Zone

Crash of a Rockwell Aero Commander 500B near Sylacauga

Date & Time: Jan 28, 2023 at 1751 LT
Operator:
Registration:
N107DF
Flight Phase:
Flight Type:
Survivors:
Yes
Schedule:
Tampa - Birmingham
MSN:
500B-1191-97
YOM:
1962
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
1337
Captain / Total hours on type:
366.00
Aircraft flight hours:
20061
Circumstances:
The pilot was taking the airplane on a flight to another airport for maintenance. During the preflight inspection, the pilot turned on the electrical power and noticed that the fuel gauge was indicating 80 gallons of fuel. The pilot reported the airplane holds a maximum of 156 gallons of fuel and he calculated that he needed 113 gallons of fuel to legally complete the flight. He informed the fixed base operator (FBO) that he wanted the fuel tanks topped off, but was informed by the ramp technician that the fuel tanks were full and he did not need fuel. The pilot went back to the airplane and removed the fuel cap. He noticed fuel in the filler neck and assumed the fuel tanks were full. He did not push open the anti-siphon fuel valve to see if the tanks were full or if residual fuel was pooled on top of the anti-siphon fuel valve. When the pilot started the engines, he noticed the fuel gauge was flickering and thought it was malfunctioning. He proceeded to depart for the maintenance base. After about 2 hours of flight time both engines lost power. Unable to reach the closest airport, the pilot executed an off field landing in a cotton field. After landing, the airplane rolled into the trees and the left wing separated from the fuselage. The airplane sustained substantial damage to the left and right wings. According to the fueler at the FBO, she drove out to the airplane to fuel it on the morning of the accident and, after removing the single fuel cap, saw fuel on top of the anti-siphon valve. She used her finger to push down the valve and felt fuel, so she believed the airplane was full of fuel and it did not need additional fuel. Both wing fuel bladders were breached during the accident and a minor amount of fuel was leaked onto the ground. Personnel from the company who recovered the wreckage stated that there was no fuel in the fuel tanks when the airplane was recovered. The fuel quantity transmitter was sent to the manufacturer for examination. Testing of the transmitter revealed no anomalies with the unit. Based on this information, it is likely that the pilot erred in his assessment of the airplane’s fuel quantity prior to departing on the accident flight and that the available quantity of fuel was exhausted, which resulted in the total loss of engine power and the subsequent forced landing.
Probable cause:
The pilot’s failure to assure there was an adequate amount of fuel onboard to complete the flight, which resulted in a loss of engine power due to fuel exhaustion.
Final Report:

Crash of an Airbus A300-622R in Birmingham: 2 killed

Date & Time: Aug 14, 2013 at 0447 LT
Type of aircraft:
Operator:
Registration:
N155UP
Flight Type:
Survivors:
No
Schedule:
Louisville - Birmingham
MSN:
841
YOM:
2003
Flight number:
UPS1354
Crew on board:
2
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
2
Captain / Total flying hours:
6406
Captain / Total hours on type:
3265.00
Copilot / Total flying hours:
4721
Copilot / Total hours on type:
403
Aircraft flight hours:
11000
Aircraft flight cycles:
6800
Circumstances:
On August 14, 2013, about 0447 central daylight time (CDT), UPS flight 1354, an Airbus A300-600, N155UP, crashed short of runway 18 during a localizer non precision approach to runway 18 at Birmingham-Shuttlesworth International Airport (BHM), Birmingham, Alabama. The captain and first officer were fatally injured, and the airplane was destroyed by impact forces and postcrash fire. The scheduled cargo flight was operating under the provisions of 14 Code of Federal Regulations Part 121 on an instrument flight rules flight plan, and dark night visual flight rules conditions prevailed at the airport; variable instrument meteorological conditions with a variable ceiling were present north of the airport on the approach course at the time of the accident. The flight originated from Louisville International Airport-Standiford Field, Louisville, Kentucky, about 0503 eastern daylight time. A notice to airmen in effect at the time of the accident indicated that runway 06/24, the longest runway available at the airport and the one with a precision approach, would be closed from 0400 to 0500 CDT. Because the flight's scheduled arrival time was 0451, only the shorter runway 18 with a non precision approach was available to the crew. Forecasted weather at BHM indicated that the low ceilings upon arrival required an alternate airport, but the dispatcher did not discuss the low ceilings, the single-approach option to the airport, or the reopening of runway 06/24 about 0500 with the flight crew. Further, during the flight, information about variable ceilings at the airport was not provided to the flight crew.
Probable cause:
The NTSB determined that the probable causes of the crash were:
- The crew continued an unstabilized approach into Birmingham Airport,
- The crew failed to monitor the altitude and inadvertently descended below the minimum descent altitude when the runway was not yet in sight.
Contributing factors were:
- The flight crew's failure to properly configure the on-board flight management computer,
- The first officer's failure to make required call-outs,
- The captain's decision to change the approach strategy without communicating his change to the first officer,
- Flight crew fatigue.
Final Report:

Crash of a Cessna 441 Conquest II near Birmingham: 2 killed

Date & Time: Dec 10, 2003 at 1420 LT
Type of aircraft:
Registration:
N441W
Flight Phase:
Survivors:
No
Schedule:
Birmingham – Venice
MSN:
441-0181
YOM:
1980
Crew on board:
1
Crew fatalities:
Pax on board:
1
Pax fatalities:
Other fatalities:
Total fatalities:
2
Captain / Total flying hours:
8378
Captain / Total hours on type:
424.00
Aircraft flight hours:
5933
Circumstances:
The flight was climbing from 5,000 to 10,000 feet and the pilot obtained a maximum altitude of 6,300 feet. The airplane then began to lose altitude and deviate off course. The pilot declared a mayday and reported the airplane was in a spin. Several witnesses near the accident site reported hearing airplane engine noises and seeing the airplane descend from the clouds in a nose-down spiral to the ground. Two AIRMETs were valid at the time of the accident and included the accident location: "AIRMET TANGO update 3 for turbulence ... . Occasional moderate turbulence below a flight level of 18,000 feet due to wind shear ... ." "AIRMET ZULU update 2 for ice and freezing level ... . Occasional moderate rime and/or mixed icing in clouds and precipitation below 8,000 feet." Two pilots who departed in separate Beech 200 airplanes about the time of the accident airplane stated they encountered "moderate rime" icing between 5,000 and 6,000 feet, and one pilot reported instrument meteorological conditions and light turbulence between 1,800 to 6,000 feet. Examination of the airplane revealed no evidence of airframe or engine malfunction. The de-ice ejector flow control valves for the left wing, right wing, and empennage pneumatic boots were removed for examination, and all valves functioned when power was supplied.
Probable cause:
The pilot's failure to maintain adequate airspeed during climb in icing conditions, which resulted in an inadvertent stall / spin of the airplane and subsequent uncontrolled descent and collision with terrain. A factor was the accumulation of airframe ice.
Final Report:

Crash of a Beechcraft E18 in Birmingham: 1 killed

Date & Time: Jun 20, 1985 at 2101 LT
Type of aircraft:
Operator:
Registration:
N19T
Flight Phase:
Flight Type:
Survivors:
No
Schedule:
Birmingham - Atlanta
MSN:
BA-147
YOM:
1956
Flight number:
ABX74
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
1
Captain / Total flying hours:
10600
Captain / Total hours on type:
5000.00
Aircraft flight hours:
10936
Circumstances:
At 2045 the military flight, Dixie 06, contacted Birmingham approach and obtained clearance for a low approach followed by a full-stop landing on runway 05. At 2053, Dixie 06 reported a 4 mile final for a low approach to the local controller. At 2054:19, the local controller cleared ABX74, N19T, '...taxi position and hold five.' ABX74 was awaiting takeoff instructions on runway 05 when the collision occurred. Investigation revealed the local controller forgot ABX74. She became preoccupied with other traffic using runway 36. The local controller termed the traffic as busier than normal for a night operation. At the time of the accident, the tower was staffed with two air traffic controllers and an air traffic assistant. No supervisor or coordinator was available in the cab to detect controller overload and offer assistance. The pilot, sole on board, was killed. The military aircraft involved in the collision was a USAF Douglas RF-4C Phantom II registered 64-1032 with two pilots on board. They escaped uninjured.
Probable cause:
Occurrence #1: on ground/water collision with object
Phase of operation: standing - engine(s) operating
Findings
1. (c) identification of aircraft visually - not performed - atc personnel (lcl/gnd/clnc)
2. (c) diverted attention - atc personnel (lcl/gnd/clnc)
3. (c) visual separation - not maintained - atc personnel (lcl/gnd/clnc)
4. (c) mental performance overload - atc personnel (lcl/gnd/clnc)
5. (c) atc clearance - improper - atc personnel (lcl/gnd/clnc)
6. (c) supervision - inadequate - atc personnel (supervisor)
----------
Occurrence #2: fire
Phase of operation: other
Final Report:

Crash of a Beechcraft 100 King Air in Birmingham: 2 killed

Date & Time: Dec 1, 1974 at 2032 LT
Type of aircraft:
Registration:
N50PC
Survivors:
Yes
Schedule:
Chantilly - Birmingham
MSN:
B-19
YOM:
1970
Crew on board:
2
Crew fatalities:
Pax on board:
2
Pax fatalities:
Other fatalities:
Total fatalities:
2
Captain / Total flying hours:
4393
Captain / Total hours on type:
1991.00
Circumstances:
On a night approach to Birmingham Airport, the crew reported trim trouble to ATC and decided to initiate a go-around. While trying to gain altitude, the crew lost control of the airplane that stalled and crashed near the airport. Both pilots were killed while both passengers were seriously injured.
Probable cause:
The crew failed to obtain/maintain flying speed, causing the aircraft to stall. The following contributing factors were reported:
- Improper in-flight decisions or planning,
- Airframe ice,
- Icing conditions including sleet and freezing rain,
- Ice engine,
- The pilot commenced a go-around, reported trim trouble and lost control in steep nose up attitude.
Final Report: