Crash of a De Havilland DHC-2 Beaver I in Hesquiat Lake: 2 killed

Date & Time: Aug 16, 2013 at 1023 LT
Type of aircraft:
Operator:
Registration:
C-GPVB
Flight Phase:
Survivors:
Yes
Schedule:
Hesquiat Lake - Gold River
MSN:
871
YOM:
1956
Country:
Crew on board:
1
Crew fatalities:
Pax on board:
5
Pax fatalities:
Other fatalities:
Total fatalities:
2
Captain / Total flying hours:
17000
Circumstances:
At 1015 Pacific Daylight Time, the de Havilland DHC-2 (Beaver) floatplane (registration CGPVB, serial number 871), operated by Air Nootka Ltd., departed Hesquiat Lake, British Columbia, with the pilot and 5 passengers for Air Nootka Ltd.’s water aerodrome base near Gold River, British Columbia. Visibility at Hesquiat Lake was about 2 ½ nautical miles in rain, and the cloud ceiling was about 400 feet above lake and sea level. Approximately 3 nautical miles west of the lake, while over Hesquiat Peninsula, the aircraft struck a tree top at about 800 feet above sea level and crashed. Shortly after the aircraft came to rest, a post-crash fire developed. All 6 persons on board survived the impact, but the pilot and 1 passenger died shortly after. A brief 406 megahertz emergency locator transmitter signal was transmitted, and a search and rescue helicopter recovered the survivors at about 1600.
Probable cause:
Findings as to causes and contributing factors:
1. The pilot flew just above the tree tops into instrument meteorological conditions and rising terrain, and the aircraft struck a tree that was significantly taller than the others.
2. The pilot and 1 passenger did not exit the aircraft before it was consumed in the postimpact fire.
3. Air Nootka did not have effective methods to monitor its pilots’ in-flight decision making and associated practices. As a result, Air Nootka had no way to detect and correct unsafe behavior or poor decision making such as occurred on this flight.
Findings as to risk:
1. If aircraft are not fitted with technology to reduce fuel leakage or to eliminate ignition sources, the risk of post-impact fire is increased.
2. If aircraft are not equipped with shoulder harnesses for all seating positions then there is an increased risk of injuries.
3. If aircraft are not equipped with some alternate means of escape such as push-out windows, then there is a risk that post-crash structural deformation will jam doors shut and restrict exit for the occupants.
4. If companies operating under self-dispatch do not monitor their operations, they risk not being able to identify unsafe practices that are a hazard to flight crew and passengers.
5. If flight data recordings are not available to an investigation, this may preclude the identification and communication of safety deficiencies to advance transportation safety.
Final Report:

Crash of a De Havilland DHC-2 Beaver in Thorne Bay

Date & Time: Jul 24, 2013 at 1140 LT
Type of aircraft:
Operator:
Registration:
N4787C
Flight Phase:
Survivors:
Yes
Schedule:
Ketchikan – Shipley Bay
MSN:
1330
YOM:
1959
Crew on board:
1
Crew fatalities:
Pax on board:
3
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
19500
Captain / Total hours on type:
600.00
Aircraft flight hours:
33326
Circumstances:
The pilot reported that, while the float-equipped airplane was in cruise flight about 1,200 ft above ground level, the engine made a loud noise and lost partial power, so he maneuvered the airplane to land on a nearby lake. During the approach, the engine lost total power, and the airplane descended into an area of trees before reaching the lake, which resulted in substantial damage to the wings, fuselage, and empennage. The operator reported that the engine had been overhauled (zero-timed) 31 hours before the accident. A postaccident engine examination revealed metal fragments and heavy gouging damage to the rotating components within the crankcase. The bottom portion (crankshaft end) of the n°1 linkrod and its respective bushing were missing from the n°1 linkpin; the oil sump contained metal debris consistent with heavily damaged remnants of these (and other) components. The n°2 cylinder barrel and linkrod and the n°3 linkrod showed deformation to the left (in the direction of engine rotation). Based on the damage observed in the engine, it is likely that the event that initiated the engine failure involved either the the n°1 linkrod bushing or the bottom portion of the n°1 linkrod; however, the extensive damage to these components precluded determination of the failure mode.
Probable cause:
The failure of the n°1 linkrod bushing or the bottom portion of the linkrod, which resulted in a total loss of engine power.
Final Report:

Crash of a De Havilland DHC-2 Beaver I near Petersburg: 1 killed

Date & Time: Jun 4, 2013 at 1531 LT
Type of aircraft:
Operator:
Registration:
N616W
Flight Phase:
Survivors:
Yes
Site:
Schedule:
Petersburg - Petersburg
MSN:
1290
YOM:
1958
Crew on board:
1
Crew fatalities:
Pax on board:
6
Pax fatalities:
Other fatalities:
Total fatalities:
1
Captain / Total flying hours:
4841
Captain / Total hours on type:
1465.00
Aircraft flight hours:
34909
Circumstances:
The pilot reported that the accident flight was his fourth flight and the third tour flight of the day in a float-equipped airplane. The weather had deteriorated throughout the day with lowering ceilings, light rain, and fog on the mountain ridges. The pilot said that when approaching a mountain pass, he initiated a climb by adding a “little bit” of flap (about 1 pump of the flap handle actuator) but did not adjust the engine power from the cruise power setting. He noted his airspeed at 80 knots, with a 200-feet-per-minute climb on the vertical speed indicator. He was having difficulty seeing over the cowling due to the nose-high attitude, when he suddenly noticed trees in his flight path. He initiated an immediate left turn; the airplane stalled, and began to drop, impacting the mountainous, tree-covered terrain. A passenger reported that the weather conditions at the time of the accident consisted of tufts of low clouds, and good visibility. They did not enter the clouds at any time during the flight. He reported that the airplane made a left turn, stalled, and then made a sharp left turn right before impact. The airplane seemed to be operating fine, and he heard no unusual sounds, other than the engine speed seemed to increase significantly right before impact. The pilot reported that there were no preaccident mechanical anomalies that would have precluded normal operation, and the postaccident examination of the airframe and engine revealed no evidence of mechanical malfunctions or failures that would have precluded normal operation.
Probable cause:
The pilot’s failure to maintain adequate altitude above the trees, and his subsequent failure to maintain adequate airspeed while maneuvering to avoid the trees, which resulted in an
inadvertent aerodynamic stall/spin and an uncontrolled descent.
Final Report:

Crash of a De Havilland DHC-2 Beaver in Big River Lake

Date & Time: Aug 25, 2012 at 0800 LT
Type of aircraft:
Operator:
Registration:
N314HA
Survivors:
Yes
Schedule:
Soldotna - Big River Lake
MSN:
868
YOM:
1956
Location:
Crew on board:
1
Crew fatalities:
Pax on board:
5
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
1500
Captain / Total hours on type:
725.00
Aircraft flight hours:
20174
Circumstances:
The pilot of a float-equipped airplane was landing at a remote lake. The pilot stated that he was on a left base leg turning onto a short final approach when the left float struck the ground. The airplane sustained substantial damage to the wings and fuselage. The pilot indicated there were no preaccident mechanical malfunctions or anomalies that would have precluded normal operation. Accident occurred in Big River Lake, in the Kenai region.
Probable cause:
The pilot’s failure to maintain adequate ground clearance during his landing approach, which resulted in a collision with terrain.
Final Report:

Crash of a De Havilland DHC-2 Beaver in Lillabelle Lake: 2 killed

Date & Time: May 25, 2012 at 1408 LT
Type of aircraft:
Operator:
Registration:
C-FGBF
Survivors:
Yes
Schedule:
Edgar Lake - Lillabelle Lake
MSN:
168
YOM:
1952
Country:
Crew on board:
1
Crew fatalities:
Pax on board:
2
Pax fatalities:
Other fatalities:
Total fatalities:
2
Captain / Total flying hours:
1100
Captain / Total hours on type:
300.00
Aircraft flight hours:
22000
Circumstances:
The Cochrane Air Service de Havilland DHC-2 Mk.1 Beaver floatplane (registration C-FGBF, serial number 168) departed Edgar Lake, Ontario, with 2 passengers and 300 pounds of cargo on board. The aircraft was destined for the company’s main base located on Lillabelle Lake, Ontario, approximately 77 miles to the south. On arrival, a southwest-bound landing was attempted across the narrow width of the lake, as the winds favoured this direction. The pilot was unable to land the aircraft in the distance available and executed a go-around. At 1408, Eastern Daylight Time, shortly after full power application, the aircraft rolled quickly to the left and struck the water in a partially inverted attitude. The aircraft came to rest on the muddy lake bottom, partially suspended by the undamaged floats. The passenger in the front seat was able to exit the aircraft and was subsequently rescued. The pilot and rear-seat passenger were not able to exit and drowned. The emergency locator transmitter activated on impact.
Probable cause:
Findings as to Causes and Contributing Factors:
1. On the windward side of the landing surface, there was significant mechanical turbulence and associated wind shear caused by the passage of strong gusty winds over surface obstructions.
2. During the attempted overshoot, the rapid application of full power caused the aircraft to yaw to the left, and a left roll quickly developed. This movement, in combination with a high angle of attack and low airspeed, likely caused the aircraft to stall. The altitude available to regain control before striking the water was insufficient.
3. The pilot survived the impact, but was unable to exit the aircraft, possibly due to difficulties finding or opening an exit. The pilot subsequently drowned.
4. The rear-seat passenger did not have a shoulder harness and was critically injured. The passenger’s head struck the pilot’s seat in front; this passenger did not exit the aircraft and drowned.
Findings as to Risk:
1. Without a full passenger safety briefing, there is increased risk that passengers may not use the available safety equipment or be able to perform necessary emergency functions in a timely manner to avoid injury or death.
2. Not wearing a shoulder harness can increase the risk of injury or death in an accident.
3. Not having a stall warning system increases the risk that the pilot may not be aware of an impending aerodynamic stall.
4. Commercial seaplane pilots who do not receive underwater egress training are at increased risk of being unable to exit the aircraft following a survivable impact with water.
Final Report:

Crash of a De Havilland DHC-2 Beaver near Peachland: 3 killed

Date & Time: May 13, 2012 at 1845 LT
Type of aircraft:
Operator:
Registration:
C-GCZA
Flight Phase:
Flight Type:
Survivors:
No
Site:
Schedule:
Okanagan Lake - Pitt Meadows
MSN:
1667
YOM:
1966
Country:
Crew on board:
1
Crew fatalities:
Pax on board:
2
Pax fatalities:
Other fatalities:
Total fatalities:
3
Captain / Total flying hours:
420
Captain / Total hours on type:
50.00
Circumstances:
The privately operated de Havilland DHC-2 MK 1 amphibious floatplane (registration C-GCZA, serial number 1667) departed Okanagan Lake, near Kelowna, for a daytime flight under visual flight rules to Pitt Meadows, British Columbia, with the pilot and 2 passengers on board. While enroute, the aircraft struck trees and collided with terrain close to and 100 feet below the level of Highway 97C, near the Brenda Mines tailings hill. At 1850 Pacific Daylight Time, a brief 406-megahertz emergency-locator-transmitter signal was detected, which identified the aircraft; however, a location could not be determined. Most of the aircraft was consumed by a post-impact fire. The 3 occupants were fatally injured.
Probable cause:
There was no indication that an aircraft system malfunction contributed to this occurrence. There were no drastic changes in the aircraft’s flight path, and no emergency calls from the pilot to indicate that an in-flight emergency was experienced. The constant ground speed and flight path would also suggest that the aircraft was under the control of the pilot. As a result, this analysis will focus on the phenomenon of controlled flight into terrain (CFIT).
Findings as to Causes and Contributing Factors:
1. The combination of relatively high weight, effects of density altitude, and down-flowing air likely reduced the climb performance of the aircraft, resulting in the aircraft’s altitude being lower than anticipated at that stage in the flight.
2. The pilot’s vision was likely impaired by the sun, and the pilot may have been exposed to visual illusions; both were factors that contributed to the pilot not noticing the trees and the rising terrain, and colliding with them.
Findings as to Risk:
1. Visual illusions cause false impressions or misconceptions of actual conditions. Unrecognized and uncorrected spatial disorientation, caused by illusions, carries a high risk of incident or accident.
2. When there are no special departure procedures published for airports in mountainous regions surrounded by high terrain, there is a risk of pilots departing the valley at an altitude too low for terrain clearance.
Other Findings:
1. Information from the Wide Area Multilateration system was not preserved following the occurrence, as local NAV CANADA personnel were not aware that unfiltered data were only available for a limited time.
Final Report:

Crash of a De Havilland DHC-2 Beaver near Niblack

Date & Time: Mar 13, 2012 at 1040 LT
Type of aircraft:
Operator:
Registration:
N82SF
Flight Phase:
Survivors:
Yes
Schedule:
Niblack - Ketchikan
MSN:
839
YOM:
1955
Location:
Crew on board:
1
Crew fatalities:
Pax on board:
1
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
23000
Captain / Total hours on type:
12000.00
Aircraft flight hours:
17574
Circumstances:
The pilot departed from an off-airport site in marginal visual flight rules conditions. Shortly after departure, the weather worsened, and flight visibility dropped to near zero in heavy snow. He attempted to follow the shoreline at a low altitude but was unable to maintain visual contact with the ground. He stated that he saw trees immediately in front of the airplane and attempted a right turn toward what he thought was an open bay. During the turn, the right float contacted a rock outcrop, and the airplane impacted the water. The pilot did not report any mechanical anomalies that would have precluded normal operation.
Probable cause:
The pilot's decision to depart in marginal visual meteorological conditions, and his continued visual flight into instrument meteorological conditions.
Final Report:

Crash of a De Havilland DHC-2 Beaver near Buss Lakes: 5 killed

Date & Time: Jun 30, 2011 at 1111 LT
Type of aircraft:
Registration:
C-GUJX
Flight Phase:
Survivors:
No
Schedule:
Buss Lakes - Southend
MSN:
1132
YOM:
1958
Country:
Crew on board:
1
Crew fatalities:
Pax on board:
4
Pax fatalities:
Other fatalities:
Total fatalities:
5
Captain / Total flying hours:
4023
Captain / Total hours on type:
3664.00
Aircraft flight hours:
12746
Circumstances:
The Lawrence Bay Airways Ltd. float-equipped de Havilland DHC-2 (registration C-GUJX, serial number 1132) departed from a lake adjacent to a remote fishing cabin near Buss Lakes for a day visual flight rules flight to Southend, Saskatchewan, about 37 nautical miles (nm) southeast. There were 4 passengers and 1 pilot onboard. The aircraft crashed along the shoreline of another lake located about 2 nm southeast of its point of departure. The impact was severe and the 5 occupants were killed on impact. The emergency locator transmitter activated, and the aircraft was found partially submerged in shallow water with the right wing tip resting on the shore. There was no post-crash fire. The accident occurred during daylight hours at about 1111 Central Standard Time.
Probable cause:
Findings as to Causes and Contributing Factors:
While manoeuvring at low level, the aircraft's critical angle of attack was likely exceeded and the aircraft stalled. The stall occurred at an altitude from which recovery was not possible.
Other Findings:
The separation of the propeller blade tip likely resulted from impact forces.
The investigation could not determine whether the fuel pressure warning light was illuminated prior to the accident.
Final Report: