Zone

Crash of a Beechcraft 300 Super King Air in Cullman: 2 killed

Date & Time: Jan 14, 1999 at 0918 LT
Registration:
N780BF
Survivors:
No
Schedule:
Greenville - Cullman
MSN:
FA-70
YOM:
1985
Location:
Crew on board:
1
Crew fatalities:
Pax on board:
1
Pax fatalities:
Other fatalities:
Total fatalities:
2
Captain / Total flying hours:
4100
Aircraft flight hours:
7687
Circumstances:
The airplane descended to 2,600 feet to the NDB, and initiated the approach upon crossing the NDB. As the airplane descended below 1,500 feet MSL, Huntsville lost radar contact. The next communication with the airplane was when the pilot radioed that he was initiating the missed approach. The published missed approach procedure is, 'Climbing lift turn to 2,700 direct CPP NDB and hold.' The airplane made a series of turns within the next one minute and 24 seconds. Additionally, the airplane's altitude varied but it never climbed above the altitude of 1,700 feet. The airplane wreckage was located approximately 3.5 miles north of the airport on a 345 degree heading on the opposite side of the outbound course to the NDB. Witnesses in the immediate area stated that they could hear the airplane flying low over their homes but could not see it due to the foggy conditions. A review of pilot records did not show the pilot having any fixed wing airplane experience.
Probable cause:
The pilot's failure to adhere to the missed approach procedure resulting in a collision with terrain. Contributing factors were fog and the rotorcraft rated pilot's lack of fixed wing certification/experience.
Final Report:

Crash of a Cessna 421B Golden Eagle II in Cullman: 6 killed

Date & Time: Mar 5, 1984 at 1836 LT
Operator:
Registration:
N3291Q
Survivors:
No
Schedule:
Montgomery - Cullman
MSN:
421B-0911
YOM:
1975
Location:
Crew on board:
1
Crew fatalities:
Pax on board:
5
Pax fatalities:
Other fatalities:
Total fatalities:
6
Captain / Total flying hours:
3423
Captain / Total hours on type:
1599.00
Aircraft flight hours:
2478
Circumstances:
Pilot cleared for night NDB runway 19 approach to Folsom Field. Erratic radar track during procedure turn and inbound intercept. Witnesses described 200 feet ceiling and reduced visibility in fog at airport. Other witnesses observed aircraft on northbound course, followed by turn to west at rooftop height, well below MDA, at a point one mile northeast of airport. Engine operation sounded normal. Aircraft contacted trees at about airport elevation, one mile north of airport. Wreckage produced 632 feet path. Severed limbs, prop damage and engine examination revealed evidence of power at impact. 62 year old pilot had not flown with cfi in years, instrument currency unknown. Pilot found to have severe coronary atherosclerosis with near total occlusion of right coronary artery and evidence of past total occlusion of left circumflex coronary artery. Ceiling lower than forecast for area. Flight purpose to carry employees to meet truck, go job site. Limitation on pilot medical certificate, not for night flight. Sunset at 1745 cst, 51 minutes before accident. All six occupants were killed.
Probable cause:
Occurrence #1: in flight collision with object
Phase of operation: approach - faf/outer marker to threshold (IFR)
Findings
1. (f) weather condition - low ceiling
2. (f) weather condition - fog
3. (f) light condition - dark night
4. (f) object - tree(s)
5. (c) IFR procedure - not followed - pilot in command
6. (c) visual/aural perception - pilot in command
7. (c) minimum descent altitude - not maintained - pilot in command
8. (c) lack of recent instrument time - pilot in command
9. (c) missed approach - not performed - pilot in command
10. (c) physical impairment - pilot in command
Final Report:

Crash of a Fairchild C-119G-FA Flying Boxcar near Cullman

Date & Time: Mar 10, 1955
Operator:
Registration:
51-8095
Flight Phase:
Flight Type:
Survivors:
Yes
MSN:
10989
YOM:
1952
Location:
Crew on board:
11
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
Following an engine failure in flight, all 11 crew members bailed out and abandoned the aircraft that dove into the ground and crashed in a prairie located near Cullman. All 11 crew members were uninjured while the aircraft was destroyed.
Probable cause:
Engine failure in flight.