Crash of a Cessna 401 in Linville: 1 killed

Date & Time: Apr 7, 1980 at 0837 LT
Type of aircraft:
Operator:
Registration:
N9912F
Flight Phase:
Survivors:
No
Site:
Schedule:
Myrtle Beach - Cincinnati
MSN:
401-0091
YOM:
1969
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
1
Captain / Total flying hours:
8919
Captain / Total hours on type:
480.00
Circumstances:
While cruising at an altitude of 5,900 feet in limited visibility due to marginal weather conditions, the twin engine airplane struck the slope of a mountain located near Linville. The aircraft was destroyed and the pilot, sole on board, was killed. At the time of the accident, the visibility was reduced to zero due to low ceiling, rains falls and fog.
Probable cause:
Controlled flight into terrain during normal cruise after the pilot continued VFR flight into adverse weather conditions. The following contributing factors were reported:
- Physical impairment of the pilot,
- Alcoholic impairment of efficiency and judgment,
- Low ceiling,
- Rain,
- Fog,
- Blood ethanol level 90 mg %,
- Hit the mountain at 5,909 feet,
- Mountain obscured.
Final Report:

Crash of a Piper PA-31-310 Navajo in Charlotte

Date & Time: Aug 31, 1978 at 1643 LT
Type of aircraft:
Operator:
Registration:
N9173Y
Flight Phase:
Flight Type:
Survivors:
Yes
Schedule:
Charlotte - Charlotte
MSN:
31-230
YOM:
1968
Crew on board:
2
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
3950
Captain / Total hours on type:
800.00
Circumstances:
The crew was engaged in a local training mission at Charlotte-Douglas Airport. Just after liftoff, while in initial climb, the instructor pilot cut the right engine mixture. The airplane encountered difficulties to gain height then stalled and crashed near the airport. Both occupants were injured and the aircraft was destroyed.
Probable cause:
Stall during initial climb after the crew exercised poor judgment. The following contributing factors were reported:
- Inadequate supervision of flight,
- Failed to follow approved procedures,
- Misused or failed to use flaps,
- Failed to maintain flying speed,
- Diverted attention from operation of aircraft,
- Aircraft flaps remained down,
- Pilots preoccupied with engine restart.
Final Report:

Crash of a De Havilland DHC-6 Twin Otter 300 in Candor: 5 killed

Date & Time: Jul 13, 1978 at 2145 LT
Operator:
Registration:
N76214
Flight Phase:
Flight Type:
Survivors:
No
Schedule:
Fort Bragg - Fort Bragg
MSN:
236
YOM:
1969
Crew on board:
2
Crew fatalities:
Pax on board:
3
Pax fatalities:
Other fatalities:
Total fatalities:
5
Circumstances:
The twin engine airplane departed Fort Bragg AFB on a training flight for the US Army, carrying three passengers and two pilots. While flying by night, the pilot failed to realize his altitude was too low when the airplane struck a tree and crashed in Candor, about 43 miles northwest of Fort Bragg.

Crash of a Beechcraft G18S in Rockingham

Date & Time: Mar 2, 1978 at 2020 LT
Type of aircraft:
Registration:
N180P
Flight Phase:
Flight Type:
Survivors:
Yes
Schedule:
Rockingham - Pontiac
MSN:
BA-478
YOM:
1959
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
6500
Captain / Total hours on type:
2825.00
Circumstances:
Shortly after a night takeoff from Rockingham-Hamlet Airport, the twin engine airplane struck wires and crashed in flames in a snow covered field. The pilot, sole on board, was seriously injured.
Probable cause:
Collision with wires during initial climb due to inadequate preflight preparation on part of the pilot-in-command. The following contributing factors were reported:
- Failed to abort takeoff,
- Selected unsuitable terrain,
- Disregard of good operating practice,
- Airport conditions: snow on runway,
- Launched from snow covered runway with half inch of snow on wings.
Final Report:

Crash of a Rockwell Grand Commander 680 in Morrisville: 4 killed

Date & Time: Feb 13, 1978 at 2002 LT
Operator:
Registration:
N26511
Flight Type:
Survivors:
Yes
Schedule:
Bedford - Raleigh
MSN:
680-1408-60
YOM:
1964
Crew on board:
1
Crew fatalities:
Pax on board:
5
Pax fatalities:
Other fatalities:
Total fatalities:
4
Captain / Total flying hours:
1061
Circumstances:
On final approach to Raleigh-Durham Airport, the twin engine airplane stalled and crashed. The pilot and three passengers were killed while two others were seriously injured.
Probable cause:
Stall and spin on final approach after the pilot failed to maintain flying speed. The following contributing factors were reported:
- Lack of familiarity with aircraft,
- Low ceiling,
- Fog,
- Improperly loaded aircraft, W&B and CofG.
- Visibility one mile or less,
- Aircraft heavy,
- No record of any pilot training type aircraft found,
- Narcotics and over 24,000 $ found in aircraft.
Final Report:

Crash of a Cessna 402B in Greensboro: 1 killed

Date & Time: Feb 6, 1978 at 1520 LT
Type of aircraft:
Operator:
Registration:
N69284
Flight Type:
Survivors:
No
Schedule:
Gulfport – Winston-Salem – Raleigh
MSN:
402B-0407
YOM:
1973
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
1
Captain / Total flying hours:
7408
Captain / Total hours on type:
540.00
Circumstances:
While approaching Winston-Salem Airport, the pilot informed ATC about engine problems. Shortly later, the twin engine airplane went out of control, entered a dive and crashed in flames in a field located in Greensboro. The aircraft was destroyed and the pilot, sole on board, was killed.
Probable cause:
Stalled and spiraled while descending to Winston-Salem Airport due to foreign material affecting normal operations. The following contributing factors were reported:
- Ice in fuel,
- Fuel starvation,
- Failed to maintain flying speed,
- Failure of both engines.
Final Report:

Crash of a Grumman E-2C Hawkeye in Supply: 5 killed

Date & Time: Jan 14, 1978
Type of aircraft:
Operator:
Registration:
159108
Flight Phase:
Flight Type:
Survivors:
No
MSN:
A015
Crew on board:
5
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
5
Circumstances:
The crew was completing a flight from USS John Fitzgerald Kennedy to the New River MCAS in Jacksonville, North Carolina. En route, the airplane went out of control and crashed in unknown circumstances in Supply, NC. All five crew members were killed.

Crash of a Learjet 25B in Sanford: 5 killed

Date & Time: Sep 8, 1977 at 2020 LT
Type of aircraft:
Operator:
Registration:
N999HG
Flight Phase:
Survivors:
No
Schedule:
Sanford - Flint
MSN:
25-178
YOM:
1974
Crew on board:
2
Crew fatalities:
Pax on board:
3
Pax fatalities:
Other fatalities:
Total fatalities:
5
Captain / Total flying hours:
9364
Aircraft flight hours:
700
Circumstances:
About 2020 EST, on September 8, 1977, Champion Home Builders Company, Gates Learjet 25B, N999HG, crashed shortly after takeoff at Sanford, North Carolina. All five persons aboard were killed, and the aircraft was destroyed. The aircraft departed Sanford Airport about 2018 EST, for a flight to Flint, Michigan. In accordance with departure instructions from Fayetteville departure control, the flight was about 3 mi west of the airport, climbing through 3,000 ft, on a heading of 270°, when it disappeared from radar. There were no distress calls, but several witnesses west of the airport saw the aircraft on fire below the 600 feet suddenly dove to the ground. People in the immediate vicinity reported that the overcast ceiling. The flight completed a right turn to a northeasterly heading and aircraft was on fire before it crashed.
Probable cause:
The National Transportation Safety Board determines that the probable cause of this accident was one or more low-order explosions in the aircraft's aft fuselage determine conclusively the fuel and ignition sources of the initial explosion; which resulted in a fire and loss of control capability. The Safety Board could not however, gases from the aircraft's batteries or fuel leakage from fuel system components, or both, could have been present in the area of the initial explosion.
Final Report:

Crash of a Grumman TC-4C Gulfstream I at Cherry Point MCAS: 9 killed

Date & Time: Oct 16, 1975
Type of aircraft:
Operator:
Registration:
155723
Flight Phase:
Flight Type:
Survivors:
No
Schedule:
Cherry Point - Cherry Point
MSN:
178
YOM:
1967
Crew on board:
2
Crew fatalities:
Pax on board:
7
Pax fatalities:
Other fatalities:
Total fatalities:
9
Circumstances:
Shortly after lift off, a low torque sensing switch failed precipitating an auto feather of an engine. The crew mis-handled the required feathering procedure, allowing the propeller to unfeather and windmill. Subsequently, the crew retracted the flaps. This disabled a spring tab on the rudder which was designed to give additional rudder authority for high power/low airspeed situations. The result of the windmilling propeller and the loss in rudder authority was that V(mca) increased from 101 kts to 138 kts. The airplane rolled inverted and crashed. Witness marks on the operating engine's propeller reportedly indicated that the airplane's speed when it crashed was less than 90 kts. All on board, four crew men, four students and one instructor, were killed.

Crash of a Beechcraft E18S in Charlotte: 1 killed

Date & Time: Oct 1, 1975 at 1152 LT
Type of aircraft:
Operator:
Registration:
N882L
Flight Phase:
Flight Type:
Survivors:
No
Schedule:
Charlotte – Columbia
MSN:
BA-102
YOM:
1955
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
1
Captain / Total flying hours:
3323
Captain / Total hours on type:
250.00
Circumstances:
After takeoff from Charlotte-Douglas Airport, while climbing, the pilot informed ground about an engine failure and was cleared to return for an emergency landing. The pilot encountered other technical problems and was unable to lower the gear when control was lost. The airplane lost altitude and crashed in flames by the airport. The aircraft was destroyed and the pilot, sole on board, was killed.
Probable cause:
Powerplant failure for undetermined reasons. The following contributing factors were reported:
- Failed to follow approved procedures,
- Failed to maintain flying speed,
- Failed to extend landing gear.
Final Report: