Zone

Crash of a Rockwell Shrike Commander 500S off Key West

Date & Time: Aug 13, 2023 at 1020 LT
Operator:
Registration:
N62WE
Flight Phase:
Flight Type:
Survivors:
Yes
Schedule:
Orlando - Key West
MSN:
500-3317
YOM:
1978
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
975
Captain / Total hours on type:
338.00
Aircraft flight hours:
3997
Circumstances:
The pilot was enroute to the destination airport and overflying the Gulf of Mexico when about 15 nautical miles from the airport and at an altitude of 3,000 ft, the right engine suddenly lost power. The pilot described that about that time, the fuel totalizers indicated that 48 gallons of fuel were onboard, and his fuel quantity gauge indicated similarly. He then contacted air traffic control and declared an emergency. Shortly thereafter, the left engine also suddenly lost power. The pilot attempted to troubleshoot the issue and restart both engines but was unsuccessful. He subsequently ditched the airplane and was rescued from the water without injury. The airplane was not recovered and could not be examined after the accident, therefore the reason for the loss of engine power could not be determined.
Probable cause:
A total loss of engine power for reasons that could not be determined.
Final Report:

Crash of a Beechcraft 200 Super King Air in Orlando

Date & Time: Sep 10, 2016 at 1530 LT
Registration:
N369CD
Flight Type:
Survivors:
Yes
Schedule:
Marathon – Orlando
MSN:
BB-110
YOM:
1976
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
5000
Captain / Total hours on type:
50.00
Aircraft flight hours:
10321
Circumstances:
The pilot of a multi-engine turboprop airplane reported that during the landing flare he encountered a crosswind gust, which pushed the airplane to the right of the runway centerline. The pilot further reported that he applied power to abort the landing, but the airplane touched down in the grass to the right of the runway. After the wheels touched down in the grass, he reported that the power added "caught up with the aircraft," but the airplane was rolling toward trees and hangars. Subsequently, the pilot pulled the power to idle, but the right wing impacted a tree and the right main landing gear and nose wheel collapsed. A post-crash fire ensued after the collision and the right wing sustained substantial damage. The pilot reported no preaccident mechanical malfunctions or failures with the airplane that would have precluded normal operation. There was no record of the observed weather at the airport during the accident. An automated weather observing system about 14 nautical miles from the accident airport, near the time of the accident, recorded the wind variable at 5 knots.
Probable cause:
The pilot's failure to maintain directional control during an attempted aborted landing in gusty crosswind conditions, which resulted in a runway excursion and an impact with a tree.
Final Report: