Crash of a Cessna 401A in Morrisville: 5 killed

Date & Time: Apr 2, 1970 at 0001 LT
Type of aircraft:
Registration:
N401RA
Survivors:
No
Schedule:
Huntsville – Morrisville
MSN:
401A-0117
YOM:
1969
Crew on board:
1
Crew fatalities:
Pax on board:
4
Pax fatalities:
Other fatalities:
Total fatalities:
5
Captain / Total flying hours:
3247
Captain / Total hours on type:
297.00
Circumstances:
On final approach in poor weather conditions, the twin engine aircraft went out of control, struck trees and crashed in an open field located short of runway threshold. The airplane was destroyed and all five occupants were killed.
Probable cause:
Improper IFR operation on part of the pilot-in-command. The following factors were considered as contributing:
- Improper compensation for wind coditions,
- Sudden windshift,
- Erratic flight path after passing outer marker,
- ILS straight-in approach,
- Strong windshift reported at approximately 400 feet.
Final Report:

Crash of a Beechcraft 65-A80 Queen Air in Chicago: 1 killed

Date & Time: Mar 25, 1970 at 1940 LT
Type of aircraft:
Operator:
Registration:
N242U
Flight Phase:
Survivors:
Yes
Schedule:
Chicago - New Castle
MSN:
LD-242
YOM:
1965
Crew on board:
2
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
1
Captain / Total flying hours:
6115
Captain / Total hours on type:
263.00
Circumstances:
At liftoff, the twin engine encountered serious difficulties to gain height, stalled and crashed. A pilot was killed while the second crew member was seriously injured.
Probable cause:
Stall after takeoff due to an excessive accumulation of snow on wings and fuselage. The following contributing factors were reported:
- Inadequate preflight preparation,
- Airframe ice,
- Icing conditions,
- Snow,
- Slush on runway,
- The crew partially removed snow before taxi,
- 13 minutes time span between taxi out and takeoff in snow conditions.
Final Report:

Crash of a Convair CV-240-0 at Langley AFB

Date & Time: Feb 20, 1970 at 1244 LT
Type of aircraft:
Registration:
N741J
Survivors:
Yes
Schedule:
Richmond - Linden
MSN:
146
YOM:
1949
Crew on board:
4
Crew fatalities:
Pax on board:
24
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
11000
Captain / Total hours on type:
1000.00
Circumstances:
En route from Richmond to Linden, NJ, the crew informed ATC about technical problems and that he was unable to lower the landing gear. ATC cleared the crew to divert to Langley AFB for an emergency landing. The airplane belly landed on a foamed runway and came to rest. All 28 occupants were evacuated safely while the aircraft was damaged beyond repair.
Probable cause:
Wheels-up landing caused by the malfunction of the landing gear mechanism. The following contributing factors were reported:
- Improper maintenance on part of the maintenant personnel,
- Failure of the landing gear mechanism,
- Material failure, corrosion,
- Suspected mechanical discrepancy,
- Numerous aircraft maintenance discrepancies,
- Uplock cable broken,
- Emergency system pressure too low.
Final Report:

Crash of a Swearingen SA26T Merlin IIB in Cleveland: 1 killed

Date & Time: Jan 29, 1970 at 1924 LT
Type of aircraft:
Operator:
Registration:
N239P
Survivors:
Yes
Schedule:
Jamestown - Cleveland
MSN:
T26-147
YOM:
1969
Crew on board:
2
Crew fatalities:
Pax on board:
2
Pax fatalities:
Other fatalities:
Total fatalities:
1
Captain / Total flying hours:
3733
Captain / Total hours on type:
225.00
Circumstances:
On final approach by night to Cuyahoga County Airport, the crew encountered poor weather conditions with snow falls and icing. At the decision height, the runway was not in sight but the captain decided to continue when the airplane struck tree tops and crashed in a wooded area located 4,610 feet short of runway 24. A pilot was killed while three other occupants were injured.
Probable cause:
The accident was the consequence of improper IFR operation on part of the flying crew. The following factors were considered as contributing:
- Airframe ice,
- Snow,
- Icing conditions with sleet and freezing rain,
- Turbulences associated with thunderstorm activity,
- The crew decided to descend below the minimum descent altitude,
- Both landing lights were ON in heavy snow falls.
Final Report:

Crash of a Mitsubishi MU-2B-20 Marquise in Salisbury

Date & Time: Jan 16, 1970 at 0115 LT
Type of aircraft:
Operator:
Registration:
N764Q
Survivors:
Yes
Schedule:
Miami – Norfolk – Philadelphia
MSN:
141
YOM:
1969
Crew on board:
1
Crew fatalities:
Pax on board:
4
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
9100
Captain / Total hours on type:
137.00
Circumstances:
The twin engine aircraft was completing a flight from Miami to Philadelphia with an intermediate stop in Norfolk, Virginia. On the second leg, the pilot encountered fuel problems and was forced to divert to Salisbury Regional Airport for an emergency landing. On final, both engines stopped simultaneously and the airplane stalled, struck trees and crashed in a wooded area. All five occupants were injured, two of them seriously. The aircraft was destroyed.
Probable cause:
Double engine failure caused by a fuel starvation. The following factors were considered as contributing:
- Mismanagement of fuel on part of the pilot,
- Miscalculation of fuel consumption on part of the pilot,
- Fuel starvation,
- Double engine failure,
- Fuel in tip tanks only as the others were empty,
- Undetermined amount of fuel lost due to broken O ring seal,
- Fuel level control valve.
Final Report:

Crash of a Cessna 401 in Piketon: 5 killed

Date & Time: Dec 17, 1969 at 0920 LT
Type of aircraft:
Operator:
Registration:
N8167F
Flight Phase:
Survivors:
No
Schedule:
Cincinnati - Parkersburg
MSN:
401-0236
Location:
Crew on board:
1
Crew fatalities:
Pax on board:
4
Pax fatalities:
Other fatalities:
Total fatalities:
5
Captain / Total flying hours:
8477
Captain / Total hours on type:
500.00
Circumstances:
En route, the right engine caught fire that spread to the right wing. An aileron detached, causing the airplane to be uncontrollable. The pilot informed ATC and elected to make an emergency landing when the airplane crashed in flames in an open field located in Piketon. All five occupants were killed.
Probable cause:
Uncontrolled descent following the failure of the right engine turbocharger in flight. Escaping heat ignited fuel and oil lines caused the aileron to burn and detach. The following factors were reported:
- Powerplant, engine accessories failure,
- Material failure, fire in engine and wing,
- Separation in flight.
Final Report:

Crash of a Rockwell 1121B Jet Commander in Salt Lake City: 2 killed

Date & Time: Dec 16, 1969 at 0610 LT
Operator:
Registration:
N403M
Flight Phase:
Survivors:
No
Schedule:
Salt Lake City - Seattle
MSN:
1121-132
YOM:
1969
Crew on board:
2
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
2
Captain / Total flying hours:
9423
Captain / Total hours on type:
1195.00
Circumstances:
During the takeoff roll at Salt Lake City Airport, the crew completed the rotation too early. The aircraft stalled then crashed in flames near the runway. The aircraft was destroyed and both pilots were killed.
Probable cause:
Premature liftoff on part of the flying crew. The following factors were considered as contributing:
- The pilot-in-command failed to obtain flying speed,
- Physical impairment,
- Crew fatigue,
- Improperly loaded aircraft-weight and/or CofG,
- Icing conditions including sleet and freezing rain,
- Obstructions to vision.
Final Report:

Crash of a Beechcraft 60 Duke in Houston

Date & Time: Nov 21, 1969 at 1520 LT
Type of aircraft:
Registration:
N812JR
Survivors:
Yes
Schedule:
Alief - Alief
MSN:
P-44
YOM:
1969
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
1762
Captain / Total hours on type:
439.00
Circumstances:
After touchdown at Houston Airport, the pilot started the braking procedure when he inadvertently raised the landing gear. The aircraft sank on its belly and slid for dozen yards before coming to rest in flames. The pilot escaped uninjured while the aircraft was destroyed.
Probable cause:
The pilot inadvertently retracted the landing gear after touchdown.
Final Report:

Crash of a BAe 125-400A in Wabush: 8 killed

Date & Time: Nov 11, 1969 at 1830 LT
Type of aircraft:
Operator:
Registration:
CF-CFL
Survivors:
No
Schedule:
Churchill Falls - Wabush - Montreal
MSN:
25193/NA725
YOM:
1969
Country:
Crew on board:
2
Crew fatalities:
Pax on board:
6
Pax fatalities:
Other fatalities:
Total fatalities:
8
Circumstances:
The twin engine aircraft departed Churchill Falls Airport at 1800LT on a flight to Montreal with an intermediate stop in Wabush (Labrador City). On final approach, the crew encountered poor weather conditions and failed to realize his altitude was insufficient. Out of track, the airplane struck trees then crashed on a mountainous terrain located few km from the airport. The controller at Wabush Airport informed Moncton ATC about the disappearance of the aircraft and SAR operations were initiated. All eight occupants were killed, among them Donald J. McParland, President of Churchill Falls (Labrador) Corporation, his assistant John Lethbridge, Eric Lambert and three employees of the Acres Canadian Bechtel.
Probable cause:
It was determined that the aircraft was off course on approach after the crew referred to the wrong NDB. Low visibility caused by poor weather conditions was a contributing factor.

Crash of a Learjet 23 off Racine: 7 killed

Date & Time: Nov 6, 1969 at 1107 LT
Type of aircraft:
Operator:
Registration:
N1021B
Survivors:
No
Schedule:
Benton Harbor - Racine
MSN:
23-086
YOM:
1966
Crew on board:
2
Crew fatalities:
Pax on board:
5
Pax fatalities:
Other fatalities:
Total fatalities:
7
Captain / Total flying hours:
7076
Captain / Total hours on type:
625.00
Circumstances:
On approach to Racine-Batten Airport, the crew failed to realize his altitude was insufficient when the airplane struck the water surface and crashed into Lake Michigan, few miles offshore. The floating wreckage was recovered but all seven occupants were killed.
Probable cause:
Investigations were unable to determined the exact cause of the accident and the reason why the crew was approaching the airport below the minimum safe altitude.
Final Report: