Crash of a Piper PA-60-602P Aerostar (Ted Smith 600) in Greenville: 3 killed

Date & Time: Jul 30, 2018 at 1044 LT
Operator:
Registration:
C-GRRS
Flight Type:
Survivors:
No
Schedule:
Pembroke – Charlottetown
MSN:
60-8265-026
YOM:
1982
Crew on board:
1
Crew fatalities:
Pax on board:
2
Pax fatalities:
Other fatalities:
Total fatalities:
3
Captain / Total flying hours:
590
Captain / Total hours on type:
136.00
Aircraft flight hours:
4856
Circumstances:
The private pilot of the multiengine airplane was in cruise flight at 23,000 ft mean sea level (msl) in day visual meteorological conditions when he reported to air traffic control that the airplane was losing altitude due to a loss of engine power. The controller provided vectors to a nearby airport; about 7 minutes later, the pilot reported the airport in sight and stated that he would enter a downwind leg for runway 14. By this time, the airplane had descended to about 3,200 ft above ground level. Radar data indicated that the airplane proceeded toward the runway but that it was about 400 ft above ground level on short final. The airplane flew directly over the airport at a low altitude before entering a left turn to a close downwind for runway 21. Witnesses stated that the airplane's propellers were turning, but they could not estimate engine power. When the airplane reached the approach end of runway 21, it entered a steep left turn and was flying slowly before the left wing suddenly "stalled" and the airplane pitched nose-down toward the ground. Postaccident examination of the airplane and engines revealed no mechanical deficiencies that would have precluded normal operation at the time of impact. Examination of both propeller systems indicated power symmetry at the time of impact, with damage to both assemblies consistent with low or idle engine power. The onboard engine monitor recorded battery voltage, engine exhaust gas temperature, and cylinder head temperature for both engines. A review of the recorded data revealed that about 14 minutes before the accident, there was a jump followed by a decrease in exhaust gas temperature (EGT) and cylinder head temperature (CHT) for both engines. The temperatures decreased for about 9 minutes, during which time the right engine EGT data spiked twice. Both engines' EGT and CHT values then returned to normal, consistent with both engines producing power, for the remaining 5 minutes of data. It is possible that a fuel interruption may have caused the momentary increase in both engines' EGT and CHT values and prompted the pilot to report the engine power loss; however, the engine monitor did not record fuel pressure or fuel flow, and examination of the airplane's fuel system and engines did not reveal any mechanical anomalies. Therefore, the reason for the reported loss of engine power could not be determined. It is likely that the pilot's initial approach for landing was too high, and he attempted to circle over the airport to lose altitude. While doing so, he exceeded the airplane's critical angle of attack while in a left turn and the airplane entered an aerodynamic stall at an altitude too low for recovery.
Probable cause:
The pilot's exceedance of the airplane's critical angle of attack while maneuvering to land, which resulted in an aerodynamic stall.
Final Report:

Crash of a Piper PA-31-310 Navajo in Charlottetown: 3 killed

Date & Time: Jun 5, 2001 at 1621 LT
Type of aircraft:
Operator:
Registration:
C-GMTT
Flight Phase:
Survivors:
Yes
Schedule:
Gander – Charlottetown – Natuashish
MSN:
31-7712004
YOM:
1977
Country:
Crew on board:
1
Crew fatalities:
Pax on board:
3
Pax fatalities:
Other fatalities:
Total fatalities:
3
Captain / Total flying hours:
2085
Captain / Total hours on type:
185.00
Circumstances:
The flight took off on Runway 22 at Gander, Newfoundland and Labrador, at 1428 Newfoundland daylight time with the pilot and four passengers on board. Their destination was Sango Bay, Newfoundland and Labrador, with an intermediate stop in Charlottetown, Newfoundland and Labrador, to drop off one of the passengers. Radar data show that, on departure from Gander, the aircraft climbed at about 500 feet per minute at 125 knots ground speed to 2500 feet, then descended and proceeded en route to Charlottetown at 1900 feet and 150 knots. The aircraft landed at Charlottetown at 1615. After a brief stop, the flight continued to Sango Bay. The pilot broadcast his intention to take off on Runway 10, taxied the aircraft to the threshold of the runway, and commenced the take-off roll. Part-way down the runway, the pilot aborted the take-off. He then broadcast his intention to take off on Runway 28. Both radio broadcasts were acknowledged by a local pilot who was approaching the airport to land. Upon reaching the threshold of Runway 28, the aircraft turned and accelerated, without stopping, on the take-off roll. The aircraft lifted off shortly before the runway end and remained near treetop height until disappearing from view. After lift-off, the stall warning horn sounded intermittently until impact. The aircraft was unable to climb above the hilly terrain and struck the road 1.5 nautical miles from the departure end of the runway. A passing motorist spotted the downed aircraft and notified firefighters and medical personnel who were then dispatched to the scene. The accident occurred at about 1621 during daylight hours, at 58°45' N, 55°66' W, at 440 feet above sea level.
Probable cause:
Findings as to Causes and Contributing Factors:
1. The aircraft was over the maximum allowable take-off weight throughout its journey, reducing aircraft performance: the pilot apparently did not complete weight and balance calculations for
either of the flights.
2. The pilot did not use the proper short field take-off technique, and the aircraft was forced into the air before reaching sufficient flying speed.
3 The best angle of climb speed was not attained.
4. The unsecured cargo, some of which was found on top of the back of the rear passenger seat, most probably contributed to the severity of the injuries to the passenger in this seat.
Final Report:

Crash of a Consolidated B-32-2 Liberator II in Charlottetown: 1 killed

Date & Time: Feb 21, 1946
Operator:
Registration:
G-AGEM
Survivors:
Yes
Schedule:
London – Shannon – Keflavik – Gander – New York
MSN:
26
YOM:
1942
Country:
Crew on board:
6
Crew fatalities:
Pax on board:
8
Pax fatalities:
Other fatalities:
Total fatalities:
1
Circumstances:
While cruising along the east Canadian coast, the crew informed ATC about severe icing conditions and obtained the permission to divert to Charlottetown Airport. The aircraft passed the runway threshold at a height of 7 meters and then stalled and crashed in flames on the runway. The copilot was killed while 13 other occupants were injured. The aircraft was destroyed.
Probable cause:
The exact cause of the crash was not determined. However, it is believed that the plane would have stalled during the last segment due to the combination of an excessive accumulation of ice and frost and an insufficient approach speed.

Crash of a Noorduyn Norseman in Charlottetown: 2 killed

Date & Time: May 1, 1945
Type of aircraft:
Operator:
Registration:
FR405
Flight Phase:
Flight Type:
Survivors:
No
MSN:
128
YOM:
1943
Country:
Crew on board:
2
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
2
Circumstances:
Crashed in unknown circumstances, killing both occupants, pilots John J. Gilmour and Frank L. Radcliffe.

Crash of an Avro 652 Anson I off Tracadie

Date & Time: Aug 24, 1942
Type of aircraft:
Operator:
Registration:
K6265
Flight Phase:
Flight Type:
Survivors:
Yes
Schedule:
Charlottetown - Charlottetown
Country:
Crew on board:
5
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
The crew was involved in a training exercise from Charlottetown. En route, the pilot was forced to ditch the aircraft for unknown reason in the Tracadie Bay, Nova Scotia. While all five crew members were rescued, the aircraft was lost.

Crash of an Avro 652 Anson I in Charlottetown: 4 killed

Date & Time: Nov 20, 1941 at 2117 LT
Type of aircraft:
Operator:
Registration:
N4894
Flight Type:
Survivors:
Yes
Schedule:
Charlottetown - Chatham - Charlottetown
Country:
Crew on board:
4
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
4
Captain / Total flying hours:
305
Captain / Total hours on type:
152.00
Copilot / Total flying hours:
57
Circumstances:
The airplane departed Charlottetown on a night navigation exercise. It was not heard of after setting out of wireless touch with at night. It landed at Chatham then took off to return to base without refuelling or contacting base. Approaching Charlottetown, the airplane crashed for unknown reasons few km from the airfield. All four crew members were killed.
Crew (31st GRS):
P/O Alfred John Freeman,
LAC Norman James Ficken,
LAC Stanley Vincent Clench,
AC1 William Thomas.
Final Report:

Crash of a De Havilland DH.60X Moth in Charlottetown

Date & Time: Nov 2, 1930
Type of aircraft:
Operator:
Registration:
G-CAVG
Flight Phase:
Flight Type:
Survivors:
Yes
MSN:
689
YOM:
1928
Country:
Crew on board:
1
Crew fatalities:
Pax on board:
1
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
Shortly after takeoff from Charlottetown Airport, the aircraft stalled and crashed. Both occupants were injured and the aircraft was destroyed.
Probable cause:
Engine failure shortly after rotation.