Crash of a Piper PA-31-350 Navajo Chieftain in Brownsville

Date & Time: Jan 9, 1995 at 1622 LT
Registration:
N50WT
Flight Type:
Survivors:
Yes
Schedule:
Cancún – El Paso
MSN:
31-7952018
YOM:
1979
Crew on board:
1
Crew fatalities:
Pax on board:
2
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
87
Circumstances:
During an international cross country flight the private pilot, certificated single engine land, experienced a dual engine power loss as he was being vectored to the Brownsville Airport. Following the accident the aircraft was examined by a Federal Aviation Administration inspector who found that there was fuel in the left fuel tank and that the fuel selector was in the right tank position. The pilot had reported, prior to loss of engine power, that he had low fuel indications in the right tank and that he needed a vector to Brownsville. The aircraft was landed in rough and uneven terrain, resulting in damage to the structure and wings, approximately 1/2 mile short of the runway.
Probable cause:
The fuel starvation loss of engine power due to the pilot's improper use of the fuel tank selector. Factors were the pilot's qualification and the lack of suitable terrain for landing.
Final Report:

Ground accident of a Boeing 737-2C0 in Houston

Date & Time: Nov 26, 1994 at 1102 LT
Type of aircraft:
Operator:
Registration:
N11244
Flight Phase:
Survivors:
Yes
MSN:
20073
YOM:
1969
Crew on board:
2
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
Two technicians took over the airplane from the main Continental maintenance hangar to the gate 41. While approaching the gate, the right wing of the B737 collided with the left wing of a Continental Airlines Boeing 737-300 that was towed from the next gate. While the second B737 was slightly damaged, the right wing of the B737 registered was partially sheared off. There were no casualties but the aircraft was damaged beyond repair.
Probable cause:
Failure of maintenance personnel to follow the taxi checklist resulting in the hydraulic pumps not being turned on.

Crash of a Cessna 421C Golden Eagle III in San Antonio: 2 killed

Date & Time: Feb 10, 1994 at 0713 LT
Operator:
Registration:
N741CA
Flight Type:
Survivors:
Yes
Schedule:
San Antonio - Eagle Pass
MSN:
421C-0899
YOM:
1980
Crew on board:
1
Crew fatalities:
Pax on board:
2
Pax fatalities:
Other fatalities:
Total fatalities:
2
Captain / Total flying hours:
5100
Captain / Total hours on type:
400.00
Aircraft flight hours:
2916
Circumstances:
Shortly after takeoff, the pilot reported he had 'a problem' and needed to return immediately. Witnesses observed dark black smoke coming from both engines. The airplane collided with a tree 1/2-mile northeast of the runway threshold. Analysis of fuel samples revealed the presence of approximately 50% jet fuel. The right propeller was found feathered and engine disassembly revealed a hole burned in the right engine number 5 piston. Left engine disassembly revealed piston edges eroded down to the first compression ring. Fuel filler restrictors had been installed in the airplane's fuel tanks, but the fuel truck did not have the restrictive mating nozzle. The fuel truck was owned by the fuel vender and leased to the FBO.
Probable cause:
Improper servicing of the airplane with jet fuel, which resulted in preignition and/or detonation and subsequent failure of pistons in both engines. A factor related to the accident was: the lack of a restrictive mating nozzle on the refueling truck.
Final Report:

Crash of a Piper PA-31P Pressurized Navajo in San Antonio: 1 killed

Date & Time: Sep 27, 1993 at 1723 LT
Type of aircraft:
Registration:
N891SP
Flight Phase:
Flight Type:
Survivors:
No
Schedule:
San Antonio - San Antonio
MSN:
31-7300145
YOM:
1973
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
1
Captain / Total flying hours:
1668
Captain / Total hours on type:
12.00
Aircraft flight hours:
6374
Circumstances:
During takeoff roll, the left engine began to emit black smoke. The tower informed the pilot, who did not respond, and continued his takeoff. After becoming airborne, the aircraft was observed to level off then enter a left turn and impact the ground approximately 2 miles west of the airport. Examination of the engine provided no evidence of malfunction. Review of available pilot records indicated the pilot had 12 hours in type.
Probable cause:
Failure by the pilot-in-command to maintain VMC following takeoff. Factors were: partial loss of power to one engine for undetermined reason, and lack of total experience in aircraft type.
Final Report:

Crash of a Douglas DC-10-30 in Dallas

Date & Time: Apr 14, 1993 at 0659 LT
Type of aircraft:
Operator:
Registration:
N139AA
Survivors:
Yes
Schedule:
Honolulu - Dallas
MSN:
46711
YOM:
1973
Flight number:
AA102
Crew on board:
13
Crew fatalities:
Pax on board:
189
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
12562
Captain / Total hours on type:
555.00
Copilot / Total flying hours:
4454
Copilot / Total hours on type:
376
Aircraft flight hours:
74831
Aircraft flight cycles:
17920
Circumstances:
At the time flight AA102 landed at DFW Airport, it was raining and there were numerous thunderstorms in the area. Shortly after touchdown on runway 17L, the pilot loss directional control when the airplane began to weathervane and the captain failed to use sufficient rudder control to regain the proper ground track. The airplane eventually departed the right side of the runway. At the time of landing the wind (a cross wind) was blowing at 15 knots with gusts approximately 5 knots above the steady wind speed. The aircraft was damaged beyond repair and all 202 occupants were evacuated, among them 40 were injured, two seriously.
Probable cause:
Failure of the captain to use proper directional control techniques to maintain the airplane on the runway.
Final Report:

Crash of a Cessna 340A in Kerrville: 2 killed

Date & Time: Feb 27, 1993 at 1840 LT
Type of aircraft:
Registration:
N88KH
Flight Type:
Survivors:
No
Schedule:
Houston - Kerrville
MSN:
340A-1801
YOM:
1984
Location:
Crew on board:
1
Crew fatalities:
Pax on board:
1
Pax fatalities:
Other fatalities:
Total fatalities:
2
Captain / Total flying hours:
1783
Captain / Total hours on type:
498.00
Aircraft flight hours:
1100
Circumstances:
The pilot was cleared for an instrument approach to the airport. Once clear of clouds, the pilot was observed circling at low altitude on a closed left downwind for runway 30. Witnesses observed that on the turn from base to final, a very steep angle of bank was established as the engine power was heard being increased. Control was lost and the airplane impacted the ground inverted in a nose low attitude. A post impact fire consumed the airplane. The weather at the airport was reported as 900 overcast with 2 miles visibility in fog and haze with a light mist. Official sunset was one minute prior to the impact. Both occupants were killed.
Probable cause:
Inadvertent stall. Factors were the weather and the light conditions.
Final Report:

Crash of a Beechcraft A90 King Air in Marfa

Date & Time: Jan 29, 1993 at 1940 LT
Type of aircraft:
Operator:
Registration:
N363N
Survivors:
Yes
Schedule:
Houston - Marfa
MSN:
LJ-263
YOM:
1967
Location:
Crew on board:
2
Crew fatalities:
Pax on board:
6
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
2016
Captain / Total hours on type:
675.00
Aircraft flight hours:
6226
Circumstances:
During a dark night cross country in instrument meteorological conditions, the airplane was cleared for a VOR approach to runway 30. Due to unfavorable winds, the pilot elected to circle to land on runway 12. While on a right downwind, visual contact with the runway was lost and not reestablished. The pilot continued the descent on the base leg and impacted the terrain in a slight right turn.
Probable cause:
The pilot's continued descent below the proper altitude. Factors were the dark night, fog, and the crew's poor coordination.
Final Report:

Crash of a Swearingen SA227AC Metro III in San Antonio

Date & Time: Sep 18, 1992 at 1310 LT
Type of aircraft:
Operator:
Registration:
N2183A
Flight Type:
Survivors:
Yes
Schedule:
San Antonio - San Antonio
MSN:
AC-422
YOM:
1981
Crew on board:
2
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
6000
Captain / Total hours on type:
650.00
Aircraft flight hours:
17936
Circumstances:
The pilot was conducting a functional test flight and qualitative engineering evaluation of the airplane's longitudinal control during landing. During final approach to runway 12L, he reduced the engines to the flight idle positions and established 95 kias. He was unable to raise the nose of the airplane during the flare to arrest the descent rate and landed hard onto the runway. The airplane was taxied to the ramp and secured. No mechanical failure was found or reported.
Probable cause:
The landing capability of the airplane was exceeded. The lack of performance data was a factor in the accident.
Final Report:

Crash of a Cessna 402B in Roanoke

Date & Time: Nov 29, 1991 at 1720 LT
Type of aircraft:
Operator:
Registration:
N69CR
Flight Phase:
Flight Type:
Survivors:
Yes
Schedule:
Addison - Addison
MSN:
402B-0521
YOM:
1973
Location:
Crew on board:
1
Crew fatalities:
Pax on board:
1
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
4500
Circumstances:
During daylight flight, the airplane lost its right engine due to failed piston assembly because of engine overheating. The overheating was due to the engine air cooling baffle not being installed and the improper oil filter being installed. The airplane would not sustain flight due to the inoperative main landing gear which was locked in the down position and the propeller that could not feather due to corrosion. The pilot and his passenger were seriously injured in the landing due to the lack of seat belts. The airplane was operated with 137 known deficiencies.
Probable cause:
The operation of the airplane with known deficiencies, a missing air cooling baffle, and inadequate maintenance. Factors were the frozen propeller, inability of the pilot to feather the propeller, inoperative landing gear, the inability of the pilot to retract the landing gear, and the lack of seat belts.
Final Report:

Crash of an Embraer EMB-120RT Brasília in Eagle Lake: 14 killed

Date & Time: Sep 11, 1991 at 1003 LT
Type of aircraft:
Operator:
Registration:
N33701
Flight Phase:
Survivors:
No
Schedule:
Laredo - Houston
MSN:
120-077
YOM:
1987
Flight number:
CO2574
Crew on board:
3
Crew fatalities:
Pax on board:
11
Pax fatalities:
Other fatalities:
Total fatalities:
14
Captain / Total flying hours:
4243
Captain / Total hours on type:
2468.00
Copilot / Total flying hours:
11543
Copilot / Total hours on type:
1066
Aircraft flight hours:
7229
Aircraft flight cycles:
10009
Circumstances:
The airplane broke up in flight while descending from FL240. The horizontal stabilizer, or top of the T-type tail, had separated from the fuselage before ground impact. Examination revealed that the 47 screw fasteners that would have attached the upper surface of the leading edge assembly for the left side of the horizontal stabilizer were missing. They had been removed the night before during scheduled maintenance. Investigation revealed that there was a lack of compliance with the FAA-approved general maintenance manual procedures by the mechanics, inspectors, and supervisors responsible for assuring the airworthiness of the airplane the night before the accident. In addition, routine surveillance of the continental express maintenance department by the FAA was inadequate and did not detect deficiencies, such as those that led to this accident. All 14 occupants were killed.
Probable cause:
The failure of continental express maintenance and inspection personnel to adhere to proper maintenance and quality assurance procedures for the airplane's horizontal stabilizer deice boots that led to the sudden in-flight loss of the partially secured left horizontal stabilizer leading edge and the immediate severe nose down pitchover and breakup of the airplane. Contributing to the cause of the accident was the failure of continental express management to ensure compliance with the approved maintenance procedures, and the failure of the faa surveillance to detect and verify compliance with approved procedures.
Final Report: