Crash of a Mitsubishi MU-2B-35 Marquise in Smyrna

Date & Time: Sep 21, 1995 at 0425 LT
Type of aircraft:
Registration:
N309MA
Flight Phase:
Flight Type:
Survivors:
Yes
Schedule:
Smyrna - Louisville
MSN:
602
YOM:
1973
Crew on board:
1
Crew fatalities:
Pax on board:
1
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
2140
Captain / Total hours on type:
112.00
Aircraft flight hours:
4304
Circumstances:
A witness stated he observed the airplane on climbout from runway 32. The airplane started a right turn estimated at about 30 to 45° angle of bank. The airplane stopped climbing and began descending. Subsequently, it collided with a tree line, while in a right bank, and then it impacted the ground. Weather conditions at the time of accident were described by the witness as very dark, with no ambient light or visible horizon. Examination of the airframe, flight control system, engine assembly, and propeller assembly revealed no evidence of a precrash failure or malfunction. The autopilot was found in the off position, and the autopilot circuit breakers were not tripped. The pilot and passenger were seriously injured and had no memory of the flight. A radio transcript revealed that after taking off, the flight had made one radio transmission to request an ifr clearance.
Probable cause:
Failure of the pilot to maintain a proper climb rate after takeoff, and his inadvertent entry in a descending spiral, which he failed to correct. Factors relating to the accident were: darkness, and the pilot becoming spatially disoriented during the initial climb while attempting to obtain an ifr clearance.
Final Report:

Crash of a Swearingen SA226T Merlin III in Chino

Date & Time: Sep 18, 1995 at 0624 LT
Registration:
N693PG
Flight Type:
Survivors:
Yes
Schedule:
Apple Valley - Chino
MSN:
T-207
YOM:
1970
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
3282
Captain / Total hours on type:
346.00
Aircraft flight hours:
5218
Circumstances:
During arrival at dawn, the pilot contacted Approach Control about 22 miles from the airport at 8,500 feet and requested an ILS runway 26 approach. The ATIS was reporting 1/8 mile visibility with fog; the minimum published visibility for the ILS landing was 3/4 mile. The controller vectored the aircraft so that it intercepted the ILS localizer at the outer marker at an intercept angle that was 5 degrees greater than the maximum allowable intercept of 30 degrees. The intercept point should have been at least 3 miles further away from the airport. The aircraft was 650 feet above the ILS glideslope at the outer marker (which was outside the ILS glideslope parameter). Instead of making a missed approach, the pilot elected to continue the ILS. As he attempted to intercept the glideslope from above, the airplane entered a high rate of descent and passed through the glideslope. The pilot was arresting the descent, when the airplane collided with level terrain about 1,000 feet short of the runway. After the accident, at 0646 edt, the visibility was 1/16 mile with fog.
Probable cause:
The pilot's improper IFR procedure by not initiating a missed approach at the outer marker, by attempting to intercept the glideslope from above after passing the outer marker, and by allowing the airplane to continue descending after reaching the decision height. Factors relating to the accident were: the adverse weather condition, and the approach controller's improper technique in vectoring the airplane onto the ILS localizer.
Final Report:

Crash of a Short SC.7 Skyvan 3 Variant 200 near Farewell: 1 killed

Date & Time: Sep 1, 1995 at 1200 LT
Type of aircraft:
Operator:
Registration:
N30GA
Flight Phase:
Flight Type:
Survivors:
No
Site:
Schedule:
Farewell - Anchorage
MSN:
1839
YOM:
1968
Location:
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
1
Captain / Total flying hours:
11389
Captain / Total hours on type:
2200.00
Aircraft flight hours:
15798
Circumstances:
The pilot had departed a remote airstrip on the return portion of a cargo flight. An instrument flight plan was on file with the ARTCC. After departure, the pilot attempted to contact ARTCC to open his flight plan but communications were not established. The airplane struck mountainous terrain about 6 miles south of the departure airport. Radar data showed that after departure, the airplane climbed westbound and then turned southbound toward higher terrain. It circled southwest of the airport and turned eastbound while climbing to 5,300 feet msl. The airplane then turned southbound again toward the accident site. The last recorded radar data was at 5,200 feet msl. The airplane struck a ridgeline about 4,800 feet msl. Airmets were in effect for IFR conditions, low ceilings, mountain obscurations, rain, fog, and icing in clouds and in precipitation. A witness reported that when the airplane arrived at the airport, the airframe had a coating of ice. When the airplane departed, snow was falling at the airport.
Probable cause:
The pilot's continued vfr flight into instrument meteorological conditions. The weather was a factor.
Final Report:

Crash of a Douglas C-47B-1-DL in Vancouver: 1 killed

Date & Time: Aug 19, 1995 at 0906 LT
Operator:
Registration:
C-GZOF
Flight Phase:
Flight Type:
Survivors:
Yes
Schedule:
Vancouver – Whitehorse
MSN:
20833
YOM:
1944
Country:
Crew on board:
3
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
1
Circumstances:
The DC-3 aircraft, with the captain, first officer, and an apprentice aircraft maintenance engineer on board, was to be ferried from Vancouver, British Columbia, to Whitehorse, Yukon. Just after take-off from runway 08, as the first officer was setting the engine power, the right propeller began to over-speed. The captain told the first officer to shut down and feather the right engine. The first officer did as instructed, and advised the Vancouver tower controller of the engine problem and that they would return to the airport to land on runway 08. The captain turned the aircraft to the right, onto downwind for runway 08; however, because the aircraft's altitude and airspeed were decreasing, the first officer advised the tower controller that they would land on runway 30. The aircraft continued to lose height, narrowly avoiding buildings in its path, and crashed to the ground, one mile short of runway 30. The three occupants were seriously injured during the impact and the post-crash fire; the captain died of his injuries eight days after the accident.
Probable cause:
The aircraft's right engine oil system malfunctioned for reasons that were not determined, and the right propeller did not completely feather during the emergency shutdown. The aircraft was unable to maintain flight because of the drag generated by the windmilling right propeller.

Crash of a Cessna 402A in Miami

Date & Time: Jun 23, 1995 at 1054 LT
Type of aircraft:
Operator:
Registration:
N7884J
Flight Type:
Survivors:
Yes
Schedule:
Marsh Harbor - Miami
MSN:
402A-0103
YOM:
1969
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
9800
Captain / Total hours on type:
7800.00
Aircraft flight hours:
4980
Circumstances:
The aircraft crashed on a visual approach to runway 09 left at Miami International Airport, Miami, Florida. Visual meteorological conditions prevailed and an IFR flight plan was filed. The airplane was destroyed. The airline transport pilot sustained serious injuries. The flight originated from Marsh Harbor, Bahamas, about 1 hour 14 minutes before the accident. Witnesses stated they observed the airplane descending to the right of the final approach path for runway 09 left with the landing gear down and an engine was heard sputtering. The wings of the airplane were observed to be rocking back and forth. The airplane rolled right 90 degrees. The nose pitched up, the airplane rolled over inverted, the nose pitched down, the airplane collided with a parking lot and slid in between a front end loader and a dump truck coming to a complete stop. Transcripts of recorded transmissions between Miami Air Traffic Control Tower (ATCT), N7884J, and review of Miami ATCT continuous data recording radar revealed there were no airplanes in the vicinity of N7884J at the time of the accident.
Probable cause:
The pilot-in-command's failure to maintain airspeed (VMC) after loss of power of one engine while on final approach, resulting in an in-flight loss of control and subsequent in-flight collision with terrain. Contributing to the accident was a total loss of engine power of the right engine due to fuel exhaustion.
Final Report:

Crash of a Piper PA-31T Cheyenne in Liuli

Date & Time: May 16, 1995 at 1311 LT
Type of aircraft:
Registration:
5Y-FKI
Flight Phase:
Flight Type:
Survivors:
Yes
Country:
Region:
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
3500
Circumstances:
Shortly after takeoff from Liuli Airstrip, while climbing, the pilot made a sharp turn to avoid a sand dune when he lost control of the aircraft that crashed on the ground. There were no casualties but the aircraft was written off.

Crash of a Cessna 207 Skywagon in Kodiak

Date & Time: Apr 25, 1995 at 1940 LT
Operator:
Registration:
N1769U
Flight Phase:
Flight Type:
Survivors:
Yes
Site:
Schedule:
Old Harbor - Kodiak
MSN:
207-0369
YOM:
1977
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
3700
Captain / Total hours on type:
700.00
Aircraft flight hours:
11036
Circumstances:
The pilot was informed by another company pilot that the higher passes were closed. He then attempted to fly through 'high pass' located near old harbor. The pilot described the weather as overcast with ceilings obscured, and flight visibility was 2 to 3 miles. The pass was snow covered. As he entered the pass he lost visual reference due to whiteout conditions and he initiated a left turn to exit the pass. Approx half way through the turn the left wing struck the mountain.
Probable cause:
The pilot's continued flight into known adverse weather. The whiteout condition was a factor.
Final Report:

Crash of a Cessna 402B in the Pacific Ocean: 1 killed

Date & Time: Apr 18, 1995
Type of aircraft:
Registration:
N2NB
Flight Phase:
Flight Type:
Survivors:
No
Schedule:
Kolonia – Tarawa
MSN:
402B-0410
YOM:
1973
Country:
Region:
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
1
Circumstances:
The pilot, sole on board, departed Kolonia Airport on a 5 hours and 45 minutes flight to Tarawa Island, Gilbert Islands. En route, radar and contact were lost with the airplane that crashed in the Pacific Ocean. SAR operations were initiated but abandoned after few days as no trace of the aircraft nor the pilot was found.

Crash of a Douglas DC-8-63CF in Kansas City: 3 killed

Date & Time: Feb 16, 1995 at 2027 LT
Type of aircraft:
Operator:
Registration:
N782AL
Flight Phase:
Flight Type:
Survivors:
No
Schedule:
Kansas City - Westover
MSN:
45929
YOM:
1968
Crew on board:
3
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
3
Captain / Total flying hours:
9741
Captain / Total hours on type:
4483.00
Copilot / Total flying hours:
4460
Copilot / Total hours on type:
218
Aircraft flight hours:
77096
Aircraft flight cycles:
22404
Circumstances:
The airplane crashed immediately after liftoff during a three-engine takeoff. Flightcrew had shortened rest break; rest periods not required for ferry flights. Flight crew fatigue from lack of rest, sleep, and disruption of circadian rhythms. Flightcrew did not have adequate, realistic training in three-engine takeoff techniques or procedures. Flight crew did not adequately understand three-engine takeoff procedures, including significance of vmcg. Flight engineer improperly determined vmcg speed, resulting in value 9 knots too low. During first takeoff attempt, captain applied power to asymmetrical engine too soon, was unable to maintain directional control, and rejected the takeoff. Captain agreed to modify procedure by allowing flight engineer to advance throttle, a deviation of prescribed procedure. FAA oversight of operator was inadequate because the poi and geographic inspectors were unable to effectively monitor domestic crew training and international operations. Existing far part 121 flight time limits & rest requirements that pertained to the flights that the flightcrew flew prior to the ferry flights did not apply to the ferry flights flown under far part 91. Current one-engine inoperative takeoff procedures do not provide adequate rudder availability for correcting directional deviations during the takeoff roll compatible with the achievement of maximum asymmetric thrust at an appropriate speed greater than ground minimum control speed. All three crew members were killed.
Probable cause:
The accident was the consequence of the following factors:
- The loss of directional control by the pilot in command during the takeoff roll, and his decision to continue the takeoff and initiate a rotation below the computed rotation airspeed, resulting in a premature liftoff, further loss of control and collision with the terrain.
- The flightcrew's lack of understanding of the three-engine takeoff procedures, and their decision to modify those procedures.
- The failure of the company to ensure that the flightcrew had adequate experience, training, and rest to conduct the nonroutine flight. Contributing to the accident was the inadequacy of Federal Aviation Administration oversight of air transport international and federal aviation administration flight and duty time regulations that permitted a substantially reduced flightcrew rest period when conducting a non revenue ferry flight under 14 code of federal regulations part 91.
Final Report:

Crash of an ATR72-202 near Taipei: 4 killed

Date & Time: Jan 30, 1995 at 1943 LT
Type of aircraft:
Operator:
Registration:
B-22717
Flight Type:
Survivors:
No
Site:
Schedule:
Magong - Taipei
MSN:
435
YOM:
1994
Country:
Region:
Crew on board:
4
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
4
Circumstances:
The crew was completing a positioning flight from Magong to Taipei. While descending to Taipei-Songshan Airport, the crew encountered poor weather conditions with a limited visibility due to heavy rain falls. The minimum descent altitude was fixed at 2,500 feet but for unknown reasons, the crew descended to 1,000 feet when the aircraft struck the slope of a wooded hill located 20 km from the airport. The aircraft was destroyed upon impact and all four crew members were killed.
Probable cause:
The crew failed to adhere to the published approach procedures and continued the descent below MDA until the aircraft struck the ground. Brand new, the aircraft was delivered to TransAsia Airways last December 20 and was equipped with a category II GPWS. It is believed that the GPWS alarm did not sound in the cockpit and was not recorded on the CVR.