Crash of a Cessna 207 Skywagon near Hope

Date & Time: Jul 3, 2017 at 1032 LT
Operator:
Registration:
N9620M
Flight Phase:
Flight Type:
Survivors:
Yes
Schedule:
Seldovia – Anchorage
MSN:
207-0711
YOM:
1981
Location:
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
5365
Captain / Total hours on type:
3.00
Aircraft flight hours:
23833
Circumstances:
According to the pilot, he was flying the second airplane in a flight of two about 1 mile behind the lead airplane. The lead airplane pilot reported to him, via the airplane's radio, that he had encountered decreasing visibility and that he was making a 180° left turn to exit the area. The pilot recalled that, after losing sight of the lead airplane, he made a shallow climbing right turn and noticed that the terrain was rising. He recalled that he entered the clouds for a few seconds and "at that moment I ran into the trees which I never saw coming." The airplane sustained substantial damage to both wings. The pilot reported that there were no preaccident mechanical malfunctions or failures with the airplane that would have precluded normal operation. The pilot reported that the temperature was 60°F with 8 miles visibility and 1,500-eeft ceilings. The nearest METAR was about 1 mile away and reported that the temperature was 54°F, dew point was 52°F, visibility was 8 statute miles with light rain, and ceiling was broken at 500 feet and overcast at 1,500 feet.
Probable cause:
The pilot's inadvertent flight into instrument meteorological conditions and subsequent controlled flight into terrain.
Final Report:

Crash of a Cessna 421C Golden Eagle III in Catawba: 6 killed

Date & Time: Jul 1, 2017 at 0153 LT
Registration:
N2655B
Flight Phase:
Flight Type:
Survivors:
No
Schedule:
Waukegan – Winnipeg
MSN:
421C-0698
YOM:
1979
Crew on board:
1
Crew fatalities:
Pax on board:
5
Pax fatalities:
Other fatalities:
Total fatalities:
6
Captain / Total flying hours:
2335
Captain / Total hours on type:
70.00
Circumstances:
The commercial pilot of the multi-engine airplane was conducting an instrument flight rules cross-country flight at night. The pilot checked in with air traffic control at a cruise altitude about 10,000 ft mean sea level (msl). About 31 minutes later, the pilot reported that he saw lightning off the airplane's left wing. The controller advised the pilot that the weather appeared to be about 35 to 40 miles away and that the airplane should be well clear of it. The pilot responded to the controller that he had onboard weather radar and agreed that they would fly clear of the weather. There were no further communications from the pilot. About 4 minutes later, radar information showed the airplane at 10,400 ft msl. About 1 minute later, radar showed the airplane in a descending right turn at 9,400 ft. Radar contact was lost shortly thereafter. The distribution of the wreckage, which was scattered in an area with about a 1/4-mile radius, was consistent with an in-flight breakup. The left horizontal stabilizer and significant portions of both left and right elevators and their respective trim tabs were not found. Of the available components for examination, no pre-impact airframe structural anomalies were found. Examination of the engines and turbochargers did not reveal any pre-impact anomalies. Examination of the propellers showed evidence of rotation at impact and no pre-impact anomalies. Review of weather information indicated that no convection or thunderstorms were coincident with or near the airplane's route of flight, and the nearest convective activity was located about 25 miles west of the accident site. Autopsy and toxicology testing revealed no evidence of pilot impairment or incapacitation. Given the lack of radar information after the airplane passed through 9,400 ft, it is likely that it entered a rapid descent during which it exceeded its design stress limitations, which resulted in the in-flight breakup; however, based on the available information, the event that precipitated the descent and loss of control could not be determined.
Probable cause:
A loss of control and subsequent in-flight breakup for reasons that could not be determined
based on the available information.
Final Report:

Crash of a Beechcraft E90 King Air in Ruidoso: 2 killed

Date & Time: Jun 13, 2017 at 2210 LT
Type of aircraft:
Operator:
Registration:
N48TA
Flight Phase:
Flight Type:
Survivors:
No
Schedule:
Ruidoso – Abilene
MSN:
LW-283
YOM:
1978
Crew on board:
1
Crew fatalities:
Pax on board:
1
Pax fatalities:
Other fatalities:
Total fatalities:
2
Captain / Total flying hours:
1073
Captain / Total hours on type:
25.00
Aircraft flight hours:
12621
Circumstances:
The commercial pilot had filed an instrument flight rules flight plan and was departing in dark night visual meteorological conditions on a cross-country personal flight. A witness at the departure airport stated that during takeoff, the airplane sounded and looked normal. The witness said that the airplane lifted off about halfway down runway 24, and there was "plenty" of runway remaining for the airplane to land. The witness lost sight of the airplane and did not see the accident because the airport hangars blocked her view. The wreckage was located about 2,400 ft southeast of the departure end of runway 24. Examination of the accident site indicated that the airplane impacted in a nose-down attitude with a left bank of about 20°. A left turn during departure was consistent with the airport's published instrument departure procedures for obstacle avoidance, which required an immediate climbing left turn while proceeding to a navigational beacon located about 7 miles east-northeast of the airport. Examination of the wreckage did not reveal any evidence of preimpact mechanical malfunctions that would have precluded normal operation. The pilot had reportedly been awake for about 15 hours and was conducting the departure about the time he normally went to sleep and, therefore, may have been fatigued about the time of the event; however, given the available evidence, it was impossible to determine the role of fatigue in this event. Although the circumstances of the accident are consistent with spatial disorientation, there was insufficient evidence to determine whether it may have played a role in the sequence of events.
Probable cause:
The pilot's failure to maintain clearance from terrain after takeoff during dark night conditions.
Final Report:

Crash of a Mitsubishi MU-2B-40 Solitaire off Eleuthera Island: 4 killed

Date & Time: May 15, 2017 at 1329 LT
Type of aircraft:
Registration:
N220N
Flight Phase:
Flight Type:
Survivors:
No
Schedule:
Aguadilla – Space Coast
MSN:
450
YOM:
1981
Country:
Crew on board:
1
Crew fatalities:
Pax on board:
3
Pax fatalities:
Other fatalities:
Total fatalities:
4
Captain / Total flying hours:
1483
Captain / Total hours on type:
100.00
Aircraft flight hours:
4634
Circumstances:
The commercial pilot and three passengers were making a personal cross-country flight over ocean waters in the MU-2B airplane. During cruise flight at flight level (FL) 240, the airplane maintained the same relative heading, airspeed, and altitude for about 2.5 hours before radar contact was lost. While the airplane was in flight, a significant meteorological information notice was issued that warned of frequent thunderstorms with tops to FL440 in the accident area at the accident time. Satellite imagery showed cloud tops in the area were up to FL400. Moderate or greater icing conditions and super cooled large drops (SLD) were likely near or over the accident area at the accident time. Although the wreckage was not located for examination, the loss of the airplane's radar target followed by the identification of debris and a fuel sheen on the water below the last radar target location suggests that the airplane entered an uncontrolled descent after encountering adverse weather and impacted the water. Before beginning training in the airplane about 4 months before the accident, the pilot had 21 hours of multi engine experience accumulated during sporadic flights over 9 years. Per a special federal aviation regulation, a pilot must complete specific ground and flight training and log a minimum of 100 flight hours as pilot-in-command (PIC) in multi engine airplanes before acting as PIC of a MU-2B airplane. Once the pilot began training in the airplane, he appeared to attempt to reach the 100-hour threshold quickly, flying about 50 hours in 1 month. These 50 hours included about 40 hours of long, cross-country flights that the flight instructor who was flying with the pilot described as "familiarization flights" for the pilot and "demonstration flights" for the airplane's owner. The pilot successfully completed the training required for the MU-2B, and at the time of the accident, he had accumulated an estimated 120 hours of multi engine flight experience of which 100 hours were in the MU-2B. Although an MU-2B instructor described the pilot as a good, attentive student, it cannot be determined if his training was ingrained enough for him to effectively apply it in an operational environment without an instructor present. Although available evidence about the pilot's activities suggested he may not have obtained adequate restorative sleep during the night before the accident, there was insufficient evidence to determine the extent to which fatigue played a role in his decision making or the sequence of events.The pilot's last known weather briefing occurred about 8 hours before the airplane departed, and it is not known if the pilot obtained any updated weather information before or during the flight. Sufficient weather information (including a hazardous weather advisory provided by an air traffic control broadcast message about 25 minutes before the accident) was available for the pilot to expect convective activity and the potential for icing along the accident flight's route; however, there is no evidence from the airplane's radar track or the pilot's communications with air traffic controllers that he recognized or attempted to avoid the convective conditions or exit icing conditions.
Probable cause:
The pilot's intentional flight into an area of known icing and convective thunderstorm activity, which resulted in a loss of control of the airplane.
Final Report:

Crash of a Piper PA-31T-620 Cheyenne II in Cascais: 5 killed

Date & Time: Apr 17, 2017 at 1204 LT
Type of aircraft:
Operator:
Registration:
HB-LTI
Flight Phase:
Flight Type:
Survivors:
No
Site:
Schedule:
Cascais – Marseille
MSN:
31T-8020091
YOM:
1980
Country:
Region:
Crew on board:
1
Crew fatalities:
Pax on board:
3
Pax fatalities:
Other fatalities:
Total fatalities:
5
Captain / Total flying hours:
4900
Aircraft flight hours:
8323
Circumstances:
On April 17th, at 11:04 UTC, the aircraft turboprop Piper PA-31 Cheyenne II, registration HBLTI, private property, took off from runway 17 of the Cascais aerodrome (LPCS) bound to Marseille airport (LFML), IFR private flight, with 1 pilot and 3 passengers on board. According to several eyewitness testimonies, after takeoff, the Swiss twin-engine started to put the left wing down and consequently to turn left while climbing slowly to about 300’ feet of altitude. The left bank1 increased and the speed decreased leading the aircraft to stall. The aircraft entered a steep dive and impacted the ground next to a logistics dock of a local supermarket, located southeast of the airfield. The crash occurred 700 m from the end of the departure runway. Following the impact, the aircraft exploded and caught fire affecting a logistic dock, a house and a truck. The aircraft was destroyed by impact force and the post-collision fire, all the four occupants were killed. The driver of the truck affected by the explosion of the plane was also killed. The fuselage, wings, the engines and propellers were severely damaged by the impact force and post-impact fuel-fed fire. The structural damage to the aircraft was consistent with the application of extensive structural loads during the impact sequence, and the effects of the subsequent fire. No pre-crash structural defects were found. All aircraft parts and control surfaces were located at the site. The flaps and the landing gear were found retracted at the time of impact.
Probable cause:
- The pilot’s failure to maintain the airplane control following the power loss in the left critical engine. The root cause for the left engine failure could not be determined due to the extensive impact damages and intensive fire.
Contributing factors:
- Lack of proper pilot training especially concerning the emergency scenario of critical engine failure immediately after takeoff.
Final Report:

Crash of a Piper PA-46-310P Malibu in Harrisburg: 4 killed

Date & Time: Apr 7, 2017 at 1048 LT
Registration:
N123SB
Flight Type:
Survivors:
No
Schedule:
Van Nuys – Eugene
MSN:
46-8508023
YOM:
1985
Crew on board:
1
Crew fatalities:
Pax on board:
3
Pax fatalities:
Other fatalities:
Total fatalities:
4
Captain / Total flying hours:
5060
Captain / Total hours on type:
163.00
Aircraft flight hours:
3681
Circumstances:
The commercial pilot and three passengers departed on an instrument flight rules crosscountry flight. While on approach to the destination airport, the pilot indicated to the air traffic controller that the airplane was passing through areas of moderate-to-extreme precipitation. After clearing the airplane for the approach, the controller noted that the airplane descended below its assigned altitude; the controller issued a low altitude alert, but no response was received from the pilot. The airplane subsequently impacted terrain in a level attitude about 12 miles from the airport. Examination of the airframe, engine, and system components revealed no evidence of preimpact mechanical malfunction that would have precluded normal operation. An area of disturbed, flattened, tall grass was located about 450 ft southwest of the accident site. Based on the images of the grass, the National Weather Service estimated that it would take greater than 35 knots of wind to lay over tall grass as the images indicated, and that a downburst/microburst event could not be ruled out. A downburst is an intense downdraft that creates strong, often damaging winds. About 6 hours before the flight, the pilot obtained weather information through a mobile application. Review of weather data indicated the presence of strong winds, heavy precipitation, turbulence, and low-level wind shear (LLWS) in the area at the time of arrival, which was reflected in the information the pilot received. Given the weather conditions, it is likely that the airplane encountered an intense downdraft, or downburst, which would have resulted in a sudden, major change in wind velocity. The airplane was on approach for landing at the time and was particularly susceptible to this hazardous condition given its lower altitude and slower airspeed. The downburst likely exceeded the climb performance capabilities of the airplane and resulted in a subsequent descent into terrain. It is unknown if the accident pilot checked or received additional weather information before or during the accident flight. While the flight was en route, several PIREPs were issued for the area of the accident site, which also indicated the potential of LLWS near the destination airport; however, the controller did not provide this information to the pilot, nor did he solicit PIREP information from the pilot. Based on published Federal Aviation Administration guidance for controllers and the widespread adverse weather conditions in the vicinity of the accident site, the controller should have both solicited PIREP information from the pilot and disseminated information from previous PIREPs to him; this would have provided the pilot with more complete information about the conditions to expect during the approach and landing at the destination.
Probable cause:
An encounter with a downburst during an instrument approach, which resulted in a loss of control at low altitude. Contributing to the accident was the air traffic controller's failure to
solicit and disseminate pilot reports from arriving and departing aircraft in order to provide pilots with current and useful weather information near the airport.
Final Report:

Crash of a Cessna 500 Citation I in Marietta: 1 killed

Date & Time: Mar 24, 2017 at 1924 LT
Type of aircraft:
Registration:
N8DX
Flight Type:
Survivors:
No
Site:
Schedule:
Cincinnati – Atlanta
MSN:
500-0303
YOM:
1976
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
1
Captain / Total flying hours:
6000
Aircraft flight hours:
9299
Circumstances:
The private pilot departed on an instrument flight rules flight plan in his twin-engine turbojet airplane. The flight was uneventful until the air traffic controller amended the flight plan, which required the pilot to manually enter the new routing information into the GPS. A few minutes later, the pilot told the controller that he was having problems with the GPS and asked for a direct route to his destination. The controller authorized the direct route and instructed the pilot to descend from 22,000 ft to 6,000 ft, during which time the sound of the autopilot disconnect was heard on the cockpit voice recorder (CVR). During the descent, the pilot told the controller that the airplane had a steering problem and was in the clouds. The pilot was instructed to descend the airplane to 4,100 ft, which was the minimum vectoring altitude. The airplane continued to descend, entered visual meteorological conditions, and then descended below the assigned altitude. The controller queried the pilot about the airplane's low altitude and instructed the pilot to maintain 4,100 ft. The pilot responded that he was unsure if he would be able to climb the airplane back to that altitude due to steering issues. The controller issued a low altitude warning and again advised the pilot to climb back to 4,100 ft. The pilot responded that the autopilot was working again and that he was able to climb the airplane to the assigned altitude. The controller then instructed the pilot to change to another radio frequency, but the pilot responded that he was still having a problem with the GPS. The pilot asked the controller to give him direct routing to the airport. A few minutes later, the pilot told the controller that he was barely able to keep the airplane straight and its wings level. The controller asked the pilot if he had the airport in sight, which he did not. The pilot then declared an emergency and expressed concerns related to identifying the landing runway. Afterward, radio contact between the controller and the pilot was lost. Shortly before the airplane impacted the ground, a witness saw the airplane make a complete 360° roll to the left, enter a steep 90° bank to the left, roll inverted, and enter a vertical nose-down dive. Another witness saw the airplane spiral to the ground. The airplane impacted the front lawn of a private residence, and a postcrash fire ensued.The pilot held a type rating for the airplane, but the pilot's personal logbooks were not available for review. As a result, his overall currency and total flight experience in the accident airplane could not be determined. The airplane was originally certified for operations with a pilot and copilot. To obtain an exemption to operate the airplane as a single pilot, a pilot must successfully complete an approved single-pilot exemption training course annually. The accident airplane was modified, and the previous owner was issued a single-pilot conformity certificate by the company that performed the modifications. However, there was no record indicating that the accident pilot received training under this exemption. Several facilities that have single-pilot exemption training for the accident airplane series also had no record of the pilot receiving training for single-pilot operations in the accident airplane. Therefore, unlikely that the pilot was properly certificated to act as a single-pilot. The GPS was installed in the airplane about 3.5 years before the accident. A friend of the pilot trained him on how to use the GPS. The friend said that the pilot generally was confused about how the unit operated and struggled with pulling up pages and correlating data. The friend of the pilot had flown with him several times and indicated that, if an air traffic controller amended a preprogrammed flight plan while en route, the pilot would be confused with the procedure for amending the flight plan. The friend also said the pilot depended heavily on the autopilot, which was integrated with the GPS, and that he would activate the autopilot immediately after takeoff and deactivate it on short final approach to a runway. The pilot would not trim the airplane before turning on the autopilot because he assumed that the autopilot would automatically trim the airplane, which led to the autopilot working against the mis-trimmed airplane. The friend added that the pilot was "constantly complaining" that the airplane was "uncontrollable." A postaccident examination of the airplane and the autopilot system revealed no evidence of any preimpact deficiencies that would have precluded normal operation. This information suggests that pilot historically had difficulty flying the airplane without the aid of the autopilot. When coupled with his performance flying the airplane during the accident flight without the aid of the autopilot, it further suggests that the pilot was consistently unable to manually fly the airplane. Additionally, given the pilot's previous experience with the GPS installed on the airplane, it is likely that during the accident flight the pilot became confused about how to operate the GPS and ultimately was unable to properly control of the airplane without the autopilot engaged. Based on witness information, it is likely that during the final moments of the flight the pilot lost control of the airplane and it entered an aerodynamic stall. The pilot was then unable to regain control of the airplane as it spun 4,000 ft to the ground.
Probable cause:
The pilot's failure to maintain adequate airspeed while manually flying the airplane, which resulted in the airplane exceeding its critical angle of attack and experiencing an aerodynamic stall. Contributing to the accident was the pilot's inability control the airplane without the aid of the autopilot.
Final Report:

Crash of a Pilatus PC-12/47E in Cat Cay

Date & Time: Mar 8, 2017 at 1246 LT
Type of aircraft:
Operator:
Registration:
N8TS
Flight Type:
Survivors:
Yes
Schedule:
Saint Petersburg - Cat Cay
MSN:
1650
YOM:
2016
Location:
Country:
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
Pilot advised that upon making his approach to land at Cat Cay (MYCC), on short final he experienced an unexpected accelerated sink rate. To compensate for the sink rate he increased the pitch of the aircraft. While going over the threshold, a slight impact was felt as the landing gear came into contact with the seawall. He flew the aircraft until it came to a stop about 600 feet down the runway. No injuries were sustained, aircraft received substantial damage.
Final Report:

Crash of a Cessna 421B Golden Eagle II in Cherokee County: 1 killed

Date & Time: Mar 4, 2017 at 0023 LT
Registration:
N421KL
Flight Type:
Survivors:
No
Schedule:
Tulsa - Cherokee County
MSN:
421B-0015
YOM:
1970
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
1
Captain / Total flying hours:
4000
Aircraft flight hours:
7522
Circumstances:
The 69-year-old commercial pilot was making a personal cross-country flight in the newly purchased airplane. When the airplane was on final approach to the destination airport in night visual meteorological conditions, airport surveillance video showed it pitch up and roll to the right. The airplane then descended in a nose-down attitude to impact in a ravine on the right side of the runway. During the descent over the ravine the right wing came in contact with a powerline that briefly cut power to the airport. Postaccident examination of the airframe, engines, and their components revealed no evidence of mechanical anomalies or malfunctions that would have precluded normal operation. The pilot's toxicology findings identified five different impairing medications: clonazepam, temazepam, hydrocodone, nortriptyline, and diphenhydramine. Although the results were from cavity blood and may not accurately reflect antemortem levels, the hydrocodone, temazepam, and diphenhydramine levels were high enough to likely have had some psychoactive effects. While the exact effects of these drugs in combination are not known, it is likely that the pilot was impaired to some degree by his use of this combination of medications, which likely contributed to his failure to maintain control of the airplane.
Probable cause:
The pilot's failure to maintain control of the airplane during a night visual landing approach. Contributing to the accident was the pilot's impairment due to his use of a combination of medications.
Final Report:

Crash of a Beechcraft G18S off Metlakatla

Date & Time: Mar 3, 2017 at 0815 LT
Type of aircraft:
Operator:
Registration:
N103AF
Flight Type:
Survivors:
Yes
Schedule:
Klawock – Ketchikan
MSN:
BA-526
YOM:
1960
Crew on board:
2
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
10308
Captain / Total hours on type:
330.00
Aircraft flight hours:
17646
Circumstances:
The pilot of the twin-engine airplane and the pilot-rated passenger reported that, during a missed approach in instrument meteorological conditions, at 2,000 ft mean sea level, the right engine seized. The pilot attempted to feather the right engine by pulling the propeller control to the feather position; however, the engine did not feather. The airplane would not maintain level flight, so the pilot navigated to a known airport, and the passenger made emergency communications with air traffic control. The pilot was unable to maintain visual reference with the ground until the airplane descended through about 100 to 200 ft and the visibility was 1 statute mile. The pilot stated that he was forced to ditch the airplane in the water about 5 miles short of the airport. The pilot and passenger egressed the airplane and swam ashore before it sank in about 89 ft of water. Both the pilot and passenger reported that there was postimpact fire on the surface of the water. The airplane was not recovered, which precluded a postaccident examination. Thus, the reason for the loss of engine power could not be determined.
Probable cause:
An engine power loss for reasons that could not be determined because the airplane was not recovered.
Final Report: