Crash of a Cessna 421B Golden Eagle II off Stauning

Date & Time: May 21, 1999 at 0002 LT
Operator:
Registration:
OY-BIM
Flight Phase:
Flight Type:
Survivors:
Yes
Schedule:
Stauning - Manchester
MSN:
421B-0878
YOM:
1974
Country:
Region:
Crew on board:
2
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
3706
Captain / Total hours on type:
361.00
Copilot / Total flying hours:
650
Copilot / Total hours on type:
54
Aircraft flight hours:
5518
Circumstances:
The twin engine aircraft departed Stauning Airport at 0000LT on a cargo flight to Manchester with two pilots on board. Shortly after takeoff from runway 27, while in initial climb by night, the crew declared an emergency after the main cabin door opened. The captain reduced both engines power and the aircraft crash landed on the Klægbanke, less than 4 km from the airport. Both pilots were rescued an hour later (they were uninjured) and the aircraft was damaged beyond repair.
Probable cause:
The main cabin door opened during initial climb because the crew failed to ensure it was properly closed. Investigations reported that the door locking mechanism was not properly adjusted and that the crew did not identify the abnormal situation. The following factors were identified:
- The captain immediately reduced power on both engines when the door opened,
- The captain was not properly trained,
- The operator did not ensure that the crew was qualified and trained to perform this type of flight,
- The crew failed to follow the pre departure checklist,
- The crew's attention was focused on the door that opened at a critical moment of the flight and failed to continue the flight and monitor the various instruments.
Final Report:

Ground fire of a Swearingen SA226AT Merlin IV in Copenhagen

Date & Time: Nov 12, 1982 at 1811 LT
Operator:
Registration:
OY-AUI
Survivors:
Yes
Schedule:
Stauning - Copenhagen
MSN:
AT-015
YOM:
1974
Flight number:
DX386
Country:
Region:
Crew on board:
2
Crew fatalities:
Pax on board:
13
Pax fatalities:
Other fatalities:
Total fatalities:
0
Aircraft flight hours:
2395
Circumstances:
The aircraft was completing flight DX386 from Stauning to Copenhagen. It departed Stauning at 1724LT with 13 passengers and a crew of two on board. During approach to runway 22L at Kastrup Airport, the captain noticed a faint smell of burnt insulation and asked the copilot if he could smell anything "hot". The copilot who could not confirm the smell was asked by the captain to turn the cabin temperature - which was operated in manual mode - towards cold. The captain checked indication and warning systems for generators, batteries, circuit breakers and continued the approach. After a normal approach and landing at 18:07 hours the aircraft was cleared to the parking area via taxiway two and to change frequency to Apron Tower when clear of the runway. After contact with Apron Tower instructions were received for taxi to parking via taxiway two and inner perimeter but one minute later new instructions were received to taxi via runway three zero. While taxiing the left engine was shut down as is normal company procedure and taxiing continued on the right engine. Suddenly the captain noticed a flash outside the aircraft. The captain's first thought was that fire had started in the left engine or in the brakes and he brought the aircraft to a halt to investigate. Very shortly after a flash fire erupted in the left hand cockpit side console aft of and close to the captain's left leg. The crew made no radio transmissions about the fire since all electrical power was immediately turned off, in accordance with emergency procedure, after the aircraft was brought to a stop. The captain shouted towards the cabin: "It is burning, out". The passengers and crew then vacated the aircraft. The accident occurred at or about 18:11 hours on runway 30 during darkness. All 15 occupants escaped uninjured.
Probable cause:
An intense fire had erupted in the aft end of the left hand cockpit side console/ originating from an electrical short to ground. Contributing to the intensity of the fire was escaping oxygen under 70 PSI pressure through a melted PVC oxygen tube.