with the wing flaps being extended to 40 degrees, and on the right wing the flap jack nut and actuator measurements were consistent with the right flap being extended to about a 20-degrees. In addition, the right flap torque tube assembly between the flap motor and the flap stop assembly had disconnected, and the flap torque tube assembly's female coupler which attaches to the male spline end of the flap motor and flap stop assembly was found with a cotter pin installed through the female coupler of the flap stop assembly. The cotter pin, had not been placed through the spline and the coupler consistent with normal installation as per Mitsubishi's maintenance manual, or as specified in Airworthiness Directive 88-23-01. Instead, the cotter pin had missed the male spline on the flap motor. In addition, the flap coupler on the opposite side of the flap motor was found to also found to not have a cotter pin installed. Company maintenance records showed that on April 3, 2001, about 87 flight hours before the accident, the airplane was inspected per Airworthiness Directive (AD) 88-23-01, which required the disassembly, inspection, and reassembly of the flap torque tube joints. In addition, on July 9, 2001, the airplane was given a phase 1 inspection, and Bankair records showed that a company authorized maintenance person performed the applicable maintenance items, and certified the airplane for return to service.
Probable cause:
Improper maintenance/installation and and inadequate inspection of the airplane's flap torque tube joints during routine maintenance by company maintenance personnel, which resulted in the right flap torque tube assembly coupler becoming detached and the flaps developing asymmetrical lift when extended, which resulted in an uncontrolled roll, a descent, and an impact with a tree during approach to land.
Final Report:

Crash of a Piper PA-46-350P Malibu Mirage in Westfield: 1 killed

Date & Time: Jul 28, 2001 at 1655 LT
Registration:
N3DM
Flight Type:
Survivors:
Yes
Schedule:
Nantucket – Westfield
MSN:
46-22079
YOM:
1989
Crew on board:
1
Crew fatalities:
Pax on board:
2
Pax fatalities:
Other fatalities:
Total fatalities:
1
Captain / Total flying hours:
1660
Aircraft flight hours:
1030
Circumstances:
After a normal cross country flight, the airplane was on final approach for landing to runway 20, when the air traffic controller instructed the pilot to "go-around" because a preceding airplane had not cleared the runway. The airplane was observed to pitch up and enter a steep, almost 90 degree left bank. The passenger in the rear seat described the flights from and to BAF as "smooth." She stated she thought that the airplane would be landing; however, then realized the airplane was in a left turn. The airplane impacted on the roof of a commercial building, and came to rest upright on a heading of 020 degrees, in a parking lot, about 1/4 mile east of the approach end the runway. Examination of the airplane, which included a teardown of the engine, did not reveal evidence of any pre-impact malfunctions. Weather reported at the airport about the time of the accident included winds from 240 degrees at 7 knots; visibility 10 status miles and few clouds at 6,500 feet. The pilot owned the airplane and had accumulated about 1,660 hours of total flight experience.
Probable cause:
The pilot's failure to maintain aircraft control while maneuvering during a go-around.
Final Report:

Crash of a Piper PA-46-350P Malibu Mirage in Black Mountain: 1 killed

Date & Time: Jul 21, 2001 at 1707 LT
Registration:
N396PM
Flight Phase:
Flight Type:
Survivors:
No
Site:
Schedule:
Asheville – Burnsville
MSN:
46-36024
YOM:
1996
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
1
Captain / Total flying hours:
2555
Captain / Total hours on type:
127.00
Aircraft flight hours:
709
Circumstances:
The pilot had left the airplane at Asheville on the day before the accident due to low cloud ceilings and visibility at Mountain Air Airport, his destination, and completed the trip by rental car. On the day of the accident the pilot returned the rental car and at 1656 departed Asheville in N396PM, enroute to Mountain Air Airport, 27 miles north of Asheville. The last radio contact with the pilot was at 1701:44, when the pilot told controllers at Asheville that he was in visual flight rule conditions, at 4,000 feet. The last radar contact with the flight was by FAA Atlanta Center, at 1704:00, when the flight was about 5 miles south of the accident site at 3,800 feet. The flight did not arrive at the destination, an emergency locator transmitter signal was received by satellite, and search and rescue operations were begun. The pilot and the wreckage of the airplane was located the next day about 1400. The airplane had collided with 75-foot tall trees, at about the 4,800-foot msl level on the side of Bullhead Mountain, while in a wings level attitude, while on a 170 degree heading. After the initial impact the airplane continued for another 300 feet, causing general breakup of the airplane. The main wreckage came to rest on a northerly heading. All components of the airplane were located at the crash site and there was no evidence of precrash failure or malfunction of the airplane structure, flight controls, airplane systems, engine, or propeller. A witness reported that the weather near the time of the accident on the Blue Ridge Parkway, located about 3/4 mile to the west of the crash site, was very foggy. Satellite images show clouds were present at the crash site and the Asheville airport, located 20 miles south-southwest of the crash site, reported overcast clouds 2,600 feet agl or 4,765 feet msl, and visibility 4 miles in haze, at the time of the accident. An Airmet for mountain obscuration due to clouds, mist, and haze was in effect at the time the pilot departed and the at the time of the accident. No record to show that the pilot received a weather briefing from a FAA Flight Service Station was found.
Probable cause:
The pilot's continued VFR flight into IMC conditions resulting in the airplane colliding with mountainous terrain.
Final Report:

Crash of a Piper PA-46-310P Malibu in Stow

Date & Time: Jul 15, 2001 at 2107 LT
Registration:
N9133D
Survivors:
Yes
Schedule:
Columbia – Newburgh – Stow
MSN:
46-08110
YOM:
1988
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
3500
Captain / Total hours on type:
2616.00
Aircraft flight hours:
2692
Circumstances:
Witnesses reported hearing an airplane engine at night, at high power for about 5 seconds followed by impact. They went to the scene and found the airplane on the left side of the approach end of runway 03, on fire. The pilot was removed and the fire was extinguished. The airplane had struck a runway threshold light located about 25 feet to the left side of the runway, and slid about 100 feet into trees, angling away from the runway on a heading of 360 degrees. The outboard 5 feet of the left wing was bent up about 20 degrees. Ground scars were found corresponding to the positions of the left, right, and nose landing gears, all of which had collapsed. The inboard section of the left wing came to rest on the nose of the airplane. The propeller blades were deformed with "S" bending and leading edge gouges. Flight control continuity was verified to the rudder and elevator. The aileron control cables had separated with puffed ends. All separations occurred at other than attach points. The pilot had received head injuries and has no memory of the accident.
Probable cause:
The pilot's failure to maintain airplane control during a go-around.
Final Report:

Crash of a Cessna 402C in Boston

Date & Time: Jul 8, 2001 at 1214 LT
Type of aircraft:
Operator:
Registration:
N760EA
Flight Phase:
Flight Type:
Survivors:
Yes
Schedule:
Boston – Nantucket
MSN:
402C-0056
YOM:
1979
Flight number:
9K065
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
2539
Captain / Total hours on type:
476.00
Aircraft flight hours:
15140
Circumstances:
The pilot accepted an intersection departure and waived the wake turbulence holding time. A Boeing 737-300 departed ahead of him, and according to pilot, the Boeing's nosewheel lifted off the runway just as it passed him. The pilot also noted that the Boeing and its exhaust smoke drifted to the left of the runway's centerline. A wake turbulence advisory and takeoff clearance were issued by the tower controller and acknowledged by the pilot. The pilot initiated the takeoff, and after liftoff, the left wing dropped. It contacted the runway, and the airplane rolled inverted. The airplane then slid off the left side of the runway and a post-crash fire developed.
Probable cause:
The pilot's improper decision to waive the wake turbulence hold time, and his subsequent loss of control when wake vortex turbulence was encountered.
Final Report:

Crash of a Cessna 208B Grand Caravan off Fort Lauderdale

Date & Time: Jul 6, 2001 at 1900 LT
Type of aircraft:
Operator:
Registration:
N812MA
Flight Phase:
Flight Type:
Survivors:
Yes
Schedule:
Freeport – Fort Lauderdale
MSN:
208B-0553
YOM:
1996
Crew on board:
2
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
3700
Captain / Total hours on type:
1200.00
Aircraft flight hours:
5936
Circumstances:
While in cruise flight at 6,500 feet, the airplane's engine jolted and made a whining noise. The propeller stopped and feathered. Attempts to restore engine power were unsuccessful. An emergency was declared, and the airplane was ditched into the Atlantic Ocean 20 miles east of Ft. Lauderdale, Florida. The airplane was not recovered for post-crash examination.
Probable cause:
The undetermined malfunction of the propeller system.
Final Report: