Crash of a Learjet 23 off Muskegon

Date & Time: Oct 25, 1967 at 1108 LT
Type of aircraft:
Registration:
N432EJ
Survivors:
Yes
MSN:
23-028
YOM:
1965
Crew on board:
2
Crew fatalities:
Pax on board:
2
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
10278
Captain / Total hours on type:
820.00
Circumstances:
While on approach to Muskegon County Airport, both engines failed simultaneously. The aircraft stalled and crashed into Lake Michigan. All four occupants were quickly rescued while the aircraft was lost.
Probable cause:
Failure of both engines while on approach after the compressors stalled due to ice ingestion.
Final Report:

Crash of a Beechcraft C-45G in Saskatchewan: 5 killed

Date & Time: Oct 5, 1967 at 1450 LT
Type of aircraft:
Registration:
N505N
Flight Phase:
Survivors:
No
MSN:
AF-19
YOM:
1952
Country:
Crew on board:
1
Crew fatalities:
Pax on board:
4
Pax fatalities:
Other fatalities:
Total fatalities:
5
Captain / Total flying hours:
771
Circumstances:
En route, weather conditions worsened and the pilot decided to reduce his altitude in an attempt to maintain a visual contact with the ground. While cruising at an altitude of some 250 feet, the twin engine aircraft struck a radio antenna and crashed in flames in a field. All five occupants were killed.
Probable cause:
The pilot took the decision to continue under VFR mode in adverse weather conditions. Due to improper in-flight decisions, he failed to see and avoid the radio antenna.
Final Report:

Crash of a Dassault Falcon 20C in Goose Bay

Date & Time: Oct 1, 1967
Type of aircraft:
Registration:
HB-VAP
Survivors:
Yes
Schedule:
Geneva – Keflavik – Goose Bay
MSN:
37
YOM:
1966
Country:
Crew on board:
3
Crew fatalities:
Pax on board:
4
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
The aircraft was completing a transatlantic flight from Geneva to Goose Bay with an intermediate stop in Keflavik. On final approach to Goose Bay Airport, both engines failed simultaneously. The crew realized he could not reach the airport so the captain decided to attempt an emergency landing. The airplane belly landed, slid for several yards and came to rest 11 km short of runway. All seven occupants were rescued while the aircraft was damaged beyond repair.
Probable cause:
Double engine failure on approach caused by a fuel exhaustion.

Crash of a Rockwell Aero Commander 560E in Dallas: 7 killed

Date & Time: Sep 27, 1967 at 1536 LT
Operator:
Registration:
N3831C
Survivors:
No
Site:
MSN:
560-747
YOM:
1959
Crew on board:
1
Crew fatalities:
Pax on board:
6
Pax fatalities:
Other fatalities:
Total fatalities:
7
Captain / Total flying hours:
13247
Captain / Total hours on type:
2010.00
Circumstances:
While on approach to Dallas-Love Field Airport, the left wing broke away and control was lost. The airplane entered a dive and crashed on the elementary school of Bradfield. All seven occupants on board the airplane were killed while no one on the ground was injured. The school was partially destroyed as well as several vehicles. The airplane was operated on behalf of LTV Electrosystems (Ling-Temco-Vought).
Probable cause:
Uncontrolled descent following the structural failure of the left wing due to fatigue fracture. Two overlapping rivet holes found in aft leg of the spar cap.
Final Report:

Crash of a Grumman G-159 Gulfstream I in Harrisburg

Date & Time: Jul 25, 1967 at 1535 LT
Type of aircraft:
Operator:
Registration:
N205M
Survivors:
Yes
MSN:
62
YOM:
1961
Crew on board:
2
Crew fatalities:
Pax on board:
6
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
16880
Captain / Total hours on type:
1668.00
Circumstances:
The approach to Harrisburg-Capital City Airport was completed in poor weather conditions. After touchdown on a wet runway, the crew encountered difficulties to decelerate and the captain eventually decided to make a sharp turn to avoid an overrun. The aircraft veered off runway, lost its undercarriage and came to a halt. While all eight occupants were uninjured, the airplane was damaged beyond repair.
Probable cause:
Wrong approach configuration on part of the crew who selected the wrong runway relative to existing wind and failed to initiate a go-around. The landing procedure was completed at an excessive speed of 105 knots with a tailwind of 9 knots.
Final Report:

Crash of a Douglas C-47B-10-DK near Sontecomapan: 7 killed

Date & Time: May 17, 1967
Operator:
Registration:
XC-BII
Flight Phase:
Survivors:
No
Schedule:
Poza Rica – Minatitlán
MSN:
14836/26281
YOM:
1944
Country:
Crew on board:
3
Crew fatalities:
Pax on board:
4
Pax fatalities:
Other fatalities:
Total fatalities:
7
Circumstances:
The airplane crashed in unknown circumstances in an isolated area located 13 km southeast of Sontecomapan, State of Veracruz. The wreckage was found a month later, on June 17. All seven occupants have been killed.

Crash of a Beechcraft King Air A90 in Endicott: 3 killed

Date & Time: Apr 16, 1967 at 2223 LT
Type of aircraft:
Operator:
Registration:
N129GP
Survivors:
Yes
MSN:
LJ-216
YOM:
1967
Crew on board:
2
Crew fatalities:
Pax on board:
3
Pax fatalities:
Other fatalities:
Total fatalities:
3
Captain / Total flying hours:
13389
Captain / Total hours on type:
41.00
Circumstances:
The crew started the descent to Endicott-Tri Cities Airport by night and poor weather conditions consisting of fog, rain falls and low clouds. On approach, the twin engine aircraft was too low, struck tree tops and crashed few miles short of runway threshold. Both pilots and a passenger were killed while two passengers were seriously injured.
Probable cause:
Improper IFR operations on part of the flying crew who was being radar vectored to over Tri-Cities Airport but was not authorized to attempt an instrument approach. Poor weather conditions were considered as a contributing factor.
Final Report:

Crash of a Rockwell Aero Commander 680E in Minneapolis: 1 killed

Date & Time: Dec 9, 1966 at 1543 LT
Registration:
N8496C
Flight Phase:
Survivors:
No
MSN:
680E-846-71
YOM:
1960
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
1
Captain / Total flying hours:
4826
Captain / Total hours on type:
117.00
Circumstances:
Shortly after takeoff from Minneapolis-World Chamberlain Airport, while climbing, the pilot informed ATC about fire on board and that smoke spread in the cabin and cockpit. He elected to make an emergency landing when control was lost and the airplane crashed in flames on Interstate highway. The aircraft was destroyed and the pilot was killed.
Probable cause:
It was determined that a fire broke out in the baggage compartment for unknown reason.
Final Report:

Crash of a Dornier DO.28B/1 in Alberta

Date & Time: Dec 7, 1966
Type of aircraft:
Registration:
CF-RZG
MSN:
3070
Location:
Country:
Crew on board:
0
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
Crashed in unknown circumstances at an oilstrip owned by the Home Oil Company somewhere in Alberta. The occupant's fate remains unknown.

Crash of a Lockheed 18-56-23 LodeStar in Chicago

Date & Time: Nov 17, 1966 at 1652 LT
Type of aircraft:
Operator:
Registration:
N339
Flight Phase:
Survivors:
Yes
Schedule:
Chicago – Pittsburgh
MSN:
2588
YOM:
1943
Crew on board:
2
Crew fatalities:
Pax on board:
6
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
12811
Captain / Total hours on type:
2365.00
Circumstances:
During the takeoff roll at Chicago-Merrill C. Meigs Airport, prior to V1 speed, a fire warning alarm sounded. The crew decided to abort the takeoff and started an emergency braking procedure. Unable to stop within the remaining distance, the twin engine aircraft overran and plunged into Lake Michigan. All eight occupants were evacuated safely while the aircraft was damaged beyond repair.
Probable cause:
Inadequate preflight preparation and/or planning on part of the flying crew. The following findings were reported:
- Inadequate maintenance and inspection on part of the maintenance personnel,
- Parts were missing on the exhaust system: manifolds,
- Despite the takeoff was interrupted prior to V1, the remaining distance was insufficient as the runway was slick and too short,
- False fire warning,
- Airport conditions.
Final Report: