Crash of a Douglas DC-8-12 in Denver: 18 killed

Date & Time: Jul 11, 1961 at 1136 LT
Type of aircraft:
Operator:
Registration:
N8040U
Survivors:
Yes
Schedule:
Philadelphia – Chicago – Omaha – Denver
MSN:
45307
YOM:
1961
Flight number:
UA859
Crew on board:
7
Crew fatalities:
Pax on board:
115
Pax fatalities:
Other fatalities:
Total fatalities:
18
Captain / Total flying hours:
17631
Captain / Total hours on type:
168.00
Copilot / Total flying hours:
9839
Aircraft flight hours:
124
Circumstances:
On July 11, 1961, at 1136 M.S.T., a United Air Lines DC-8 crashed during its landing roll at Stapleton Airfield, Denver, Colorado. None of the 122 occupants was severely injured as an immediate result of the impact; however, there were 16 passenger fatalities as a result of carbon monoxide poisoning when the aircraft burned. One other passenger, an elderly woman, broke both ankles during evacuation of the airplane and later succumbed to shock. In addition, the driver of a panel truck, which the aircraft struck after leaving the runway, also suffered fatal injuries. After experiencing hydraulic difficulties following takeoff from Omaha, Nebraska, the crew of N8040U continued the flight to Denver, using procedures set forth in the flight manual for abnormal hydraulic situations. When the flight arrived in the Denver area, preparations were made for landing. The ejectors were extended hydraulically, however, when an attempt was made to extend flaps to 25 degrees the hydraulic pressure dropped to zero. The hydraulic system selector was then placed in the No. 3 position (flap and gear downlock), and the approach was continued. After touchdown, the throttles were placed in the idle reverse thrust position and when power was applied, an uncontrollable deviation from the runway occurred.
Probable cause:
The Board determines the probable cause of this accident was the asymmetric thrust which, during hydraulic emergency, resulted from the failure of the thrust reversers on engines Nos. 1 and 2 when reverse thrust was selected. A contributing factor was the failure of the first officer to monitor the thrust reverse indicator lights when applying reverse thrust.
Final Report:

Crash of a Douglas DC-8-11 in New York: 90 killed

Date & Time: Dec 16, 1960 at 1033 LT
Type of aircraft:
Operator:
Registration:
N8013U
Survivors:
No
Site:
Schedule:
Chicago – New York
MSN:
45290
YOM:
1959
Flight number:
UA826
Crew on board:
7
Crew fatalities:
Pax on board:
77
Pax fatalities:
Other fatalities:
Total fatalities:
90
Captain / Total flying hours:
19100
Captain / Total hours on type:
344.00
Copilot / Total flying hours:
8500
Copilot / Total hours on type:
379
Aircraft flight hours:
2434
Circumstances:
On December 16, 1960, at 1033 e.s.t., a collision between Trans World Airlines Model 1049A Constellation, N 6907C, and a United Air Lines DC-8, N 8013U, occurred near Miller Army Air Field, Staten Island, New York. Trans World Airlines Flight 266 originated at Dayton, Ohio. The destination was LaGuardia Airport, New York, with one en route stop at Columbus, Ohio United Air Lines Flight 826 was a non-stop service originating at O'Hare Airport, Chicago, Illinois, with its destination New York International Airport, New York. Both aircraft were operating under Instrument Flight Rules. Following the collision the Constellation fell on Miller Army Field, and the DC-8 continued in a northeasterly direction, crashing into Sterling place near Seventh Avenue in Brooklyn, New York. Both aircraft were totally destroyed. All 128 occupants of both aircraft and 6 persons on the ground in Brooklyn were fatally injured. There was considerable damage to property in the area of the ground impact of the DC-8. TWA Flight 266 departed Port Columbus Airport at 0900, operating routinely under Air Traffic Control into the New York area The New York Air Route Traffic Control Center (ARTCC) subsequently advised that radar contact had been established and cleared the flight to the Linden. Intersection, Control of the flight was subsequently transferred to LaGuardia Approach Control. When the flight was about over the Linden Intersection, LaGuardia Approach Control began vectoring TWA 266 by radar to the final approach course for a landing on runway 4 at LaGuardia. Shortly thereafter TWA 266 was cleared to descend to 5,000 feet, and was twice advised of traffic in the vicinity on a northeasterly heading. Following the transmission of this information the radar targets appeared to merge on the LaGuardia Approach Control radar scope, and communications with TWA 266 were lost.United Air Lines Flight 826 operated routinely between Chicago and the New York area, contacting the New York ARTCC at 1012 Shortly thereafter the New York Center cleared UAL 826 to proceed from the Allentown, Pa., very high frequency omni directional radio range station (VOR) direct to the Robbinsville, New Jersey, VOR, and thence to the Preston Intersection via Victor Airway 123. At approximately 1021, UAL 826 contacted Aeronautical Radio, Inc. (ARINC) to advise their company that the No. 2 receiver accessory unit was inoperative, which would indicate that one of the aircraft's two VHF radio navigational receivers was not functioning. A "fix" is established by the intersection of two radials from two separate radio range stations. With one unit inoperative the cross-bearings necessary can be taken by tuning the remaining receiver from one station to the other. This process consumes considerable time, however, and is not as accurate as the simultaneous display of information on two separate position deviation indicators While UAL 826 advised the company that one unit was inoperative, Air Traffic Control was not advised. At 1025 the New York ARTCC issued a clearance for a new routing which shortened the distance to Preston by approximately 11 miles. As a result, this reduced the amount of time available to the crew to retune the single radio receiver to either the Colt' s Neck, New Jersey, or Solberg, New Jersey, VOR in order to establish the cross-bearing with Victor 123, which would identify the Preston Intersection. In the event the crew would not attempt to retune the single VOR receiver, crossbearings on the Scotland Low Frequency Radiobeacon could be taken with the aircraft direction finding (ADF) equipment. This would be a means of identifying the Preston Intersection but, under the circumstances, would require rapid mental calculation in the interpretation of a display which could be easily misread. Several factors support the conclusion that this occurred. Instructions had been issued to UAL 826 for holding at the Preston Intersection the clearance limit, should holding be necessary. Clearance beyond Preston for an approach to Idlewild Airport would be received from Idlewild Approach Control and the transfer of control of the flight from the New York Center to Idlewild Approach Control would normally take place as the aircraft was approaching Preston. UAL 826 was not receiving radar vectors, but was providing its own navigation. After the flight reported passing through 6,000 feet the New York Center advised that radar service was terminated and instructed the flight to contact Idlewild Approach Control. UAL 826 then called Idlewild Approach Control, stating "United 826 approaching Preston at 5,000." This was the last known transmission from UAL 826. At the time UAL 826 advised it was approaching Preston it had in fact gone on by this clearance limit several seconds before and was several miles past the point at which it should have turned into the holding pattern. This is confirmed by the data obtained from the flight recorder which had been installed in the UAL DC-8, as well as by analysis of the communication tapes At a point approximately 11 miles past the Preston Intersection a collision occurred between TWA 266 and UAL 826. Weather at the altitude of the collision and at the time of the accident was such as to preclude flight by visual means.
Probable cause:
The Board determines that the probable cause of this accident was that United Flight 826 proceeded beyond its clearance limit and the confines of the airspace allocated to the flight by Air Traffic Control A contributing factor was the high rate of speed of the United DC-8 as it approached the Preston intersection, coupled with the change of clearance which reduced the enroute distance along VICTOR 123 by approximately 11 miles.
Final Report:

Crash of a Douglas DC-7 near Las Vegas: 47 killed

Date & Time: Apr 21, 1958 at 0830 LT
Type of aircraft:
Operator:
Registration:
N6328C
Flight Phase:
Survivors:
No
Site:
Schedule:
Los Angeles – Denver – New York
MSN:
45142
YOM:
1956
Flight number:
UA736
Crew on board:
5
Crew fatalities:
Pax on board:
42
Pax fatalities:
Other fatalities:
Total fatalities:
47
Circumstances:
United Airlines Flight 736 departed Los Angeles International Airport at 0737 hours Pacific standard time with 42 passengers and 5 crew aboard. It was a scheduled passenger flight to New York, which was proceeding normally in accordance with an IFR flight plan along Victor Airway 16 to Ontario, California, and Victor Airway 8 to Denver. The aircraft was cleared to a cruising altitude of 21 000 ft msl and advised to climb in VFR weather conditions. At 0735 the flight reported to Aeronautical Radio that it was over Ontario at 12 000 ft and was climbing in VFR conditions. Then at 081 1 it reported over Daggett at its cruising altitude of 21 000 ft and estimated that it would reach Las Vegas (omni range station) at 0831, This was the last position report made by the flight. At approximately 0745 hours that morning F-100F, 56-3755, took off from Nellis Air Force Base, Las Vegas, Nevada on an instrument training flight carrying an instructor and a trainee pilot. The flight was in accordance with a VFR local flight plan filed with Nellis Operations and the local traffic control tower. At approximately 0823, 755 called Nellis VFR Control and reported that it was "inbound on KRAM" ( a local commercial radio broadcast station). The flight requested an altitude assignment from which it would conduct a simulated ADF instrument jet penetration utilizing KRAM. The VFR controller assigned 755, 28 000 ft and advised it to report over the radio station. At approximately 0828, the flight reported that it was over KRAM requesting a penetration. The VFR controller cleared it for an immediate penetration and requested that it report the penetration turn. 755 then reported leaving 28 000 ft. There were no &her reports from the flight in connection with this procedure. At 0830 the offices of Aeronautical Radio at Los Angeles, Denver and Salt Lake City heard an emergency message from the United flight.. . . . " United 736, Mayday, midair collision, over Las Vegas. " At the same time, as nearly as can be determined, there was an unrecorded emergency transmission from the F-1 00F. This message was heard by the VFR controller and by the two pilots of another F-100F. All were agreed that the first portion of the emergency transmission was "Mayday, Mayday, this is 755. " The last part of the message was either, "We've had a flameout" or 'We're bailing out." The aircraft collided at 21 000 ft over a position later determined to be about 9 miles southwest of the Las Vegas VOR station, on Victor Airway 8, approximately 1-3/4 miles to the right (southeast) of the centerline. Both aircraft fell out of control and crashed killing the 47 persons on board the DC-7 and both pilots of the F-100F.
Probable cause:
The probable cause of this collision was a high rate of near head-on closure at high altitude; human and cockpit limitations; and the failure of Nellis Air Force Base and the Civil Aeronautics Administration to take every measure to reduce a known collision exposure.
Final Report:

Crash of a Douglas DC-7 in the Grand Canyon: 58 killed

Date & Time: Jun 30, 1956 at 1032 LT
Type of aircraft:
Operator:
Registration:
N6324C
Flight Phase:
Survivors:
No
Site:
Schedule:
Los Angeles – Chicago – New York
MSN:
44288
YOM:
1955
Flight number:
UA718
Crew on board:
5
Crew fatalities:
Pax on board:
53
Pax fatalities:
Other fatalities:
Total fatalities:
58
Captain / Total flying hours:
16492
Captain / Total hours on type:
1238.00
Copilot / Total flying hours:
4540
Copilot / Total hours on type:
230
Aircraft flight hours:
5115
Circumstances:
United Air Lines Flight 718 was regularly scheduled from Los Angeles to Chicago, Illinois. On June 30, 1956, it took off from runway 25L (left) of the Los Angeles International Airport at 0904 (three minutes after TWA 2). Flight 718 was on an IFR flight plan to Chicago via Green Airway 5 Palm Springs inter-section, direct Needles, direct Painted Desert, direct Durango, direct Pueblo, direct St. Joseph. Victor Airway 116 Joliet, Victor Airway 84 Chicago Midway Airport. The flight plan proposed a .JPG"> airspeed of 288 knots., a cruising altitude of 21,000 feet, and a departure time of 0845. The flight crew consisted of Captain Robert F. Shirley, First Officer Robert W. Harms, Flight Engineer Gerard Flore, and Stewardesses Nancy L. Kemnitz and Margaret A. Shoudt. Flight preparations and dispatch of United 718 were routine and the aircraft departed with 3,850 gallons of fuel. The company load manifest showed the gross weight of the aircraft at takeoff to be 105,835 pounds, which was less than the maximum allowable of 114,060 pounds; the latter weight was restricted from a maximum of 122,200 pounds for the aircraft because of a landing limitation at Chicago. The load was properly distributed with respect to the center of gravity limitations of the aircraft. After takeoff the flight contacted the Los Angeles tower radar controller, who vectored it through the overcast over the same departure course as TWA 2. United 718 reported "on top" and changed to Los Angeles Center frequency for its en route clearance. This corresponded to the flight plan as filed; however, the controller specified that the climb to assigned altitude be in VER conditions. Flight 718 made position reports to Aeronautical Radio, Inc., which serves under contract as United company radio. It reported passing over Riverside and later over Palm Springs intersection. The latter report indicated that United 718 was still climbing to 21,000 and estimated it would reach Needles at 1000 and the Painted Desert at 1034. At approximately 0958 United 718 made a position report to the CAA communications station located at Needles. This report stated that the flight was over Needles at 0958, at 21,000 feet, and estimated the Painted Desert at 1031, with Durango next. At 1031 an unidentified radio transmission was heard by Aeronautical Radio communicators at Salt Lake City and San Francisco. They were not able to understand the message when it was received but it was later determined by playing back the recorded transmission that the message was from United 718. Context was interpreted as: "Salt Lake, United 718 . . . ah . . . we're going in."
Probable cause:
The Board determines that the probable cause of this mid-air collision was that the pilots did not see each other in time to avoid the collision. It is not possible to determine why the pilots did not see each other, but the evidence suggests that it resulted from any one or a combination of the following factors: Intervening clouds reducing time for visual separation, visual limitations due to cockpit visibility, and preoccupation with normal cockpit duties, preoccupation with matters unrelated to cockpit duties such as attempting to provide the passengers with a more scenic view of the Grand Canyon area, physiological limits to human vision reducing the time opportunity to see and avoid the other aircraft, or insufficiency of en route air traffic advisory information due to inadequacy of facilities and lack of personnel in air traffic control. The following findings were reported:
- Approaching Daggett, TWA 2 requested its company radio to obtain 21,000 feet as an assigned altitude, or 1,000 on top,
- Company radio requested 21,000 feet IFR from ARTC. This vas denied by ARTC. Request was then made for 1,000 on top. This was approved and clearance issued. The flight climbed to and proceeded at 21,000 feet,
- As an explanation for the denial of 21,000 feet, TWA 2 was furnished pertinent information on UA718,
- The last position report by each flight indicated it was at that time at 21,000, estimating the Painted Desert line of position at 1031,
- The Salt Lake controller possessed both position reports at approximately 1013, at which time both flights were in uncontrolled airspace,
- Traffic control services are not provided in the uncontrolled airspace and according to existing Air Traffic Control policies and procedures the Salt Lake controller was not required to issue traffic information; none was issued voluntarily,
- A general overcast with some breaks existed at 15,000 feet in the Grand Canyon area,
- Several cumulus buildups extending above flight level existed; one was nearly over Grand Canyon Village and others were north and northeast in the area of the collision,
- The collision occurred at approximately 1031 in visual flight rule weather conditions at about 21,000 feet,
- The collision in space was above a position a short distance west of the TWA wreckage area, 17 miles west of or approximately 3-1/2 minutes' flying time from the Painted Desert line of position,
- Under visual flight rule weather conditions it is the pilot's responsibility to maintain separation from other aircraft,
- At impact the aircraft relative to each other converged at an angle of about 25 degrees with the DC-7 to the right of the L-1049. The DC-7 was rolled about 20 degrees right wing down and pitched about 10 degrees nose down relative to the L-1049,
- There was no evidence found to indicate that malfunction or failure of the aircraft or their components was a factor in the accident.
Final Report:

Crash of a Douglas DC-6B near Longmont: 44 killed

Date & Time: Nov 1, 1955 at 1903 LT
Type of aircraft:
Operator:
Registration:
N37559
Flight Phase:
Survivors:
No
Schedule:
LaGuardia – Chicago – Denver – Portland – Seattle
MSN:
43538
YOM:
1952
Flight number:
UA629
Crew on board:
5
Crew fatalities:
Pax on board:
39
Pax fatalities:
Other fatalities:
Total fatalities:
44
Captain / Total flying hours:
10086
Captain / Total hours on type:
703.00
Copilot / Total flying hours:
3578
Copilot / Total hours on type:
1062
Aircraft flight hours:
11949
Circumstances:
After a routine radio ramp check, Flight 629 taxied to runway 08R (80 degrees, right) and at 1844 the flight was in runup position where it was given ATC clearance for the flight to Portland, the first intended landing. The clearance, in part, included compulsory radio reports from the flight upon passing the Denver Omni and when climbing through 18,000 feet to its assigned flight altitude, 21,000 feet. Following takeoff the flight reported its "off time" to the company as 1852 and thereafter reported passing the Denver Omni at 1856. The latter communication was the last from the flight. About 1903 the Denver tower controllers saw two white lights, one brighter than the other, appear in the sky north-northwest of the airport and fall to the ground. Both lights were observed 30-45 seconds and seemed to fall with approximately the same speed. There was then a momentary flash originating at or near the ground which illuminated the base of the clouds, approximately 10,000 feet above. When the controllers observed the lights they initiated action to determine if any aircraft were in distress. Radio calls were made to all aircraft in the Denver area of responsibility and all except flight 629 were accounted for. It was soon learned that the flight had crashed and all 44 occupants had been killed. It was later confirmed that the disintegration of the aircraft in the air was caused by a bomb. Two weeks later, on November 15, investigators confirmed that an explosive device has been placed on board by John Gilbert Graham aged 23 who signed a US$ 37,500 life-insurance for his mother who was on board. Convicted guilty for murder and terrorism, he was sentenced to death penalty and executed on January 11, 1956.
Probable cause:
The Board determines that the probable cause of this accident was the disintegrating force of a dynamite bomb explosion which occurred in the number 4 baggage compartment. The following findings were reported:
- At 1903, eleven minutes after departure, an in-flight disintegrating explosion occurred aboard Flight 629,
- The aircraft was climbing normally and was on course when the explosion occurred,
- Physical evidence showed conclusively the explosion took place in the number 4 baggage compartment of the aircraft,
- The violence of the explosion and the physical evidence proved the explosion was not caused by any system or component of the aircraft,
- Physical evidence at the scene and laboratory tests confirmed that the explosive material was dynamite, in the form of a bomb,
- There was no evidence found to indicate malfunction or failure of the aircraft or its components prior to the explosion.
Final Report:

Crash of a Douglas DC-4 on Medicine Bow Peak: 66 killed

Date & Time: Oct 6, 1955 at 0726 LT
Type of aircraft:
Operator:
Registration:
N30062
Flight Phase:
Survivors:
No
Site:
Schedule:
New York – Chicago – Denver – Salt Lake City – San Francisco
MSN:
18389
YOM:
1944
Flight number:
UA409
Crew on board:
3
Crew fatalities:
Pax on board:
63
Pax fatalities:
Other fatalities:
Total fatalities:
66
Captain / Total flying hours:
9807
Captain / Total hours on type:
2289.00
Copilot / Total flying hours:
2418
Copilot / Total hours on type:
343
Aircraft flight hours:
28755
Circumstances:
Flight 409 originated at New York, New York, on October 5, 1955, destination San Francisco, California, with intermediate stops including Chicago, Illinois, Denver, Colorado, and Salt Lake City, Utah. The trip to Denver was routine except for traffic delays, caused principally by weather, and the flight arrived there at 0551, October 6, one hour and 11 minutes late. Routine crew changes were made at Chicago and Denver, the last crew consisting of 'Captain Clinton C. Cooks, Jr., First Officer Ralph D. Salisbury, Jr., and Stewardess Patricia D. Shuttleworth. No discrepancies were reported by the former crew and none were found at Denver. While at Denver the aircraft was refueled to a total of 1,000 gallons of gasoline. Prior to departure Captain Cooke was briefed by the company's dispatcher on the en route weather, based on both U. S. Weather Bureau sequence reports and forecasts and the company meteorologist's forecasts and analysis. Following this briefing the flight me dispatched to Salt Lake City via airways V-4, V-118, V-6, and V-32, to cruise at 10,000 feet, and to fly in accordance with Visual Right Rules (VFR). The estimated time en route was two hours and 33 minutes. The only obligatory reporting point along the route was Rock Springs, Wyoming. The flight departed Denver at 0633, with 63 passengers, including two infants. At takeoff, the gross weight of the aircraft was 64,147 pounds, 653 pounds under the allowable weight of 64,800 pounds; an error of 100 pounds in excess of the allowable rear baggage compartment weight 2 was made in loading. Flight 409 reported its time off to the company and this was the last known radio contact with the flight. When the flight failed to report at Rock Springs at 0811, its estimated reporting time, repeated efforts were wade to establish radio contact with it. These were unsuccessful and the company then declared an emergency. A widespread search was immediately coordinated by Air Search and Rescue, which included the Wyoming Air National Guard, the Civil Air Patrol, and United Air Lines. At approximately 1140 the same day the wreckage was sighted near Medicine Bow Peak, 33 miles west of Laramie, Wyoming. The Laramie weather at 0728 was; Scattered clouds, 5,500 feet; visibility 40 miles; wind west-northwest 13 knots; snow showers of unknown intensity over the mountains. The aircraft struck the almost vertical rock cliff of the east slope of Medicine Bow Peak (elevation 12,005 feet) located in the Medicine Bow Mountains. The crash occurred at an elevation of 11,570 feet, 60 feet below the top of that portion of the mountain directly above it. Two large smudge marks were apparent on the face of the mountain. In these marks were four scars, evenly spaced and in a horizontal line, the result of the engines and propellers of the aircraft striking the cliff. At impact the aircraft disintegrated and the wreckage me strewn over a wide area. Some parts were thrown to the mountain top above the crash site, others rested on ledges at various levels, and the remainder fell to the elope below. All 66 occupants have been killed.
Probable cause:
The Board determines that the probable cause of this accident was the action of the pilot in deviating from the planned route for reasons unknown. The following findings were reported:
- The weather along the prescribed route was good and the aircraft could have been flown safely at an altitude of 10,000 feet,
- The pilot deviated from the planned route,
- The aircraft was observed flying in and out of clouds at an approximate altitude of 10,000 feet, 10 miles southeast of the accident scene and 21 miles west of the prescribed course,
- The aircraft struck the mountain peak at an altitude of 11,570 feet,
- Examination of the recovered sections of the aircraft failed to indicate any fire, structural failure, or malfunctioning of the aircraft or its components prior to impact.
Final Report:

Crash of a Douglas DC-6 in Ronkonkoma: 3 killed

Date & Time: Apr 4, 1955 at 1555 LT
Type of aircraft:
Operator:
Registration:
N37512
Flight Phase:
Flight Type:
Survivors:
No
Schedule:
New York-Idlewild – Ronkonkoma – LaGuardia
MSN:
43001
YOM:
1947
Crew on board:
3
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
3
Captain / Total flying hours:
9763
Captain / Total hours on type:
549.00
Copilot / Total flying hours:
9018
Copilot / Total hours on type:
1156
Aircraft flight hours:
22068
Circumstances:
N37512, under the command of Captain S. C. Hoyt, UAL New York area flight manager, departed New York International Airport at 1428 on a Visual Flight Rules flight plan for an estimated two-hour flight in the vicinity of MacArthur Field, Islip. The aircraft was properly dispatched on a routine check flight, and Captains V. H. Webb and H. M. Dozier were aboard for the purpose of receiving their periodic instrument proficiency check. Upon completion of the checks, the flight was scheduled to return to LaGuardia Airport. At 1501 the flight reported to the company by radio that they were “doing air work around Hempstead.” Another message was received by the company at 1527 reporting that the flight was going to make an ILS (Instrument Landing System) approach at Islip (MacArthur Field). Shortly thereafter, the flight contacted the MacArthur tower, requesting approval for an ILS approach and landing. Permission was granted by the tower, and a normal landing was made on runway 32. The aircraft was taxied to the intersection of runways 28 and 32 and the crew prepared for takeoff. The 1532 MacArthur weather observation showed scattered clouds at 20,000 feet, broken clouds at 25,000; visibility over 15 miles; temperature 53; dew-point 30; wind NNW at 20 knots, gusts to 30 knots. When the flight departed New York International Airport, weather was approximately the same and the forecast for the New York area indicated that it would be similar over the area for the duration of the flight. At 1548, the MacArthur controller cleared the flight to take position on runway 32 and take off. The aircraft took position on the runway but did not immediately take off, hence a second takeoff clearance was transmitted at 1550. The gross weight of the aircraft at takeoff from MacArthur Field was approximately 61,050 pounds, which was well below the maximum allowable. The load was correctly distributed with respect to center of gravity limits. The aircraft became airborne approximately, 1,500 to 1,800 feet down the runway. The takeoff appeared normal, as did the initial portion of the climb, and the aircraft remained on the runway heading. When about 50 feet high, the right wing lowered and the aircraft started turning to the right, at which time the landing gear was retracting. The aircraft continued a climbing turn and the degree of bank increased to approximately vertical by the time the heading changed about 90 degrees and the aircraft had attained an estimated altitude of 150 feet. The nose dropped sharply and the aircraft dived into the ground, striking on the right wing and nose. It then cartwheeled and came to rest right side up. An intense fire started and consumed a large portion of the wreckage in spite of the prompt arrival of fire fighting equipment on the field.
Probable cause:
The Board determines that the probable cause of this accident was unintentional movement of No. 4 throttle into the reverse range just before breaking ground, with the other three engines operating at high power output, which resulted in the aircraft very quickly becoming uncontrollable once airborne. The following findings were reported:
- No evidence of failure or malfunctioning of the structure powerplants, propellers, or electrical system was found,
- In reducing power to zero thrust during an instrument takeoff with a simulated engine out, No. 4 propeller was unintentionally reversed before the aircraft became airborne,
- Evidence indicated that No. 4 throttle was moved out of reverse by the pilot into the forward position in an attempt to unreverse, but the reverse warning flag was not lifted, resulting in increased reverse thrust,
- An outboard propeller on a DC-6 reversing as the aircraft becomes airborne, in conjunction with high power output of the other three engines, at takeoff configuration and airspeed causes the aircraft to become almost immediately uncontrollable,
- There was insufficient time and altitude for any pilot corrective measures to become effective.
Final Report:

Crash of a Convair CV-340-13 near Dexter

Date & Time: Jan 19, 1955 at 1625 LT
Type of aircraft:
Operator:
Registration:
N73154
Flight Phase:
Survivors:
Yes
Schedule:
Newark – Allentown – Youngstown – Akron – Cleveland – Chicago – Moline – Iowa City – Des Moines – Omaha – Lincoln
MSN:
180
YOM:
1954
Flight number:
UA329
Location:
Crew on board:
3
Crew fatalities:
Pax on board:
36
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
7578
Captain / Total hours on type:
750.00
Copilot / Total flying hours:
2123
Copilot / Total hours on type:
1147
Aircraft flight hours:
1502
Circumstances:
Flight 329 departed Des Moines on a VFR (Visual Flight Reed) night plan at 1608 for Omaha, Nebraska. The gross weight of the aircraft was 45,215 pounds 1,685 pounds less than the allowable 46,900 pounds. According to company records, the load was properly distributed with respect to the canter of gravity of the aircraft. The climb to 5,000 feet was uneventful but at that altitude the crew noticed vibration and a slight fore-and-aft movement of the control column. The climb was continued to 6,000 feet, where the aircraft was leveled off and power was reduced. As the vibration was still present at this time, the captain attempted to dampen it by engaging the autopilot; however, this was unsuccessful and it was immediately disengaged. The first officer next lowered the flaps, first to 5 degrees and then to 15 degrees, without any noticeable effect. The “Fasten Seat Belt" sign was turned on and the captain told the first officer to advise the company of their difficulty via radio. About this time a sudden failure in the control system was felt and it was with extreme difficulty that any semblance of elevator control was maintained. The first officer again tried lowering the flaps, this time to the 24-degree position, but as this did not help to maintain control he returned them to the 15-degree position, where it was found the most favorable results were attained. Accordingly, the first officer transmitted "Mayday” (distress call) on the radio and said that they were attempting to return to Des Moines but were experiencing control trouble. The buffeting became so severe it was then necessary for the copilot to help the can hold the control column. However, the buffeting lessened and the captain advised the first officer to depressurize the aircraft and tell the stewardess to prepare the passengers for an emergency landing. This was done. By that time the aircraft had descended below 3,000 feet. Both throttles were retarded in turn to see if the trouble could possibly be caused by one of the engines. This also proved to no avail. The vibration built up to high level and suddenly another failure in the control system was felt and the air-plane went into a steep climb. As it seemed that a stall was imminent, the captain quickly moved the propellers to a high r. p. m. and pushed the throttles forward until about 50 inches of manifold pressure was seen on the gauges. The airplane then nosed over and began to dive at a very steep angle. During this rapid descent the captain reduced power and headed toward open country to his right. When the aircraft reached 500 feet above the ground the captain was successful in flaring the aircraft and it struck the ground in a flat attitude. All occupants were quickly deplaned as soon as the aircraft stopped.
Probable cause:
The Board determines that the probable cause of this accident was a series of omissions made by maintenance personnel during a scheduled inspection which resulted in the release of the aircraft in an unairworthy condition and an almost complete loss of elevator control during flight. The following findings were reported:
- During a routine maintenance inspection of the aircraft an explanation was not written on the non-routine job card that the bolt had been removed and replaced finger-tight pending the arrival of a new bolt,
- Final inspection of the servo tab system failed to disclose its unairworthy condition and the aircraft was released for service,
- Vibration backed off an unsafetied not in the servo tab system resulting in a sequence of structural failures that ended in almost complete loss of control of the aircraft elevators.
Final Report:

Crash of a Douglas DC-3A in Denver: 3 killed

Date & Time: Dec 4, 1951 at 0725 LT
Type of aircraft:
Operator:
Registration:
N17109
Flight Phase:
Flight Type:
Survivors:
No
Schedule:
Denver - Denver
MSN:
4999
YOM:
1942
Flight number:
UA016
Crew on board:
3
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
3
Captain / Total flying hours:
5793
Captain / Total hours on type:
2404.00
Copilot / Total flying hours:
1250
Copilot / Total hours on type:
100
Aircraft flight hours:
15041
Circumstances:
United Air Lines operates a Flight Training Center at Denver, Colorado, to train applicants for first officer positions with the company. The crew of United Trainer 16 consisted of Senior First Officer Jordan D. Kocher, who had been designated by United Air Lines as captain and instructor, and Trainee First Officers Laurence G. Wilson and Wayne C. Moen. The flight departed Stapleton Airfield at 0655LT. The 0628 weather conditions, upon which the crew had been briefed, were ceiling measured 15,000 feet, visibility 25 miles, and wind northwest 14 knots Ceiling and visibility were unlimited at the time of the accident, with the wind northwest 16 knots. No radio contacts were made by United Trainer 16 after reporting departure time. It was cleared for a training flight of four hours’ duration within a 25-mile radius of Denver Captain Kocher occupied the left pilot’s seat at takeoff. Upon departure, the aircraft load, in addition to the crew, was 820 gallons of gasoline, full oil tanks, and 650 pounds of sand ballast tied down in the rear baggage pit. The load was properly distributed with relation to the aircraft’s center of gravity, and the 22,910-pound gross weight at takeoff was within allowable limits. Witnesses reported that at between 0720 and 0725 the aircraft was seen to stall, enter a spin, and strike the ground in a diving attitude before recovery was effected.
Probable cause:
The Board finds that the probable cause of this accident was an inadvertent spin at an altitude too low for recovery. The following findings were pointed out:
- The load was properly distributed within approved center of gravity limits and the aircraft was lightly loaded, carrying only the crew in addition to the fuel, oil and ballast,
- No malfunctioning of the aircraft or its components was reported prior to the accident, and no evidence of malfunctioning or failure was indicated by examination of the wreckage,
- The aircraft stalled at an altitude of approximately 8,200 feet MSL (about 3,200 feet above the ground), entered a spin, and crashed before recovery could be effected,
- Power was being developed by both engines upon impact.
Final Report:

Crash of a Boeing 377 Stratocruiser off Redwood City: 3 killed

Date & Time: Sep 12, 1951 at 1146 LT
Type of aircraft:
Operator:
Registration:
N31230
Flight Type:
Survivors:
No
Schedule:
San Francisco – Oakland – San Francisco
MSN:
15970
YOM:
1949
Flight number:
UA7030
Crew on board:
3
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
3
Captain / Total flying hours:
17384
Captain / Total hours on type:
572.00
Copilot / Total flying hours:
16390
Copilot / Total hours on type:
346
Aircraft flight hours:
1971
Circumstances:
The flight departed San Francisco at 1042, operating as "United Trainer 7030." Flight Manager Frederick S. Angstadt was captain and was being given his semi-annual instrument check by Assistant Flight Manager Hugh C. Worthington, who served as copilot. Flight Engineer Charles K. Brogden was the third crew member. In addition to the foregoing instrument check, consideration had been given to investigating the feasibility of using the Oakland, California, Municipal Airport for certain phases of crew training in this type aircraft for a new class of pilots and flight engineers which was to convene that afternoon. Captains Angstadt and Worthington were to supervise this training. United Air Lines' officials stated that Captains Angstadt and Worthington intended to make this determination during the flight. Captain Angstadt was given the 0928 sequence weather reports for the local area prior to completing a clearance form at the UAL dispatcher's office. Pertinent weather was as follows: stratus clouds in the Bay area with tops at approximately 1,600 feet; San Francisco and Oakland - 800 foot ceiling, overcast, visibility three miles, haze and smoke; ceiling and visibility at Fresno and Sacramento unlimited. The forecast for the Bay area indicated scattered clouds by 1100 PST. Clearance was issued for local flight under Visual Flight Rules (VFR), confined to a 100-mile radius from San Francisco and under 10,000 feet. The load was properly distributed with respect to permissible center of gravity limits. Gross weight of the aircraft at takeoff was 114,886 pounds with 4,700 gallons of fuel, well under the maximum permissible gross takeoff weight. After reporting on top of the broken scattered clouds to the San Francisco tower at 1046, the flight proceeded to Oakland. The Oakland tower approved a simulated Instrument Landing System approach; this and a missed approach procedure were performed. The flight again reported on top at 1136. Another simulated ILS approach was requested of the Oakland tower but the flight was advised that there would be a delay due to other traffic. In view of this, the pilot decided to return to San Francisco. The flight changed frequency from the Oakland tower to San Francisco Approach Control at 1137. At 1139, the flight was cleared for an ILS approach to the San Francisco Airport, but did not acknowledge the clearance on the 119.1 megacycle Approach Control frequency. Following two attempts to contact the flight, the controller heard the aircraft make an unreadable call on 121.9 megacycles, and instructed the flight to listen on 119.1. This transmission was followed by further instruction for the flight to hold VFR, and stand by. The frequency change was apparently accomplished by the flight and the pilot again requested permission to make a simulated ILS approach. The request was granted, with instructions to report upon leaving the ILS outer marker inbound. This message and one other were not acknowledged by the flight. No emergency call was received from the aircraft. The crash was reported to the U. S. Coast Guard Air Station at 1046 by the manager of a nearby airport.
Probable cause:
The Board determines that the probable cause of this accident was an inadvertent stall at a low altitude from which recovery was not effected. The following findings were pointed out:
- The aircraft, with No. 4 propeller feathered, stalled and abruptly dived from an altitude of approximately 300 feet and was demolished upon impact in San Francisco Bay,
- Engines Nos. 1, 2, and 3 were developing power at the time of impact,
- The No. 4 propeller was feathered; however, there was no evidence found of structural failure or malfunctioning of this engine or its propeller,
- The landing gear was extended and wing flaps were down 10 degrees at time of impact,
- About 75 per cent of the aircraft was recovered; no evidence of fire fuel or electrical system malfunction, or structural failure in flight,
- The cause of the stall was not definitely determined.
Final Report: