Crash of a Piper PA-46-350P Malibu Mirage in Rantoul: 3 killed

Date & Time: Jul 24, 2011 at 0920 LT
Operator:
Registration:
N46TW
Flight Phase:
Flight Type:
Survivors:
No
Schedule:
Rantoul – Sarasota
MSN:
46-22071
YOM:
1989
Crew on board:
1
Crew fatalities:
Pax on board:
2
Pax fatalities:
Other fatalities:
Total fatalities:
3
Captain / Total flying hours:
1850
Aircraft flight hours:
2560
Circumstances:
On July 24, 2011, about 0920 central daylight time, a Piper PA-46-350P, N46TW, owned and operated by a private pilot, sustained substantial damage when it impacted powerlines and terrain during takeoff from runway 27 at the Rantoul National Aviation Center Airport-Frank Elliott Field (TIP), near Rantoul, Illinois. A post impact ground fire occurred. The personal flight was operating under 14 Code of Federal Regulations Part 91. Visual meteorological conditions prevailed at the time of the accident. An instrument flight rules (IFR) flight plan was on file. The pilot and two passengers sustained fatal injuries. The flight was originating from TIP at the time of the accident and was destined for Sarasota/Bradenton International Airport (SRQ), near Sarasota, Florida. A witness, who worked at the fixed base operator, stated that the pilot performed the preflight inspection of the airplane in a hangar. An estimated 80 pounds. of luggage was loaded behind the airplane's rear seat. The witness said that the pilot's wife told the pilot that she had to use the restroom. The pilot reportedly replied to her to "hurry because a storm front was coming." The witness said that the engine start was normal and that both passengers were sitting in the rear forward-facing seats when the airplane taxied out. A witness at the airport, who was a commercial pilot, reported that he observed the airplane takeoff from runway 27 and then it started to turn to the south. He indicated that the landing gear was up when the airplane was about 500 feet above the ground. The witness stated that a weather front was arriving at the airport and that the strong winds from the northwest appeared to "push the tail of the plane up and the nose down." The airplane descended and impacted powerlines and terrain where the airplane subsequently caught on fire. The witness indicated that the airplane's engine was producing power until impact.
Probable cause:
The pilot did not maintain airplane control during takeoff with approaching thunderstorms. Contributing to the accident was the pilot's decision to depart into adverse weather conditions.
Final Report:

Crash of a Cessna 421C Golden Eagle III in Demopolis: 7 killed

Date & Time: Jul 9, 2011 at 1740 LT
Registration:
N692TT
Flight Type:
Survivors:
No
Schedule:
Creve Cœur – Destin
MSN:
421C-0616
YOM:
1979
Crew on board:
1
Crew fatalities:
Pax on board:
6
Pax fatalities:
Other fatalities:
Total fatalities:
7
Captain / Total flying hours:
1000
Captain / Total hours on type:
340.00
Aircraft flight hours:
7800
Circumstances:
The multi-engine airplane was in cruise flight at flight level 210 when the pilot declared an emergency due to a rough-running right engine and diverted to a non-towered airport about 10 miles from the airplane’s position. About 4 minutes later, the pilot reported that he had shut down the right engine. The pilot orbited around the diversion airport during the descent and reported to an air traffic controller that he did not believe he would require any assistance after landing. The airplane initially approached the airport while descending through about 17,000 feet mean sea level (msl) and circled above the airport before entering a left traffic pattern approach for runway 22. About 7,000 feet msl, the airplane was about 2.5 miles northeast of the airport. The airplane descended through 2,300 feet msl when it was abeam the runway threshold on the downwind leg of the traffic pattern. According to the airplane information manual, procedures for landing with an inoperative engine call for “excessive altitude;” however, the airplane's last radar return showed the airplane at an altitude of 700 feet msl (about 600 feet above ground level) and about 3 miles from the approach end of the runway. The airplane was configured for a single-engine landing and was likely on or turning to the final approach course when it rolled and impacted trees. The airplane came to rest in a wooded area about 0.8 miles north of the runway threshold, inverted, in a flat attitude with no longitudinal deformation. A majority of the airplane, including the cockpit, main cabin, and left wing, were consumed by a postcrash fire. Search operations located the airplane about 6 hours after its expected arrival time. Due to the severity of the postcrash fire, occupant survivability after the impact could not be determined. Examination of the airframe, the left engine, and both propellers did not reveal any preaccident mechanical malfunctions or failures that would have precluded normal operation. The investigation revealed that the right engine failed when the camshaft stopped rotating after the camshaft gear experienced a fatigue fracture on one of its gear teeth. The remaining gear teeth were fractured in overstress and/or were crushed due to interference contact with the crankshaft gear. Spalling observed on an intact gear tooth suggested abnormal loading of the camshaft gear; however, the origin of the abnormal loading could not be determined.
Probable cause:
The pilot's failure to maintain airplane control during a single-engine approach and his failure to fly an appropriate traffic pattern for a single-engine landing. Contributing to the accident was a total loss of engine power on the right engine due to a fatigue failure of the right engine cam gear.
Final Report:

Crash of an Eclipse EA500 in Nome

Date & Time: Jun 1, 2011 at 2140 LT
Type of aircraft:
Registration:
N168TT
Flight Type:
Survivors:
Yes
Schedule:
Anadyr – Nome
MSN:
42
YOM:
2007
Location:
Crew on board:
1
Crew fatalities:
Pax on board:
1
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
2370
Captain / Total hours on type:
205.00
Aircraft flight hours:
343
Circumstances:
The pilot indicated that, prior to the accident flight, the wing flaps had failed, but he decided to proceed with the flight contrary to the Airplane Flight Manual guidance. While conducting a no-flap approach to the airport, he decided that his airspeed was too fast to land, and he initiated a go-around. During the go-around, the airplane continued to descend, and the fuselage struck the runway. The pilot was able to complete the go-around, and realized that he had not extended the landing gear. He lowered the landing gear, and landed the airplane uneventfully. He elected to remain overnight at the airport due to fatigue. The next day, he decided to test fly the airplane. During the takeoff roll, the airplane had a severe vibration, and he aborted the takeoff. During a subsequent inspection, an aviation mechanic discovered that the center wing carry-through cracked when the belly skid pad deflected up into a stringer during the gear-up landing.
Probable cause:
The pilot landed without lowering the landing gear. Contributing to the accident was the pilot's decision to fly the airplane with an inoperative wing flap system.
Final Report:

Crash of a North American B-25J-35-NC Mitchell in Melun

Date & Time: May 31, 2011 at 1730 LT
Registration:
F-AZZU
Flight Phase:
Flight Type:
Survivors:
Yes
Schedule:
Melun - Melun
MSN:
108-47562
YOM:
1944
Country:
Region:
Crew on board:
1
Crew fatalities:
Pax on board:
1
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
Crew was performing a local flight at Melun-Villaroche Airport. Few minutes after takeoff, while flying at low height, the engine caught fire. The pilot elected to return to the airport but was eventually forced to attempt an emergency landing. The aircraft collided with power cables then crashed on its belly in a field, coming to rest in flames. Both occupants escaped uninjured while the aircraft was damaged beyond repair.
Probable cause:
The right engine caught fire in flight for unknown reasons.

Crash of a Socata TBM-850 in Salem

Date & Time: May 19, 2011 at 0843 LT
Type of aircraft:
Operator:
Registration:
N1UL
Flight Type:
Survivors:
Yes
Schedule:
Valparaiso - Salem
MSN:
564
YOM:
2010
Crew on board:
1
Crew fatalities:
Pax on board:
3
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
932
Captain / Total hours on type:
76.00
Aircraft flight hours:
187
Circumstances:
The pilot reported that he flew an instrument approach and was clear of clouds about 650 feet above ground level when he proceeded visually to the airport. About 1/2 mile from the runway, he thought the airplane was too high, but a few seconds later the airplane felt like it had an excessive rate of descent. His attempts to arrest the rate of descent were unsuccessful, and the left main landing gear struck the ground about 120 feet prior to the runway threshold. The recorded data downloaded from the airplane's non-volatile memory showed that the airplane's airspeed varied from about 71 - 81 knots indicated airspeed (IAS) during the 10 seconds prior to ground impact. The data also indicated that there was about a 3 - 5 knot tailwind during the final landing approach. The airplane's stall speed with the airplane in the landing configuration with landing flaps was 64 knots IAS at maximum gross weight. The pilot reported that there was no mechanical malfunction or system failure of the airplane.
Probable cause:
The pilot's failure to maintain a stabilized glide path which resulted in the airplane touching down short of the runway.
Final Report:

Crash of a Beechcraft E90 King Air in Bournemouth

Date & Time: May 18, 2011 at 1131 LT
Type of aircraft:
Registration:
N46BM
Flight Phase:
Flight Type:
Survivors:
Yes
Schedule:
Bournemouth - Manchester
MSN:
LW-198
YOM:
1976
Region:
Crew on board:
1
Crew fatalities:
Pax on board:
1
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
800
Captain / Total hours on type:
660.00
Circumstances:
The pilot had planned to fly from Bournemouth Airport to Manchester Airport operating the flight as a single pilot, with a passenger seated in the co-pilot’s seat. He arrived at the airport approximately one hour before the planned departure time of 1130 hrs, completed his pre‑flight activities and went to the aircraft at approximately 1110 hrs. The 1120 hrs ATIS gave the weather at the airport as: surface wind from 230° at 10 kt, visibility 10 km or greater, few clouds at 1,000 ft, broken cloud at 1,200 ft and at 2,000 ft, temperature 16°C, dew point 12°C and QNH 1015 hPa. After starting the engines, the pilot was cleared to taxi to holding point ‘N’ for a departure from Runway 26 and he was given clearance to take off at 1127 hrs. At 1129:45 hrs, approximately 55 seconds after the aircraft became airborne, the aerodrome controller transmitted “four six bravo mike do you have a problem?” because he believed the aircraft was not climbing normally. The pilot replied “november four six bravo going around” and, shortly afterwards, “four six bravo requesting immediate return”. The controller cleared the pilot to use either runway to land back at the airport but received no reply. The pilot carried out a forced landing into a field 1.7 nm west of the Runway 08 threshold at Bournemouth Airport and neither he nor his passenger was hurt.
Probable cause:
The pilot experienced symptoms of symmetrical power loss sufficient to prevent the aircraft from sustaining level flight and made a forced landing into a field. The deficiency in the aircraft’s takeoff performance suggested that its powerplants were not producing sufficient thrust. As fuel contamination was discounted and no fault was found in either engine, it was concluded that, in all probability, the poor performance was not caused by a failure in either powerplant. Maximum rpm was not selected for departure but it was unlikely that this explained the aircraft’s poor performance on the runway or in the air. The pilot insisted that he had set torque to the takeoff limit. There was insufficient evidence to enable the cause of the apparent power loss to be determined.
Final Report:

Crash of a PZL-Mielec AN-2TP in Loxley

Date & Time: Apr 11, 2011 at 1216 LT
Type of aircraft:
Operator:
Registration:
N122AN
Flight Phase:
Flight Type:
Survivors:
Yes
Schedule:
Destin – DeRidder
MSN:
1G176-31
YOM:
1977
Location:
Crew on board:
1
Crew fatalities:
Pax on board:
2
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
4888
Captain / Total hours on type:
21.00
Aircraft flight hours:
10371
Circumstances:
According to the pilot, during cruise flight the engine began to run rough and lose power. He heard a loud metallic sound; the engine vibrated violently and then lost power. He performed a forced landing to a farm field, and the airplane nosed over in the soft terrain, resulting in substantial damage to the wings. A postaccident inspection revealed that the crankshaft would not rotate. An internal inspection of the cylinders and spark plugs did not reveal a reason for the power loss. The oil system was examined and there were large amounts of metal particles in the oil. Due to a lack of suitable equipment and facilities, further disassembly of the engine was not attempted.
Probable cause:
A loss of engine power due to internal failure.
Final Report:

Crash of a Cessna 402B in Biddeford: 1 killed

Date & Time: Apr 10, 2011 at 1805 LT
Type of aircraft:
Operator:
Registration:
N402RC
Flight Type:
Survivors:
No
Site:
Schedule:
White Plains - Portland
MSN:
402B-1218
YOM:
1977
Location:
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
1
Captain / Total flying hours:
4735
Captain / Total hours on type:
120.00
Aircraft flight hours:
6624
Circumstances:
The multi-engine airplane was being repositioned to its base airport, and the pilot had requested to change the destination, but gave no reason for the destination change. Radar data indicated that the airplane entered the left downwind leg of the traffic pattern, flew at pattern attitude, and then performed a right approximate 250-degree turn to enter the final leg of the approach. During the final leg of the approach, the airplane crashed short of the runway into a house located in a residential neighborhood near the airport. According to the airplane's pilot operating handbook, the minimum multi-engine approach speed was 95 knots indicated airspeed (KIAS), and the minimum controllable airspeed was 82 KIAS. According to radar data, the airplane's ground speed was about 69 knots with the probability of a direct crosswind. Post accident examination of the propellers indicated that both propellers were turning at a low power setting at impact. During a controlled test run of the right engine, a partial power loss was noted. After examination of the throttle and control assembly, two o-rings within the assembly were found to be damaged. The o-rings were replaced with comparable o-rings and the assembly was reinstalled. During the subsequent test run, the engine operated smoothly with no noted anomalies. Examination of the o-rings revealed that the damage was consistent with the o-rings being pinched between the corner of the top o-ring groove and the fuel inlet surface during installation. It is probable that the right engine had a partial loss of engine power while on final approach to the runway due to the damaged o-ring and that the pilot retarded the engine power to prevent the airplane from rolling to the right. The investigation found no mechanical malfunction of the left engine that would have prevented the airplane from maintaining the published airspeed.
Probable cause:
The pilot did not maintain minimum controllable airspeed while on final approach with a partial loss of power in the right engine, which resulted in a loss of control. Contributing to the accident was the partial loss of engine power in the right engine due to the improperly installed o-rings in the engine’s throttle and control assembly.
Final Report:

Crash of a Rockwell Sabreliner 60 in Fort Lauderdale

Date & Time: Apr 9, 2011 at 1357 LT
Type of aircraft:
Operator:
Registration:
N71CC
Flight Type:
Survivors:
Yes
Schedule:
Fort Lauderdale – West Palm Beach
MSN:
306-71
YOM:
1974
Crew on board:
2
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
On approach to West Palm Beach Airport, the crew encountered technical problems with the undercarriage that could not be lowered. The crew decided to return to his base in Fort Lauderdale. On final, the crew was again unable to lower the gear so the decision was taken to complete a wheels-up landing. The airplane landed on its belly on runway 08 then slid for few dozen metres before coming to rest. The occupants escaped uninjured and the aircraft was damaged beyond repair.
Probable cause:
No investigation was carried out by the NTSB.

Crash of a Piper PA-46-350P Malibu Mirage in Monroe: 3 killed

Date & Time: Mar 29, 2011 at 1604 LT
Registration:
N619VH
Flight Type:
Survivors:
No
Schedule:
Bedford – Monroe
MSN:
46-36402
YOM:
2006
Crew on board:
1
Crew fatalities:
Pax on board:
2
Pax fatalities:
Other fatalities:
Total fatalities:
3
Captain / Total flying hours:
1600
Aircraft flight hours:
851
Circumstances:
A witness reported and radar data showed the airplane approaching the runway at a higher‐than‐normal speed. As the airplane leveled low over the runway, the propeller began striking the runway surface. The damage from repetitive propeller strikes resulted in a loss of the thrust and airspeed necessary for flight. The airplane impacted the ground and subsequently caught fire. The postaccident examination of the wreckage confirmed that the airplane was configured with the landing gear and flaps retracted. No mechanical anomalies were observed that would have precluded normal operation of the airplane. Weight and balance estimates of the airplane indicated that the pilot was operating the airplane outside of its certified weight and center of gravity limits. Forensic toxicology performed on the pilot showed the presence of Hydrocodone and Dihydrocodeine, indicative of the pilot using disqualifying sedating cough or pain medications. These medications can impair performance in high workload environments. The level of medication found in the pilot’s blood at the time of the accident could not be determined. Additionally, Nortriptyline was detected in the pilot’s tissues. While the medications could have had degrading effects on the pilot’s performance, the investigation was not able to determine what role they may have played in the accident sequence.
Probable cause:
The pilot's demonstration of poor judgment by attempting a high‐speed pass several feet above the runway and his subsequent failure to maintain clearance from the runway.
Final Report: