Zone

Crash of an Airbus A319-115 in Chongqing

Date & Time: May 12, 2022 at 0805 LT
Type of aircraft:
Operator:
Registration:
B-6425
Flight Phase:
Survivors:
Yes
Schedule:
Chongqing – Nyingchi
MSN:
5157
YOM:
2012
Flight number:
TV9833
Country:
Region:
Crew on board:
9
Crew fatalities:
Pax on board:
113
Pax fatalities:
Other fatalities:
Total fatalities:
0
Aircraft flight hours:
28364
Aircraft flight cycles:
14495
Circumstances:
The airplane was departing Chongqing-Jiangbei Airport on a regular schedule service to Nyingchi, Tibet, carrying 113 passengers and a crew of nine. During the takeoff roll on runway 03, at a speed of 145 knots (just below V1 speed), the captain encountered an unexpected situation and decided to abandon the takeoff procedure. He initiated an emergency braking manoeuvre when the airplane started to deviate to the left. It veered off runway and went through a grassy area. While contacting the parallel concrete taxiway, the nose gear was sheared off. The airplane continued for 120 metres when it impacted a drainage ditch, causing both main landing gears and both engines to be sheared off as well. The airplane later came into a stop, bursting into flames. 36 occupants were injured while all others evacuated safely. The aircraft was destroyed.
Probable cause:
It was determined that, during the takeoff run, the captain was distracted by items falling, and momentarily lost the monitoring of the aircraft's flight sequence. During this short period of time, he unconsciously held the left rudder, which resulted in an unintended deviation of the aircraft to the left direction. After he noticed the deviation, the crew failed to execute the standard callouts, and the captain reduced the throttle in an attempt to abort the takeoff. Due to the combined effects of maximum braking force and inertia, the crew was unable to maintain a safe control, causing the airplane to veer off the runway to the left at a speed of approximately 127 knots. Poor decision makings on part of the crew was considered as the main cause of the accident.
Final Report:

Crash of a Boeing 737-31B in Shenzhen: 35 killed

Date & Time: May 8, 1997 at 2132 LT
Type of aircraft:
Operator:
Registration:
B-2925
Survivors:
Yes
Schedule:
Chongqing - Shenzhen
MSN:
27288
YOM:
1994
Flight number:
CZ3456
Country:
Region:
Crew on board:
9
Crew fatalities:
Pax on board:
65
Pax fatalities:
Other fatalities:
Total fatalities:
35
Circumstances:
The approach to Shenzhen-Huangtian Airport was completed in poor weather conditions with thunderstorm activity, heavy rain falls and turbulences. During the last segment, the aircraft was unstable but the crew continued the descent when the aircraft landed hard. The aircraft bounced and suffered undercarriage damages. Despite the situation, the captain decided to initiate a go-around procedure and increased engine power. During the second attempt to land, the crew encountered control difficulties as the aircraft suffered damages from the first missed landing. Also, weather conditions were poor so the aircraft was unstable on approach. After landing at an excessive speed, the aircraft went out of control, veered off runway and came to rest in a soft ground, broken in three and bursting into flames. Two crew members and 33 passengers were killed while 39 other people were injured.