Crash of a Beechcraft E90 King Air in Sotillo de las Palomas: 4 killed

Date & Time: Dec 4, 2016 at 1617 LT
Type of aircraft:
Registration:
N79CT
Flight Phase:
Flight Type:
Survivors:
No
Schedule:
Madrid – Cascais
MSN:
LW-303
YOM:
1979
Country:
Region:
Crew on board:
1
Crew fatalities:
Pax on board:
3
Pax fatalities:
Other fatalities:
Total fatalities:
4
Circumstances:
The twin engine aircraft departed Madrid-Cuatro Vientos Airport on a private flight to Cascais, Portugal, carrying three passengers and one pilot. One of the reasons for the flight was to repair the weather radar at a Portuguese maintenance center that specialized in this equipment. The pilot had to delay the takeoff until 1557LT due to bad weather conditions. The aerodrome of Cuatros Vietnos was in instrument conditions (IMC), which forced its closing from 0900LT until 1444LT. At 1615LT, the aircraft was en route, climbing from flight level 190 to its authorized cruise level of 210. Moments later, according to a detailed analysis of the data taken from the radar, there was a yaw to the left, and the aircraft started to turn in this direction and suddenly lose altitude. After this event, the airspeed fell quickly and gradually until the aircraft stalled. The aircraft went into a spin, which after some time turned into a flat spin. As the airplane descended out of control, and with the spin fully developped, loads were placed on the horizontal tail that exceeded the design loads, causing the tail to break up in flight into five parts before the aircraft impacted the ground. The aircraft was completely destroyed by the impact and sibsequent fire, and its four occupants were killed in the accident.
Probable cause:
The investigation has concluded that this accident was caused by the loss of control of the aircraft in flight due to a stall and subsequent spin. Due to the high degree of destruction of the aircraft's wreckage after the ground impact and subsequent fire, and the lack of other pertinent data to do so, it has not been possible to determine with precision the sequence of the process leading to the aircraft stall/spin.
The investigation identified the following contributing factors:
- The decision to make the flight with adverse meteorological conditions (IMC) along the planned route, considering the fact that the weather radar was not operational.
- The forecast of moderate to strong icing conditions in areas of the route (presence of cumulonimbus with caps of up to 35,000 feet and with temperatures between -17°C and -19°C at flight level FL180) suggests that the formation of ice or its accumulation on the aircraft has been a significant contributory factor in this accident
- The use of the autopilot and the failure to disengage it when the emergency situation arose, as it is concluded from the detailed analysis of the radar data, could have contributed significantly to the process that resulted in the loss of control of the aircraft.
- The inadequate training of the pilot (who lacked the type rating for the accident aircraft) in abnormal or emergency situations on the accident aircraft.
Final Report:

Crash of a Swearingen SA226T Merlin III in Andorra

Date & Time: Apr 26, 2016 at 1535 LT
Operator:
Registration:
N125WG
Flight Type:
Survivors:
Yes
Schedule:
Alicante - Andorra
MSN:
T-250
YOM:
1974
Country:
Region:
Crew on board:
1
Crew fatalities:
Pax on board:
4
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
4750
Captain / Total hours on type:
1200.00
Circumstances:
The twin engine airplane departed Alicante-Mutxamel Airport at 1221LT on a private flight to Andorra, carrying four passengers and one pilot. Following an uneventful flight at an altitude of 12,500 feet, the pilot informed ATC about electrical problems then initiated the descent to Andorra. About two minutes later, the electrical system totally failed. The pilot continued the approach to Andorra-La Seu d'Urgell Airport. After touchdown on runway 21, the undercarriage collapsed. The aircraft veered off runway to the right and came to rest in a grassy area. All five occupants evacuated safely and the aircraft was damaged beyond repair.
Probable cause:
It is considered that the accident was caused by an error in the application of the emergency extension procedure of the landing gear following a total failure of the electrical system.
Contributing factors :
- Start a visual flight with a deferred pending repair in the electrical system, specifically with the generator on the right side.
- Lack of recent training and simulation with emergency procedures.
- The versatility of the pilot and diversity of different aircraft types flown.
- The non-activation of the warning light on the left-hand side of the cockpit panel when the electrical system failed about 30 minutes prior to the total exhaustion of all batteries.
Final Report: