Crash of a Cessna 441 Conquest II in Winfield: 2 killed

Date & Time: Jan 30, 2002 at 1359 LT
Type of aircraft:
Operator:
Registration:
N441AR
Flight Phase:
Survivors:
No
Schedule:
Springdale – Rifle
MSN:
441-0148
YOM:
1980
Location:
Crew on board:
1
Crew fatalities:
Pax on board:
1
Pax fatalities:
Other fatalities:
Total fatalities:
2
Captain / Total flying hours:
1500
Aircraft flight hours:
3529
Circumstances:
Impact forces and fire destroyed the airplane when it impacted the terrain after a loss of control during cruise flight. The pilot received a weather brief by AFSS prior to departure concerning the IFR conditions along the route of flight, which included, rain, freezing rain, icing, turbulence, and snow. The cloud tops were forecast to be 25,000 feet. The pilot filed a flight plan with a cruise flight level of 28,000 feet. About 32 minutes after takeoff, at 1345:58, the pilot reported he had an attitude gyro problem and that he was hand flying the airplane. The airplane's altitude remained at about 28,000 feet for the next seven minutes. At 1352:46, the pilot stated he had an emergency, but at 1352:53, the pilot stated, "Uh it came back on never mind." At 1353:26, the pilot stated, "I need to get to uh anywhere I can get a visual." At 1353:56, the airplane was cleared to climb to 31,000 feet, and radar data indicated the airplane was currently at 27,000 feet. The radar data indicated the airplane went into a series of steep descents and climbs over the next 4.5 minutes until radar contact was lost at 2,500 feet. The pilot of a commercial airline who was flying in the same sector as the accident airplane reported that he heard the accident pilot state that he was in a spin. The commercial airline pilot stated they were flying at 33,000 feet and were "barely above the tops" of the clouds. The airplane impacted the terrain in a steep nose down attitude and burst into flames. The engines, flight controls, and flight instruments did not exhibit any pre-existing anomalies. A witness reported that two days prior to the accident, the pilot had advised him that the airplane's attitude gyro was having problems. There was no record that the pilot had the attitude gyro inspected prior to the accident. A witness reported the pilot routinely flew with the autopilot engaged soon after takeoff. He reported that he had never observed the pilot hand-fly the airplane in instrument conditions.
Probable cause:
The pilot's spatial disorientation resulting in a loss of control and collision with the ground. Additional factors included the pilot operating the airplane with known deficiencies and the instrument flight conditions.
Final Report:

Crash of a Cessna 340A in Temple: 3 killed

Date & Time: Jan 17, 2002 at 1522 LT
Type of aircraft:
Registration:
N339S
Survivors:
Yes
Site:
Schedule:
League City – Killeen
MSN:
340A-0712
YOM:
1979
Crew on board:
1
Crew fatalities:
Pax on board:
4
Pax fatalities:
Other fatalities:
Total fatalities:
3
Captain / Total flying hours:
3464
Captain / Total hours on type:
10.00
Aircraft flight hours:
5877
Circumstances:
While on an IFR clearance, the pilot reported to approach control that he was unable to maintain 4,000 feet msl, and did not give a reason. Shortly thereafter, the pilot contacted approach control and stated that he had "fuel starvation" in the right engine and the left engine had just quit. Radar data depicted the aircraft at an altitude of 3,400 feet. The controller asked the pilot if they were completely without power, and the pilot responded, "yes, we're now gliding." The controller gave the pilot instructions to the nearest airport, which was approximately 4.5 nautical miles away. After passing 2,100 feet, the pilot informed the controller that he would be landing short. During the forced landing, the airplane struck the top of a tree, crossed over a house, struck another tree, struck a telephone wire which crossed diagonally over a street, and then cleared a set of wires which paralleled the street. The airplane then impacted a private residence within a residential area, and a fire erupted damaging the airplane and the private residence. Ten gallons of fuel were drained from the left locker tank, which supplements the left main fuel tank. Examination of the airframe and engines did not disclose any structural or mechanical anomalies that would have prevented normal operation. Examination of the propeller revealed that neither propeller had been
feathered.
Probable cause:
The pilot's mismanagement of fuel, which resulted in a total loss of engine power due to fuel starvation. Contributing factors were the pilot's failure to follow the checklist to feather the propellers in order to reduce drag.
Final Report:

Crash of a Piper PA-46-350P Malibu Mirage in Raleigh: 3 killed

Date & Time: Dec 12, 2001 at 1904 LT
Operator:
Registration:
N41003
Survivors:
No
Schedule:
Dothan - Raleigh
MSN:
46-22044
YOM:
1989
Crew on board:
1
Crew fatalities:
Pax on board:
2
Pax fatalities:
Other fatalities:
Total fatalities:
3
Captain / Total flying hours:
926
Captain / Total hours on type:
10.00
Aircraft flight hours:
1679
Circumstances:
The flight was cleared for the ILS approach to runway 5R. The flight was at mid runway, at 2,100 feet, heading 049 degrees, at a speed of 163 knots, when the pilot stated "...missed approach." He was instructed to maintain 2,000, and to fly runway heading. Radar showed N41003 started a right turn, was flying away from the airport/VOR, descending. At a point 0.57 miles from the airport/VOR, the flight had descended to 1,500 feet, was turning right, and increasing speed. The flight had descended 400 feet, and had traveled about 0.32 miles in 10 seconds. When radio and radar contact were lost, the flight was 2.35 miles from the airport/VOR, level at 1,600 feet, on a heading of 123 degrees, and at a speed of 169 knots. The published decision height (DH) was 620 feet mean sea level (msl). The published minimum visibility was 1/2 mile. The published Missed Approach in use at the time of the accident was; "Climb to 1,000 [feet], then climbing right turn to 2,500 [feet] via heading 130 degrees, and RDU R-087 [087 degree radial] to ZEBUL Int [intersection] and hold." A witness stated that the aircraft was flying low, power seemed to be in a cruise configuration, and maintaining the same sound up until the crash. The reported weather at the time was: Winds 050 at 5 knots, visibility 1/2 statute mile, obscuration fog and drizzle, ceiling overcast 100, temperature and dew point 11 C, altimeter 30.30 in HG. At the time of the accident the pilot had 10 total flight hours in this make and model airplane; 33 total night flight hours; and 59 total instrument flight hours.
Probable cause:
The pilot's failure to maintain control of the airplane, due to spatial disorientation, while performing a missed approach, resulting in an uncontrolled descent, and subsequent impact with a tree and a house. Factors in this accident were dark night, fog, drizzle, the pilot's lack of total instrument time, and his lack of total experience in this type of aircraft.
Final Report:

Crash of a Piper PA-31T Cheyenne in Graham: 4 killed

Date & Time: Nov 12, 2001 at 2324 LT
Type of aircraft:
Registration:
N6134A
Survivors:
No
Site:
Schedule:
Wharton – Graham
MSN:
31-7804006
YOM:
1978
Location:
Crew on board:
1
Crew fatalities:
Pax on board:
3
Pax fatalities:
Other fatalities:
Total fatalities:
4
Captain / Total flying hours:
4849
Aircraft flight hours:
3240
Circumstances:
At 2144, the pilot contacted air traffic control and requested visual flight rules (VFR) flight following to his destination. The flight was the final leg of a four-leg trip, which the pilot had begun approximately 1120 that morning. At 2220, the flight began a slow descent toward the destination airport. Radar data confirmed that the airplane executed a steady descent, and flew a straight line course toward Graham. The final radar return occurred 37 minutes later at an altitude of 3,000 feet (radar coverage is not available below 3,000 feet), 8 miles southeast of the Graham Municipal Airport. Two minutes after the final radar return, the pilot reported to air traffic control that the flight was two miles out, and he canceled VFR flight following. No further communications or distress calls were received from the airplane. The pilot did not request or receive updated weather from the air traffic controllers during the flight. According to witnesses who lived near the accident site, they heard an airplane flying low, observed dense fog and heard the sounds of an airplane crashing. According to the nearest weather reporting station, near the time of the accident, the temperature- dew point spread was within 2 degrees, visibilities were reduced to between 3 and 4 miles in fog, and the ceiling was decreasing from 600 feet broken to 400 feet overcast. At the time of the accident, the pilot's duty day exceeded 12 hours. Examination of the airframe revealed no preimpact anomalies and that the gear was extended and the flaps were retracted. Examination of both engines revealed evidence of power at the time of impact.
Probable cause:
The pilot's failure to discontinue the approach after encountering instrument meteorological conditions, which resulted in controlled flight into terrain. Contributing factors were the dark night light condition, low ceiling, and reduced visibility due to fog.
Final Report:

Crash of a Beechcraft B200 Super King Air in Chesterfield

Date & Time: Oct 25, 2001 at 1538 LT
Operator:
Registration:
N200RW
Survivors:
Yes
Schedule:
Chesterfield - Osage Beach
MSN:
BB-242
YOM:
1977
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
19213
Captain / Total hours on type:
13242.00
Aircraft flight hours:
11416
Circumstances:
The Beech 200 was substantially damaged during an aborted landing. The winds were gusting in excess of the airplane's maximum demonstrated crosswind component. A witness reported finding landing gear strut pieces on the runway after the Beech 200's landing attempt. The flight then aborted the landing and continued on to its originating airport where the airplane veered off the runway and damaged airport property during its landing.
Probable cause:
The inadequate planning/decision and the exceeded crosswind component by the pilot. The gusts were a contributing factor.
Final Report:

Crash of a Beechcraft C90 King Air in Dallas

Date & Time: Oct 9, 2001 at 1322 LT
Type of aircraft:
Registration:
N690JP
Survivors:
Yes
Schedule:
Taos - Dallas
MSN:
LJ-690
YOM:
1976
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
7000
Captain / Total hours on type:
100.00
Aircraft flight hours:
2356
Circumstances:
The commercial pilot flew the airplane on a cross-country flight of at least 2 hours and 47 minutes before dropping of his passengers, and flew back for 2 hours and 7 minutes without refueling. The pilot reported that as the airplane turned onto final approach, the right engine began to surge. He reduced the power on the right engine and increased power on the left, but the airplane started to roll right so he elected to reduce the power on the left engine and land in an alley. Prior to impacting wires, the pilot retracted the landing gear and brought the condition levers to "cut-off." A witness observed the airplane prior to impact and noted that the "motor wasn't on." The airplane impacted power lines, a tree, a natural gas meter, two residences, and a fence. The fuel tanks were compromised during the impact sequence, and the fire department sprayed the area with fire retardant foam. A test of the water runoff revealed "negative results for petroleum risk." Examination of both engines' fuel lines between their respective firewalls and fuel heaters, and fuel pumps and fuel control units revealed that they were void of fuel.
Probable cause:
The pilot's failure to refuel the airplane, which resulted in fuel exhaustion and subsequent loss of dual engine power while on approach.
Final Report:

Crash of a Beechcraft C90 King Air near Mainpuri: 8 killed

Date & Time: Sep 30, 2001 at 1331 LT
Type of aircraft:
Registration:
VT-EFF
Flight Phase:
Survivors:
No
Schedule:
New Delhi - Kanpur
MSN:
LJ-705
YOM:
1977
Country:
Region:
Crew on board:
2
Crew fatalities:
Pax on board:
6
Pax fatalities:
Other fatalities:
Total fatalities:
8
Captain / Total flying hours:
1596
Circumstances:
En route from New Delhi to Kanpur, the crew reported over Aligarh. Short of next reporting point Kadas, the aircraft was about 10 miles right of track for which the permission was obtained and the pilot requested for a direct routing to Kanpur. About 10 minutes later, at an altitude of 14,000 feet, while cruising in bad weather conditions, the twin engine aircraft entered an uncontrolled descent, partially disintegrated in the air and eventually crashed in an open field near Mainpuri. All eight occupants were killed.
Probable cause:
While in cruising altitude, the crew encountered severe updrafts while flying in thunderstorm activity. Following a possible abrupt and abnormal manoeuvre, the crew lost control of the airplane that entered a spiral dive, resulting in an in-flight break up due to aerodynamic overload, leading to a total loss of control followed with a heavy impact with the ground.
Final Report:

Crash of a De Havilland DHC-2 Beaver near Mackenzie Lake: 5 killed

Date & Time: Aug 13, 2001 at 1706 LT
Type of aircraft:
Operator:
Registration:
C-GVHT
Flight Phase:
Survivors:
No
Schedule:
Campbell River - Mackenzie Sound
MSN:
257
YOM:
1952
Country:
Crew on board:
1
Crew fatalities:
Pax on board:
4
Pax fatalities:
Other fatalities:
Total fatalities:
5
Aircraft flight hours:
11325
Circumstances:
A de Havilland DHC-2 Beaver floatplane, C-GVHT (serial number 257), took off from Campbell River, British Columbia, at 1530 Pacific daylight time, with a pilot and four passengers on board. The aircraft was on a visual flight rules flight to a logging camp on Mackenzie Sound, 76 nautical miles northwest of Campbell River, and was scheduled to arrive at 1700. When the aircraft arrived over the Mackenzie logging camp, the pilot informed ground personnel by radio that he was overhead at 2800 feet, between cloud layers with no place to descend, and that because of unfavourable weather conditions, he was returning, presumably to Campbell River. The aircraft then flew to a clear area north of the camp and entered the Frederic Creek valley. When company ground personnel could not contact the aircraft by radio, they began a ground search, later followed by an aerial search. The searches were hampered by poor weather. The aircraft wreckage was found three days later, about four nautical miles northeast of the camp. The accident occurred at 1706 in daylight conditions. All occupants were fatally injured, and the aircraft was destroyed. The emergency locator transmitter was destroyed on impact and did not transmit a signal. No fire occurred.
Probable cause:
Findings as to Causes and Contributing Factors:
1. The pilot abandoned his attempt to fly through the pass because of unsuitable weather conditions. He flew into a confined area that required him to manoeuvre the aircraft aggressively to avoid the rising terrain, causing the aircraft to stall.
2. The aircraft weight exceeded the certificated MAUW, and the CG was outside the floatplane aft limit. The out-of-limit weight and balance aggravated aerodynamic stall and produced rapid and
uncontrolled aircraft attitudes from which the pilot could not recover before striking the trees.
3. Basic weight and balance of the aircraft was incorrectly recorded in several aircraft documents, leading to remarkable discrepancies in take-off weight and CG calculations. As a result, a pilot could not calculate an accurate weight and balance. In certain conditions, calculations erroneously showed that the aircraft was below maximum allowable gross weight.
Findings as to Risk:
1. The practice of using a non-standard passenger weight led to inaccurate take-off weight calculations and provided an estimated total passenger weight that was 185 pounds less than actual.
2. Weight and balance calculations performed using inaccurate figures would not have revealed that the aircraft was overloaded until it was approximately 450 pounds beyond the maximum limit.
3. Aircraft weight exceeded the maximum allowable gross weight, and the CG was outside the aft CG limit. This weight and balance combination placed the aircraft outside the manufacturer’s
original design envelope, to where slow speed and stall handling characteristics are neither proven nor certificated.
4. Cargo was not secured by the available cargo restraint and might have shifted during aircraft manoeuvring. Such cargo movement would have exacerbated the effects of the existing aft CG and likely increased the level of injury to the occupants.
Other Findings:
1. The pilot chose to fly above cloud in accordance with the visual flight rules and could not descend through the cloud at his intended landing site.
2. The Alaska cargo door installation increases the volume of the cargo compartment. The installation is thereby conducive to larger loads being stowed farther aft and possible overloading of the cargo compartment.
3. The DHC-2 Beaver is not equipped with an aural or visual stall warning system, nor is it required by regulation. Warning of an impending stall is dependent on juddering or some other aerodynamic indication.
Final Report:

Crash of a Piper PA-60 Aerostar (Ted Smith 602P) in Rock Springs

Date & Time: Aug 9, 2001 at 1330 LT
Registration:
N44JH
Survivors:
Yes
Schedule:
Rock Springs – Marysville
MSN:
62-0902-8165031
YOM:
1981
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
2578
Captain / Total hours on type:
520.00
Aircraft flight hours:
2998
Circumstances:
The airplane had just taken off and was climbing through 9,000 feet when the pilot heard "a very loud explosive sound" that came from the right side of the aircraft. He returned to the airport and landed. When the airplane touched down, it began veered to the right and the pilot attempted to correct. The airplane departed the right side of the runway and the right main landing gear collapsed, driving it through the top of the wing. Half of the right main tire (30 hours total time in service) and most of its inner tube (with a round section blown out) were found at the point of touch down. Missing was the valve stem. Continuous S-shaped marks indicated the tire came off the rim.
Probable cause:
The right main tire blowing out in flight, which resulted in a loss of directional control during landing.
Final Report:

Crash of a Beechcraft B200 Super King Air in Sandersville

Date & Time: Aug 9, 2001 at 0948 LT
Registration:
N899RW
Survivors:
Yes
Schedule:
Dublin - Sandersville
MSN:
BB-1637
YOM:
1998
Crew on board:
1
Crew fatalities:
Pax on board:
5
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
4900
Captain / Total hours on type:
978.00
Aircraft flight hours:
996
Circumstances:
The flight made two instrument approaches to minimums and executed two missed approaches before the crew elected to land about 25 miles south and wait for the low ceiling condition to improve. An hour later, having topped off fuel tanks, confirmed by telephone that destination weather was improving, the flight re-launched to their original destination. They executed a GPS-A, (circling) instrument approach, broke out of instrument conditions about 100 ft. above minimums, (600 feet, agl) and about one mile from the runway, and started a right downwind turn to enter a left base leg for landing runway 30. During the turn to final approach, the crew extended the landing gear and flaps for landing, and according to the copilot, the pilot flew through the extended runway centerline requiring a, " teardrop turn back toward the runway. In the turn the bank angle was about 45 degrees, the descent rate increased rapidly and a faint warning [stall warning] sounded, the nose then pitches down and [the PIC] screams as he shoves both throttles full forward and using both hands pulls the yoke back and as soon as the nose came above the horizon the plane impacted the ground wings were fairly level mains hit first and we paralleled the runway about fifty feet or so to the right of the runway". The impact sheared the landing gear, shed the propellers, broke the engines from their mounts, started a fire in the left engine, and broke open the fuselage 3 feet aft of the cabin pressure bulkhead. The two pilots and three of four passengers received minor injuries, and one passenger received serious injuries. The cockpit voice recorder was shipped to the NTSB Vehicle Recorders Laboratory in Washington, DC. Readout of data recorded from the cockpit area microphone revealed that 6.4 seconds before impact the stall warning sounded, and 4.4 seconds before impact the altitude alerter sounded.
Probable cause:
The pilot-in command's failure to maintain airspeed during the approach, resulting in an inadvertent stall and in-flight collision with the terrain during an uncontrollable descent.
Final Report: