Crash of a Grumman G-44A Widgeon in Big Lake: 1 killed

Date & Time: Jul 30, 1983 at 1600 LT
Type of aircraft:
Operator:
Registration:
N1423
Flight Phase:
Flight Type:
Survivors:
Yes
Schedule:
Big Lake - Big Lake
MSN:
1423
YOM:
1945
Location:
Crew on board:
1
Crew fatalities:
Pax on board:
1
Pax fatalities:
Other fatalities:
Total fatalities:
1
Captain / Total flying hours:
3726
Captain / Total hours on type:
420.00
Aircraft flight hours:
1200
Circumstances:
The aircraft crashed in a level, wooded area. The initial impact with trees occurred approximately 40 feet agl. Both wing tips and a portion of the left stabilizer and elevator were found at the bases of the trees that were first impacted. From the first impact point, the wreckage was disintegrated and scattered over an area that was 30 feet wide and 140 feet long. No known eye witnesses were reported. However, a short time before the accident, the aircraft was observed being flown in abrupt maneuvers and buzzing boats. A toxicological exam of the pilot's blood showed an alcohol level of 2,41‰. An exam of the wreckage was made, but no preimpact/mechanical malfunction or failures were found. The passenger was killed while the pilot was seriously injured.
Probable cause:
Occurrence #1: in flight collision with terrain/water
Phase of operation: maneuvering
Findings
1. (c) judgment - poor - pilot in command
2. (c) impairment (alcohol) - pilot in command
3. (c) buzzing - performed - pilot in command
4. (c) maneuver - excessive - pilot in command
5. (c) clearance - misjudged - pilot in command
Final Report:

Crash of a Grumman G-21A Goose off Cape Yakataga

Date & Time: Feb 20, 1982 at 1310 LT
Type of aircraft:
Operator:
Registration:
N2845D
Flight Phase:
Flight Type:
Survivors:
Yes
Schedule:
Anchorage - Hollywood
MSN:
B112
YOM:
1945
Crew on board:
2
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
3628
Captain / Total hours on type:
40.00
Aircraft flight hours:
2941
Circumstances:
Aircraft departed Merrill Field at 1110 with 220 gallons of fuel. Two hours later both engines quit while flying at an altitude of 6,500 feet approximately 10 miles offshore. The crew was unable to restart the engines and the aircraft was ditched into 12 to 15 foot waves with a 40 knot surface wind. The right float was torn off and both engine mounts broke. The aircraft sank at 1745 and was not recovered. The aircraft had an annual inspection 4 days prior to the accident. The fueling facilities were checked and found free of water or other contaminants.
Probable cause:
Occurrence #1: loss of engine power
Phase of operation: cruise - normal
Findings
1. (c) reason for occurrence undetermined
----------
Occurrence #2: ditching
Phase of operation: landing - flare/touchdown
Findings
2. (c) terrain condition - water,rough
3. (f) weather condition - high wind
4. (f) weather condition - unfavorable wind
Final Report: