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Crash of a Beechcraft 65 Queen Air in Lawrenceville: 1 killed

Date & Time: Feb 8, 2010 at 1705 LT
Type of aircraft:
Registration:
N130SP
Flight Phase:
Flight Type:
Survivors:
Yes
Schedule:
Lawrenceville - Lawrenceville
MSN:
LF-17
YOM:
1960
Crew on board:
1
Crew fatalities:
Pax on board:
3
Pax fatalities:
Other fatalities:
Total fatalities:
1
Captain / Total flying hours:
10099
Captain / Total hours on type:
1332.00
Aircraft flight hours:
9234
Circumstances:
During the preflight inspection, some water was present in the fuel sample; it was drained until a clear sample was observed. Subsequently, the fuel tanks were topped off, and the remaining preflight inspection revealed no other anomalies. The pilot initiated a takeoff and upon reaching rotation speed, the airplane became airborne and the landing gear was retracted. The right engine immediately lost power, and the pilot feathered the engine and attempted to return to the airport. Shortly thereafter, the left engine lost power. The pilot informed the air traffic controller that the airplane had lost all power. The airplane subsequently collided with trees and terrain and a post crash fire ensued. A postaccident examination of the airframe and engine revealed no mechanical malfunctions or failures that would have precluded normal operation. Examination of fuel retrieved from the right main fuel tank, as well as fuel from the fixed base operator, revealed no anomalies. The left fuel selector valve was observed in the plugged port (no fluid flow) position, but it was most likely moved to that position during the accident sequence. The right fuel selector valve was partially aligned with the main fuel passageway and was unobstructed. The reason for the loss of engine power to both engines was not determined.
Probable cause:
The failure of both engines for undetermined reasons.
Final Report:

Crash of a Cessna 414A Chancellor in Lawrenceville: 3 killed

Date & Time: Dec 25, 2006 at 2030 LT
Type of aircraft:
Operator:
Registration:
N62950
Flight Type:
Survivors:
No
Schedule:
Pahokee - Lawrenceville
MSN:
414-0086
YOM:
1970
Crew on board:
1
Crew fatalities:
Pax on board:
2
Pax fatalities:
Other fatalities:
Total fatalities:
3
Captain / Total flying hours:
631
Captain / Total hours on type:
406.00
Aircraft flight hours:
4313
Circumstances:
According to Atlanta Air Route Traffic Control Center (ARTCC) personnel, the pilot was given the current weather information before attempting his first instrument approach into Gwinnett County Airport-Briscoe Field (LZU), Lawrenceville, Georgia, which included: winds calm, visibility 1/2-mile in fog, and ceiling 100 feet. The pilot acknowledged the current weather information and elected to continue for the instrument landing system (ILS) runway-25 approach. During the first landing attempt, the pilot reported that he was going to execute a missed approach, but that he saw the airport below and wanted to attempt another approach. The ARTCC controller provided the pilot with radar vectors back to the ILS runway-25 approach and again updated the pilot with current weather conditions. During the second approach the tower controller advised the pilot that he was left of the runway-25 centerline. Shortly after the pilot acknowledged that he was left of the centerline, the tower controller saw a bright "orange glow" off of the left side of the approach end of runway 25. Although the weather conditions were below approach minimums for the runway 25-approach, the pilot elected to attempt the landing. A flight inspection of the ILS was completed on December 26, 2006, and the results of the inspection revealed that the ILS runway-25 approach system was satisfactory. Examination of the airframe, flight control system components, engines and system components revealed no evidence of preimpact mechanical malfunction.
Probable cause:
The pilot's failure to follow the instrument approach procedure. Contributing to the accident was the pilot's descent below the prescribed decision height altitude.
Final Report:

Crash of a Swearingen SA26AT Merlin IIB in Lawrenceville

Date & Time: Apr 26, 2005 at 1826 LT
Type of aircraft:
Registration:
N50KV
Survivors:
Yes
Schedule:
Spartanburg – Lawrenceville
MSN:
T26-115
YOM:
1968
Crew on board:
1
Crew fatalities:
Pax on board:
1
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
14000
Captain / Total hours on type:
3500.00
Aircraft flight hours:
9415
Circumstances:
While executing an instrument approach to land on runway 25, the airplane collided with the runway, and collapsed the right main landing gear. The airplane subsequently burst into flames after the pilot and passenger exited the airplane. Post-accident examination of the engines found both the left and right engine fuel controls in a low power setting. Examination of the propeller control found both propellers at 30-degrees. The pilot did not report any flight control or mechanical problems during flight.
Probable cause:
The pilot's improper landing flare that resulted in a hard landing.
Final Report:

Crash of a Socata TBM-700 in Mobile: 1 killed

Date & Time: Apr 24, 2003 at 2012 LT
Type of aircraft:
Operator:
Registration:
N705QD
Survivors:
No
Schedule:
Lawrenceville – Mobile
MSN:
231
YOM:
2002
Flight number:
LBQ850
Location:
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
1
Captain / Total flying hours:
10000
Captain / Total hours on type:
408.00
Aircraft flight hours:
1222
Circumstances:
A review of communications between Mobile Downtown Control Tower, and the pilot revealed that while on approach the pilot reported having a problem. The Ground Controller reported that he had the airplane in sight and cleared the flight to land on runway 18. The pilot stated that he had a "run away engine", and elected to shut down the engine and continued the approach. The Controller then cleared the pilot again to runway 18. The pilot then stated that he did not think that he was going to "make it." The airplane collided with a utility pole and the ground and burst into flames short of the runway. The post-accident examination of the engine found that the fuel control unit arm to the fuel control unit interconnect rod end connection was separated from the rod end swivel ball assembly. The swivel ball assembly was found improperly attached to the inboard side of the arm, with the bolt head facing inboard, instead of outboard, and the washer and nut attached to the arm's outboard side instead of the inboard side. The rod separation would resulted in a loss of power lever control. The published emergency procedures for "Power Lever Control Lose," states; If minimum power obtained is excessive: 1) reduce airspeed by setting airplane in nose-up attitude at IAS < 178 KIAS. 2) "inert Sep" switch--On. 3) if ITT >800 C "Inert Sep"--Off. 4) Landing Gear Control--Down. 5) Flaps--Takeoff. 6) Establish a long final or an ILS approach respecting IAS < 178 KIAS. 7) When runway is assured: Condition Lever to --Cut Off. 8) Propeller Governor Lever to-- Feather. 9) Flaps --Landing as required (at IAS <122 KIAS). 10) Land Normally without reverse. 11) Braking as required. The pilot stated to Mobile Downtown Control Tower, Ground Control that he had a "run away engine" and that he "had to shut down the engine". As a result of the pilot not following the published emergency procedures, the airplane was unable to reach the runway during the emergency.
Probable cause:
The improper installation of the power control linkage on the engine fuel control unit by maintenance personnel which resulted in a loss of power lever control, and the pilot's failure to follow emergency procedures and his intentional engine shutdown which resulted in a forced landing and subsequent inflight collision with a light pole.
Final Report:

Crash of a Rockwell Gulfstream 695A Jetprop 1000 in Boca Raton: 3 killed

Date & Time: Jan 21, 1998 at 1534 LT
Registration:
N269M
Flight Phase:
Flight Type:
Survivors:
No
Schedule:
Boca Raton - Lawrenceville
MSN:
695-96098
YOM:
1985
Crew on board:
1
Crew fatalities:
Pax on board:
2
Pax fatalities:
Other fatalities:
Total fatalities:
3
Captain / Total flying hours:
1606
Captain / Total hours on type:
843.00
Aircraft flight hours:
3274
Circumstances:
The pilot had received a weather briefing and was aware of the weather conditions west and north of the airport. The pilot was issued the flight clearance as filed, and was assigned an initial altitude of 2000 feet. Approximately five minutes into the flight, the air traffic controller questioned the pilot concerning the assigned heading. The controller stated that the pilot 'sounded extremely strained' and replied, 'N269M is in trouble.' Radar altitude data showed a rapid loss of altitude for N269M; the last radar altitude data showed the flight at 2800 feet. The airplane collided with the ground in a nose low attitude. Weather radar data from the Miami Weather Surveillance Radar-1988, Doppler (WSR-88D) showed a large, intense convective cell just west of Boca Raton between 1530:15 and 1535:57. Moderate to very heavy rain showers were associated with the convective activity. A review of the radar data showed that N269M was 3.5 to 4.0 miles north of the core of the large convective cell.
Probable cause:
The pilot flew into known convective meteorological conditions and lost control of the airplane. Factors were low clouds, and moderate to heavy rain.