Zone

Crash of a Cessna 402C in Hampton

Date & Time: May 9, 2020 at 1513 LT
Type of aircraft:
Operator:
Registration:
N4661N
Survivors:
Yes
Schedule:
Peachtree City - Peachtree City
MSN:
402C-0019
YOM:
1979
Crew on board:
2
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
7330
Captain / Total hours on type:
11.00
Copilot / Total flying hours:
1096
Copilot / Total hours on type:
5
Aircraft flight hours:
17081
Circumstances:
According the commercial pilot and a flight instructor rated check pilot, they were conducting their first long-duration, aerial observation flight in the multiengine airplane, which was recently acquired by the operator. They departed with full fuel tanks, competed the 5-hour aerial observation portion of the flight, and began to return to the destination airport. About 15 miles from the airport, the left engine fuel warning light illuminated. Within a few seconds, the right engine stopped producing power. They attempted to restart the engine and turned the airplane toward an alternate airport that was closer. The pilots then turned on the electric fuel pump, the right engine began surging, and soon after the left engine stopped producing power. They turned both electric fuel pumps to the low setting, both engines continued to surge, and the pilots continued toward the alternate airport. When they were about 3 miles from the airport, both engines lost total power, and they elected to land on a highway. When they were a few feet above the ground, power returned briefly to the left engine, which resulted in the airplane climbing and beginning to roll. The commercial pilot pulled the yoke aft to avoid a highway sign, which resulted in an aerodynamic stall, and subsequent impact with trees and terrain. The airplane sustained substantial damage to the wings and fuselage. Although both pilots reported the fuel gauges indicated 20 gallons of fuel remaining on each side when the engines stopped producing power, the flight instructor noted that there was no fuel in the airplane at the time of the accident. In addition, according to a Federal Aviation Administration inspector who responded to the accident site, both fuel tanks were breached and there was no evidence of fuel spillage.
Probable cause:
A dual total loss of engine power as a result of fuel exhaustion.
Final Report:

Crash of a Cessna 501 Citation I/SP near Fairmount: 4 killed

Date & Time: Feb 8, 2020 at 1013 LT
Type of aircraft:
Operator:
Registration:
N501RG
Flight Phase:
Flight Type:
Survivors:
No
Schedule:
Peachtree City - Nashville
MSN:
501-0260
YOM:
1982
Crew on board:
2
Crew fatalities:
Pax on board:
2
Pax fatalities:
Other fatalities:
Total fatalities:
4
Captain / Total flying hours:
805
Copilot / Total flying hours:
5924
Copilot / Total hours on type:
55
Aircraft flight hours:
8078
Circumstances:
While on an instructional flight in icing and instrument meteorological conditions (IMC), the pilots indicated that they were having instrumentation difficulties to air traffic control. They initially reported a problem with the autopilot, then a navigational issue, which they later indicated were resolved, and finally they reported it was a problem with the left side attitude indicator. After air traffic control cleared them to their destination, the airplane entered a descending left turn, which continued into a 360° descending turn. An inflight breakup resulted, with the wreckage being scattered over 7,000 ft of wooded terrain. Examination of the engines revealed there were no anomalies that would have precluded normal operation prior to the accident. Control cable continuity was established from the flight controls in the cockpit to all flight control surfaces through multiple overload failures. The pitot-static system was examined, and no blockages were noted. Since there was rotational scoring noted on the vertical gyro and the directional gyro, it’s likely they were operating at the time of the accident. Furthermore, the left side attitude indicator examination revealed that there were no anomalies with the instrument. Examination of the deice valves for the deicing boots revealed that the left wing deice valve did not operate. Corrosion was visible in all three valves and it could not be determined if the corrosion was a result of postimpact environmental exposure. Furthermore, since the cockpit switch positions were compromised in the accident, it could not be determined if the pilots were operating the deicing system at the time of the accident. However, most of the pilot reports (PIREPs) in the area indicated light icing and the airplane performed a 6,000 ft per minute climb just before the loss of control. Given this information, it is unlikely the icing conditions made the airplane uncontrollable. A review of the pilots’ flight experience revealed that the pilot in the left seat did not hold a type rating for the accident airplane model but was scheduled to attend flight training to obtain such a type rating. The pilot in the right seat, who also held a flight instructor certificate, did hold a type rating for the airplane. Given that the remarks section of the filed flight plan described the flight as a “training flight” and the left-seat pilot’s plan to obtain a type rating for the accident airplane model, it is likely the pilot in the left seat was the flying pilot for the majority of the flight. Although the right-seat pilot's autopsy noted coronary artery disease, the condition was poorly described. The circumstances of the accident are not consistent with sudden physical impairment or incapacitation; therefore, it is unlikely it contributed to the event. Toxicology testing identified diphenhydramine, which can cause significant sedation, in the right-seat pilot’s blood. However, the level present at the time of the accident was too low to quantify. Therefore, it is unlikely effects from diphenhydramine contributed to the accident. Prior to entering the descending right turn, air traffic control noted that the airplane was not following assigned headings and altitudes and the pilots’ reported having autopilot problems. Subsequently, the pilots’ reported they were using the right attitude indicator as they had difficulties with the left-side indicator. Information was insufficient to evaluate whether the reported difficulties were the result of a malfunction of the autopilot or the pilots’ management of the autopilot system. However, the reported difficulties likely increased the pilots’ workload, may have diverted their attention while operating in IMC and icing conditions, resulting in task saturation, and may have increased their susceptibility to spatial disorientation. It is also possible that the onset of spatial disorientation was the beginning of the pilots’ difficulties maintaining the airplane’s flight track and what they perceived to be an instrumentation problem. Regardless, since the left seat pilot was not rated to fly the airplane, the right seat pilot’s workload would have increased by having to diagnose the issue, assess the situation, and maintain positive airplane control. The airplane’s track data are consistent with the known effects of spatial disorientation, leading to an inflight loss of control and subsequent inflight breakup.
Probable cause:
The pilots’ loss of control in flight in freezing instrument meteorological conditions due to spatial disorientation and the cumulative effects of task saturation.
Final Report:

Crash of a Piper PA-46-350P Malibu in Peachtree City: 2 killed

Date & Time: Jan 16, 1996 at 0900 LT
Registration:
N9210F
Survivors:
No
Schedule:
Lakeland – Peachtree City
MSN:
46-22119
YOM:
1991
Crew on board:
2
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
2
Captain / Total flying hours:
1080
Captain / Total hours on type:
92.00
Aircraft flight hours:
1064
Circumstances:
During the preflight briefing, the pilot was informed of reduced visibility and low ceiling in the vicinity of the destination airport, at the approximate time of the planned arrival. Upon arriving in the Atlanta area, the pilot was issued radar vectors to a final for the localizer runway 31 approach. The pilot was also given the current Atlanta altimeter setting, and was cleared for the localizer runway 31 approach. The airplane collided with a 60-foot tall light pole at a nearby baseball complex 2 miles short of the runway. The weather observation from the Hartsfield International Airport indicated that visual weather conditions prevailed at the time of the accident. However, according to a witness at the accident site, the weather conditions were foggy with reduced visibility. The wreckage distribution path was 2,467 feet right of the localizer course. The minimum descent altitude for this approach, using Atlanta's altimeter setting, was 1260 feet. The ground check of the localizer and DME facility was within normal operating range. Examination of the aircraft navigational radios also tested within normal ranges. The average field elevation in the vicinity of the accident site is 800 feet. The pilot's toxicological examinations detected pseudoephedrine (decongestant), phenylpropanolamine (decongestant), and chlorpheniramine (antihistamine). No samples were available to quantify the blood levels of these medications.
Probable cause:
The pilot's failure to follow the published instrument approach procedure. The fog was a factor.
Final Report: