Crash of a Mitsubishi MU-2B-20 Marquise in Kenefic: 1 killed

Date & Time: May 7, 1991 at 0510 LT
Type of aircraft:
Registration:
N106MA
Flight Phase:
Survivors:
No
Schedule:
Tulsa - Dallas
MSN:
0184
YOM:
1970
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
1
Captain / Total flying hours:
3850
Captain / Total hours on type:
1400.00
Circumstances:
The pilots of Mitsubishi MU-2, N106MA, and a Cessna 310 with no registration number elected to fly in formation at night, though neither pilot had formal training in formation flying nor experience in night formation. They joined up in flight and the MU-2 pilot was flying on the wing of the Cessna 310. The MU-2 pilot communicated that he was going to change positions from the right side to the left side of the 310C. The Cessna 310 pilot and his passenger lost sight of the MU-2 when it dropped back to a position in the rear of the Cessna 310. Soon thereafter, the two aircraft collided and the MU-2 went out of control and crashed. The right horizontal stabilizer was torn from the Cessna 310 and the 310's empennage, right wing and props were damaged, but it was landed without injury to its occupants. An investigation revealed the tail light of the Cessna 310 was inoperative. Sole on board, the pilot was killed.
Probable cause:
Improper planning/decision by the pilots of both aircraft, and the mitsubishi pilot's misjudgment of his position, while attempting to fly formation at night with an aircraft that did not have all navigation lights operative. Factors related to the accident were: both pilot's lack of training in the type of operation, darkness, inoperative navigation (tail) light on the Cessna 310, and the lack of visual perception that would have been available to the mitsubishi pilot.
Final Report:

Crash of a Mitsubishi MU-2B-60 Marquise in Tulsa: 3 killed

Date & Time: Feb 22, 1991 at 1519 LT
Type of aircraft:
Registration:
N274MA
Flight Phase:
Flight Type:
Survivors:
No
Schedule:
Tulsa - Tulsa
MSN:
786
YOM:
1980
Location:
Crew on board:
2
Crew fatalities:
Pax on board:
1
Pax fatalities:
Other fatalities:
Total fatalities:
3
Captain / Total flying hours:
4910
Captain / Total hours on type:
445.00
Aircraft flight hours:
6094
Circumstances:
Airplane was departing on a required maintenance test flight following replacement of both engines. Witnesses stated that the takeoff roll and initial climb appeared normal, but that at about 500 feet agl, the airplane entered a right bank which continued until the wings were vertical and the nose fell through. Airplane impacted in an inverted steep nose down attitude. Examination of wreckage revealed that the right engine had been secured and feathered. Subsequent investigation did not reveal any evidence of pre-impact failure or malfunction of either engine or any of the airframe systems. Engine mounting/rigging continuity could not be established due to impact damage. The pilot was a principal in the operator's organization and not one of the regular line pilots. Evidence indicated that the gear was up and that the left spoiler was deployed at impact. Emerg procedure taught in transition training is to use rudder trim as soon as possible after engine failure to preclude deployment of spoilers. Rudder trim found in neutral position. All three occupants were killed.
Probable cause:
The shutdown of one engine for undetermined reasons, and the pilot's failure to maintain VMCA during a critical phase of flight. A factor in the accident was the pilot's improper emergency procedure.
Final Report:

Crash of a Cessna 421B Golden Eagle II in Muskogee: 6 killed

Date & Time: Jan 5, 1991 at 2043 LT
Registration:
N421H
Flight Phase:
Flight Type:
Survivors:
No
Schedule:
Muskogee - Albuquerque
MSN:
421B-0516
YOM:
1973
Crew on board:
1
Crew fatalities:
Pax on board:
5
Pax fatalities:
Other fatalities:
Total fatalities:
6
Captain / Total flying hours:
1820
Captain / Total hours on type:
684.00
Aircraft flight hours:
2580
Circumstances:
A pilot (whose instrument currency could not be determined) took off at night in IMC. Shortly after takeoff, the aircraft crashed about 1.5 mile from the departure end of the runway. There was evidence that it impacted in an 85° right bank, nose down attitude at high speed. No preimpact part failure was found during the investigation; however, during a pre-purchase inspection on 10/16/90, several discrepancies were noted. These included an inop flight director, an autopilot malfunction and a misrigged flight control system that allowed the control wheel to indicate a left turn when the aircraft was in level flight. There was no record of these being repaired. Records showed the pitot-static system was last tested on 3/24/88. The pilot was taking sine-aid and tylenol for a chronic sinus infection. Although tox checks indicated the presence of 50.7 ug/ml of pseudoephedrine and 36.4 ug/ml of acetaminophen in the pilot's urine, none was found in his blood. The sinus cond could have affected the pilot's balance and equilibrium. All six occupants were killed.
Probable cause:
The pilot's failure to maintain control of the aircraft, due to spatial disorientation. Factors related to the accident were: darkness, adverse weather conditions, and the pilot's physical impairment from the chronic sinus infection.
Final Report:

Crash of a Northrop YC-125B Raider in Tulsa

Date & Time: Jun 29, 1988 at 0625 LT
Type of aircraft:
Registration:
N3756Q
Flight Phase:
Flight Type:
Survivors:
Yes
Schedule:
Tulsa - Dayton
MSN:
2518
Location:
Crew on board:
2
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
6274
Captain / Total hours on type:
56.00
Circumstances:
The pilot did not hold a type rating or written authorization to act as pilot in command. The copilot did not hold a type rating or written authorization to act as second in command and his medical had expired. The aircraft did not have an airworthiness certificate nor had a special flight permit been issued. The left propeller went into reverse during the initial climb due to corrosion and deterioration of the wiring that controlled the propeller. The aircraft crashed out of control after colliding with power lines during takeoff. It struck the ground and went through a fence then down a slope and over an embankment. The aircraft then bounced across a street while turning around and colliding with a power line pole tail first. The aircraft had traveled about 537 feet from initial ground contact. All 3 engines were still producing power when the aircraft came to rest. Both occupants escaped uninjured.
Probable cause:
Occurrence #1: airframe/component/system failure/malfunction
Phase of operation: takeoff - initial climb
Findings
1. (c) electrical system - corroded
2. (f) inadeq substantiation process, inadequate documentation - company/operator mgmt
3. (c) electrical system - deteriorated
4. (c) propeller system/accessories,reversing system - engaged
5. (c) procedures/directives - disregarded - pilot in command
6. (c) operation with known deficiencies in equipment - attempted - pilot in command
7. (f) lack of total experience in type of aircraft - pilot in command
8. (f) lack of total experience in type of aircraft - copilot/second pilot
----------
Occurrence #2: forced landing
Phase of operation: descent - emergency
----------
Occurrence #3: in flight collision with terrain/water
Phase of operation: descent - uncontrolled
Final Report:

Crash of an Embraer EMB-110P1 Bandeirante in Lawton

Date & Time: May 24, 1988 at 1454 LT
Operator:
Registration:
N65DA
Flight Phase:
Survivors:
Yes
Schedule:
Lawton - Dallas
MSN:
110-389
YOM:
1982
Crew on board:
2
Crew fatalities:
Pax on board:
6
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
2333
Captain / Total hours on type:
483.00
Aircraft flight hours:
13005
Circumstances:
The number one (left) engine failed during the takeoff from runway 35. It was reported that the aircraft yawed sharply left and climbed to between 50 and 100 feet agl before it began losing altitude. The aircraft struck the ground and continued to move forward on the ground several hundred feet until it struck the airport perimeter fence. The aircraft came to rest 1,600 feet west of the runway, on a heading of 290°. A post-crash fire destroyed the cargo area of the aircraft. Examination of the left engine revealed a compressor turbine blade airfoil separation. Disassembly of the propeller on the left engine indicated that the propeller had autofeathered normally after the engine failed. The captain reportedly made the takeoff. All eight occupants were injured, two seriously. The aircraft was damaged beyond repair.
Probable cause:
Occurrence #1: loss of engine power (total) - mech failure/malf
Phase of operation: takeoff - initial climb
Findings
1. 1 engine
2. (f) compressor assembly, blade - previous damage
3. (f) compressor assembly, blade - overtemperature
4. (f) compressor assembly, blade - separation
5. Propeller feathering - performed
----------
Occurrence #2: in flight collision with terrain/water
Phase of operation: takeoff - initial climb
Findings
6. (c) emergency procedure - improper - pilot in command
7. (c) directional control - not maintained - pilot in command
8. Object - fence
Final Report:

Crash of a Convair CV-640 in Bartlesville

Date & Time: Oct 28, 1987 at 0734 LT
Type of aircraft:
Operator:
Registration:
N3411
Flight Type:
Survivors:
Yes
Schedule:
Chicago - Oklahoma City
MSN:
31
YOM:
1966
Crew on board:
2
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
5389
Captain / Total hours on type:
2480.00
Aircraft flight hours:
44764
Circumstances:
The captain was cross-feeding both engines from the right tank while the first officer (f/o) was flying, without informing the f/o. The captain then left the cockpit while cross-feeding. Both tank valves and the right boost pump were on. The right tank ran dry, the right engine failed, and the prop autofeathered while the captain was absent. The captain returned, turned on the left boost pump, but left the right boost pump and the valves open, and attempted to restart the right engine. The left engine then failed but this was not recognized by the crew. The electrical system failed due to the attempted restarts and the fact that nonessential equipment was not turned off. The captain did not apply sufficient pull to the emergency gear handle to lower the gear manually. The aircraft was landed on a short wet sod runway, with the gear and flaps up, at a high rate of speed. The aircraft ran off the end of the runway, through a ditch, across a road, and into trees. Both pilots escaped uninjured.
Probable cause:
Occurrence #1: loss of engine power (total) - nonmechanical
Phase of operation: cruise - normal
Findings
1. (c) 1 engine
2. Fluid, fuel - starvation
3. (c) fuel tank selector position - inattentive - pilot in command
4. (c) crew/group coordination - improper - pilot in command
5. (f) in-flight planning/decision - improper - pilot in command
----------
Occurrence #2: loss of engine power (total) - nonmechanical
Phase of operation: cruise - normal
Findings
6. (c) all engines
7. (c) fluid, fuel - starvation
8. (c) emergency procedure - improper - pilot in command
9. (f) checklist - inadequate - company/operator management
----------
Occurrence #3: forced landing
Phase of operation: descent - emergency
Findings
10. Airspeed - excessive - copilot/second pilot
----------
Occurrence #4: gear not extended
Phase of operation: landing
Findings
11. (c) gear extension - improper use of - pilot in command
12. (f) electrical system - deteriorated
----------
Occurrence #5: on ground/water collision with object
Phase of operation: landing
Findings
13. (f) terrain condition - ditch
Final Report:

Crash of a Boeing KC-135A-BN Stratotanker at Altus AFB

Date & Time: Feb 13, 1987
Type of aircraft:
Operator:
Registration:
60-0330
Flight Type:
Survivors:
Yes
Schedule:
Altus AFB - Altus AFB
MSN:
18105
YOM:
1961
Crew on board:
7
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Aircraft flight hours:
10305
Circumstances:
The crew was performing a local training mission at Altus AFB. After landing, smoke spread in the cockpit and a fire erupted. The crew immediately stopped the aircraft and the runway and evacuated the cabin safely. There were no injuries while the aircraft was totally destroyed by fire.
Probable cause:
It was determined that UHF cables which runs near the aft wing root in the fuselage were melted due to an electrical fault. Fuel vapors in the area of the aft body tank ignited.

Crash of a Beechcraft H18 in Oklahoma City: 2 killed

Date & Time: Nov 5, 1985 at 1511 LT
Type of aircraft:
Operator:
Registration:
N1461G
Flight Phase:
Flight Type:
Survivors:
No
Schedule:
Oklahoma City - Lawton
MSN:
BA-637
YOM:
1962
Crew on board:
2
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
2
Captain / Total flying hours:
16000
Captain / Total hours on type:
3000.00
Aircraft flight hours:
9660
Circumstances:
Atr pilot departing airport under VMC experienced failure of the right engine shortly after lift-off. The aircraft yawed right followed by a steep right roll, contacting power lines with the right wing and subsequently impacted the ground. A post-crash fire destroyed the aircraft with the exception of both engines and a portion of the right wing panel. The engine failed due to lack of lubrication to the impeller shaft caused by blockage of oil jet due to fod. Oil line from scavenge sump to scavenge pump inlet had been replaced prior to accident. The aircraft had experienced maintenance problem (oil leak) approximately 2 weeks prior to accident. Source of fod is undetermined. Both occupants were killed.
Probable cause:
Occurrence #1: loss of engine power (partial) - mech failure/malf
Phase of operation: takeoff - initial climb
Findings
1. Fluid, oil - starvation
2. Engine assembly - failure, total
3. (c) maintenance - improper - other maintenance personnel
----------
Occurrence #2: loss of control - in flight
Phase of operation: takeoff - initial climb
Findings
4. (c) directional control - not maintained - pilot in command
----------
Occurrence #3: in flight collision with terrain/water
Phase of operation: descent - uncontrolled
Final Report:

Crash of a Douglas A-26B Invader in Lawton

Date & Time: Mar 17, 1985 at 1635 LT
Type of aircraft:
Registration:
N142ER
Flight Phase:
Flight Type:
Survivors:
Yes
Schedule:
Ada - Frederick
MSN:
6928
YOM:
1941
Crew on board:
3
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
5395
Captain / Total hours on type:
158.00
Circumstances:
An intermittent fire in the left engine accessory section led to loss of fuel to the engine. The right engine ingested water and quit. The landing gear had been left pinned in the down position because of a malfunction reported on the previous flight. Neither propeller was feathered, but the resulting high rate of descent led to a forced landing before the left tank blew up and the wing burned off. The aircraft was destroyed by fire after all three occupants escaped without serious injury. The aircraft was being ferried to another facility for restoration.
Probable cause:
Occurrence #1: miscellaneous/other
Phase of operation: standing - pre-flight
Findings
1. (c) maintenance, inspection - inadequate - company maintenance personnel
2. (f) preflight planning/preparation - inadequate - pilot in command
3. (f) operation with known deficiencies in equipment - intentional - pilot in command
----------
Occurrence #2: fire
Phase of operation: cruise - normal
Findings
4. (c) accessory drive assy - fire
----------
Occurrence #3: loss of engine power (total) - nonmechanical
Phase of operation: descent - emergency
Findings
5. (c) fluid,fuel - water
----------
Occurrence #4: forced landing
Phase of operation: descent - emergency
----------
Occurrence #5: forced landing
Phase of operation: landing
Findings
6. Engine assembly - fire
7. Nacelle/pylon - fire
8. Wing - fire
9. Horizontal stabilizer surface - fire
10. Landing gear - overload
Final Report:

Crash of a Cessna 402B in Altus: 2 killed

Date & Time: Feb 6, 1985 at 0943 LT
Type of aircraft:
Operator:
Registration:
N5780M
Flight Phase:
Survivors:
No
Schedule:
Altus - Oklahoma City
MSN:
402B-0358
YOM:
1973
Location:
Crew on board:
1
Crew fatalities:
Pax on board:
1
Pax fatalities:
Other fatalities:
Total fatalities:
2
Captain / Total flying hours:
4227
Captain / Total hours on type:
643.00
Aircraft flight hours:
6100
Circumstances:
During an engine start, prior to the flight, the left engine backfired 2 or 3 times. A witness described the 1st backfired as 'the loudest I have ever heard.' When the aircraft took off, two persons living near the departure end of the runway noted that the aircraft (believed to be the same) sounded different and had a 'cluttering sound'. While climbing, the pilot declared an emergency and reported a fire in the left engine. He was vectored toward Altus AFB while descending in IFR conditions. He descended into VFR conditions and saw the airport about 3 miles away. A witness saw smoke and fire trailing from the vicinity of the left engine. He stated that the aircraft's nose came up, the plane rolled to the left, then it entered a steep, nose down, inverted attitude just before it crashed and burned. An exam revealed the engine exhaust manifold header assy had failed and allowed hot exhaust gases to escape in the engine nacelle in the vicinity of fuel and oil lines. Corrosion had progressed thru the header assy. Ad 75-23-08 requested general inspection, but contained note 'do not remove clamps.' No record of replacement in 6,100 hours. Both occupants were killed.
Probable cause:
Occurrence #1: airframe/component/system failure/malfunction
Phase of operation: unknown
Findings
1. (c) exhaust system, manifold/pipe - corroded
2. (c) maintenance, inspection - inadequate
3. (f) procedure inadequate - manufacturer
4. (f) inadequate surveillance of operation - faa (organization)
5. (c) exhaust system, manifold/pipe - failure,total
6. (c) exhaust system, manifold/pipe - leak
----------
Occurrence #2: fire
Phase of operation: climb - to cruise
Findings
7. (c) miscellaneous - fire
----------
Occurrence #3: loss of control - in flight
Phase of operation: approach - vfr pattern - final approach
Findings
8. (c) reason for occurrence undetermined
9. (f) weather condition - clouds
10. Initiated - pilot in command
11. Precautionary landing - attempted - pilot in command
12. Aircraft handling - not maintained
----------
Occurrence #4: in flight collision with terrain/water
Phase of operation: descent - uncontrolled
Final Report: