Country
Crash of a Swearingen SA227AC Metro III in Palma de Majorca: 2 killed
Date & Time:
Apr 12, 2002 at 0506 LT
Registration:
EC-GKR
Survivors:
No
Schedule:
Madrid - Palma de Mallorca
MSN:
AC-620
YOM:
1985
Flight number:
TDC306
Crew on board:
2
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
2
Captain / Total hours on type:
2162.00
Copilot / Total hours on type:
487
Aircraft flight hours:
29726
Circumstances:
The twin engine aircraft departed Madrid-Barajas Airport at 0338LT on a cargo flight to Palma de Mallorca, carrying two pilots and a load of 1,340 kilos consisting of various goods. On a night approach to Palm Airport runway 24L, the crew completed a last turn when the aircraft stalled and struck the runway surface. Out of control, it veered to the right, collided with a lightning system and came to rest upside down in a grassy area. The aircraft was destroyed and both pilots were killed.
Probable cause:
The accident is considered to have occurred as a result of the aircraft performing a very close turn maneuver performed at night, at low altitude and descending in a non-standard approach, not in accordance with normal procedures and company procedures. The crew could not control the descending aircraft due to a possible start of loss of lift, slip on the turn, or both.
Final Report:
Crash of a Swearingen SA227AC Metro III in Goose Bay
Date & Time:
Mar 4, 2002 at 0456 LT
Registration:
C-FITW
Survivors:
Yes
Schedule:
Saint John's - Goose Bay
MSN:
AC-638
YOM:
1986
Flight number:
PB905
Crew on board:
2
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
The aircraft was on a scheduled courier flight from St. John=s, Newfoundland and Labrador, to Goose Bay. The aircraft touched down at 0456 Atlantic standard time and, during the landing roll on the snow-covered runway, the aircraft started to veer to the right. The captain's attempt to regain directional control by the use of full-left rudder and reverse on the engines was unsuccessful. The aircraft continued to track to the right of the centreline, departed the runway, and struck a hard-packed snow bank. There were no injuries to the two crew members. The aircraft was substantially damaged.
Probable cause:
Findings as to Cause and Contributing Factors:
1. Aircraft directional control was lost, likely because of negative castering of the nosewheel when snow piled up in front of the nosewheel assembly.
Findings as to Risk:
1. The crew members were not aware of negative castering; the aircraft flight manual and emergency checklists do not address negative castering.
2. The emergency response to the occurrence was delayed by four minutes because of the lack of communication from the aircraft to the tower.
1. Aircraft directional control was lost, likely because of negative castering of the nosewheel when snow piled up in front of the nosewheel assembly.
Findings as to Risk:
1. The crew members were not aware of negative castering; the aircraft flight manual and emergency checklists do not address negative castering.
2. The emergency response to the occurrence was delayed by four minutes because of the lack of communication from the aircraft to the tower.
Final Report: