Country
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Val-d'Oise

Crash of a Saab 2000 in Paris-Roissy-CDG

Date & Time: Jan 28, 2014 at 0731 LT
Type of aircraft:
Operator:
Registration:
HB-IZG
Survivors:
Yes
Schedule:
Leipzig – Paris
MSN:
010
YOM:
1994
Flight number:
DWT250
Country:
Region:
Crew on board:
3
Crew fatalities:
Pax on board:
16
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
6640
Captain / Total hours on type:
2260.00
Copilot / Total flying hours:
630
Copilot / Total hours on type:
80
Circumstances:
Following an uneventful flight from Leipzig, the crew started the descent to Paris-Roissy-CDG Airport runway 27R. At an altitude of 400 feet on approach, the automatic pilot system was deactivated. At an altitude of 200 feet, the decision height, the crew decided to continue the approach as the runway was in sight and the aircraft was stable. During the last segment, at a height of 50 feet, power levers were reduced to flight idle and the aircraft went into a nose up attitude (maximum value of 11°). Both main gears touched down at a speed of 120 knots but the aircraft bounced twice and went into a pitch down attitude, causing the nose gear to land first during the third touchdown. On impact, the nose gear collapsed and the aircraft slid for dozen yards before coming to rest. All 19 occupants were evacuated safely and the aircraft was later considered as damaged beyond repair.
Probable cause:
During the flare the captain detected that the landing would be hard and in an emergency action, he quickly pulled the nose up without announcing his intention to the first officer who was the pilot flying. This lack of coordination within the flight crew caused a double controls and successive and opposite actions on the flight controls during the bouncing management.
Final Report:

Mishap of a Fokker F27 Friendship 500F in Paris-Roissy-CDG

Date & Time: Oct 25, 2013 at 0125 LT
Type of aircraft:
Operator:
Registration:
I-MLVT
Flight Phase:
Flight Type:
Survivors:
Yes
Schedule:
Paris - Dole
MSN:
10373
YOM:
1968
Flight number:
MNL5921
Country:
Region:
Crew on board:
2
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
The crew was performing a night mail flight from Paris-Roissy-CDG Airport to Dole-Jura (Tavaux) Airport on behalf of Europe Airpost. Shortly after takeoff, while climbing to an altitude of 1,000 feet, the left propeller detached and impacted the left part of the fuselage, causing a large hole. The crew declared an emergency and was cleared for an immediate return. The aircraft landed safely less than 10 minutes later and was parked on the apron. Both pilots were uninjured and the aircraft was damaged beyond repair. The propeller was found in an open field in Mesnil-Amelot, near the airport. Nobody on ground was injured.
Probable cause:
The n°2 propeller blade root on the left engine failed due to fatigue, resulting in separation from the propeller hub and then interaction with the n°1 blade and its disconnection from the propeller hub. The imbalance created by the loss of these two blades led to the front part of the engine being torn off. The cause of the fatigue cracking could not be determined with certainty. The following may have contributed to the fatigue fracture of the propeller blade root:
- Insufficient preloading of the propeller, increasing the stress exerted on it. The lack of maintenance documentation made it impossible to determine the preload values of the bearings during the last general overhaul;
- The presence of manganese sulphide in a heavily charged area of the propeller. The presence of this sulphide may have generated a significant stress concentration factor, raising the local stress level.
The tests and research carried out as part of this investigation show that the propeller blade root is made of a steel whose microstructure and composition are not optimal for fatigue resistance. However, the uniqueness of the rupture more than 50 years after commissioning makes it unlikely that the rate of inclusions, their distribution, size, or sulphur content of the propeller is a contributing factor in the accident.
Final Report: