Crash of an Airbus A320-214 in Karachi: 98 killed

Date & Time: May 22, 2020 at 1440 LT
Type of aircraft:
Operator:
Registration:
AP-BLD
Survivors:
Yes
Site:
Schedule:
Lahore - Karachi
MSN:
2274
YOM:
2004
Flight number:
PK8303
Country:
Region:
Crew on board:
8
Crew fatalities:
Pax on board:
91
Pax fatalities:
Other fatalities:
Total fatalities:
98
Captain / Total flying hours:
17252
Captain / Total hours on type:
4783.00
Copilot / Total flying hours:
2291
Copilot / Total hours on type:
1504
Aircraft flight hours:
47124
Aircraft flight cycles:
25866
Circumstances:
On 22nd May, 2020 at 08:05:30 Universal Time Coordinated (UTC), PIA Airbus A320-214 aircraft Reg. No. AP-BLD, took off from Allama Iqbal International Airport (AIIAP) Lahore, Pakistan to perform a regular commercial passenger flight (PIA 8303) to JIAP Karachi, Pakistan with 08 crew members [Captain, First Officer (FO) and 06 flight attendants] and 91 passengers. At 09:15:38 UTC, descent for Approach was initiated. Flight was cleared for an Instrument Landing System (ILS) Approach Runway (R/W) 25L. Aircraft altitude was around 9,000 feet (ft) instead of 3,000 ft at 15 Nautical Mile (NM) from touchdown. Speed Brakes and Landing Gears were extended. Aircraft was significantly above the published vertical approach path. Around 5 NM from the touchdown, both Speed Brakes and Landing Gears were retracted. Several Warnings, cockpit indications and Air Traffic Control (ATC) instructions were disregarded by flight crew and the Unstabilized Approach was continued. At 09:34:28 UTC, aircraft touched almost 4,500 ft down the R/W 25L with Landing Gears retracted. Flight crew initiated a Go-Around. Both Engines were damaged during the contact with the R/W. The resultant loss of Engine oil and subsequent lack of lubrication resulted in failure of both Engines. Around 2,000 ft, flight crew announced that they have lost Engines, followed by a MAYDAY call. Aircraft started to lose height and crashed at 09:40:18 UTC in a populated area 1,340 meters (m) short of R/W 25L. Out of 99 persons on-board, 97 were fatally injured whereas 02 passengers survived. On ground 04 persons were injured, out of them 01 expired later in the hospital.
Probable cause:
It was determined that the aircraft made gears up landing where both engines’ nacelle made contact with runway. Both engines were damaged causing loss of engine oil and lubrication which resulted in failure of both engines during go-around. Non-adherence to SOPs and disregard of ATC instructions during the event flight. Lack of communication between the ATC and the flight crew regarding gears up landing particularly once aircraft was on the runway.
The following contributing factors were identified:
- Ineffective implementation of FDA program.
- Flight Data Analysys (FDA) regulatory oversight program was ineffective in producing sufficient and timely improvement.
- Lack of clear and precise regulations to restrict flying while fasting.
- Inadequate level of crew resources management (CRM) application during the event flight.
Final Report:

Crash of a Boeing 737-4H6 in Lahore

Date & Time: Nov 3, 2015 at 0926 LT
Type of aircraft:
Operator:
Registration:
AP-BJO
Survivors:
Yes
Schedule:
Karachi – Lahore
MSN:
27166/2410
YOM:
1992
Flight number:
NL142
Country:
Region:
Crew on board:
7
Crew fatalities:
Pax on board:
114
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
19302
Captain / Total hours on type:
4859.00
Copilot / Total flying hours:
2076
Copilot / Total hours on type:
410
Aircraft flight hours:
51585
Aircraft flight cycles:
46547
Circumstances:
On 03rd November 2015, M/s Shaheen Air International Flight NL-142, Boeing 737-400 aircraft Reg # AP-BJO, was on a scheduled passenger flight from Karachi to Lahore. The flight landed on Runway 36L as Runway 36R was not available due to ILS CAT-III up-gradation. After touchdown, both main landing gears broke one after the other. Subsequently, the aircraft departed runway while resting on both engines and stopped 8302 ft from Runway Threshold (RWT), 197ft left of runway centreline. The nose landing gear, however, remained intact. All the passengers were safely evacuated through emergency procedure.
Probable cause:
The accident took place due to:
- Cockpit crew landing the aircraft through unstabilized approach (high ground speed and incorrect flight path).
- Low sink rate of left main landing gear (LMLG) as it touched down and probable presence of (more than the specified limits) play in the linkages of shimmy damper mechanism. This situation led to torsional vibrations / breakage of shimmy damper after touchdown. The resultant torsional excitation experienced by the LMLG due to free pivoting of wheels (along vertical axis) caused collapse of LMLG.
- The RMLG collapsed due to overload as the aircraft moved on unprepared surface.
Final Report:

Crash of a Boeing 737-4H6 in Lahore

Date & Time: Dec 30, 2014 at 1522 LT
Type of aircraft:
Operator:
Registration:
AP-BJN
Survivors:
Yes
Schedule:
Karachi – Lahore
MSN:
26460/2533
YOM:
1993
Flight number:
NL148
Country:
Region:
Crew on board:
6
Crew fatalities:
Pax on board:
166
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
Following an uneventful flight from Karachi, the crew completed the approach and landing on runway 36L at Lahore-Allama Muhammad Iqbal Airport. After touchdown, the crew initiated the braking procedure when the left main gear partially collapsed. Control was lost and the aircraft veered to the right before coming to rest in a grassy area. All 172 occupants evacuated safely and the aircraft was damaged beyond repair.
Probable cause:
It was determined that the left main gear partially collapsed after it suffered a bird strike (rapacious) on approach.

Ground fire of a Fokker F27 Friendship 100 in Lahore

Date & Time: Feb 2, 1971
Type of aircraft:
Operator:
Registration:
VT-DMA
Flight Phase:
Survivors:
Yes
Schedule:
Srinagar – Jammu
MSN:
10171
YOM:
1961
Country:
Region:
Crew on board:
4
Crew fatalities:
Pax on board:
28
Pax fatalities:
Other fatalities:
Total fatalities:
0
Aircraft flight hours:
21091
Aircraft flight cycles:
17638
Circumstances:
While on a flight from Srinagar to Jammu, the airplane was hijacked by two members of the Jammu and Kashmir National Liberation Front (NLF). After being diverted to Lahore Airport, the aircraft stand on this airport for three days before all 32 occupants were released. The aircraft was then set afire and destroyed.
Probable cause:
Hijacked and destroyed by fire on ground.