Crash of a PZL-Mielec AN-2R in Narsarsuaq

Date & Time: Feb 4, 2007
Type of aircraft:
Operator:
Registration:
LY-AJG
Flight Phase:
Flight Type:
Survivors:
Yes
Schedule:
Vágar - Reykjavik - Kulusuk - Narsarsuaq
MSN:
1G178-48
YOM:
1977
Country:
Region:
Crew on board:
2
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
On take off from Narsarsuaq Airport, the single engine aircraft was caught by strong winds, veered off runway and collided with a bank. Both left wings were damaged while the undercarriage were torn off. Both pilots escaped uninjured while the aircraft was damaged beyond repair. A snow storm was approaching Narsarsuaq at the time of the accident.

Crash of a Cessna 401 in Narsarsuaq

Date & Time: Jan 31, 2007
Type of aircraft:
Operator:
Registration:
N6274Q
Flight Type:
Survivors:
Yes
Schedule:
Goose Bay - Narsarsuaq
MSN:
401-0074
YOM:
1969
Country:
Region:
Crew on board:
2
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
For unknown reasons, the twin engine aircraft made a wheels up landing at Narsarsuaq Airport and came to rest. Both pilots escaped uninjured while the aircraft was damaged beyond repair. They were completing a flight from Goose Bay. The exact date of the occurrence remains unknown, somewhere in January 2007.

Crash of a Dassault Falcon 20C in Narsarsuaq: 3 killed

Date & Time: Aug 5, 2001 at 0245 LT
Type of aircraft:
Operator:
Registration:
D-CBNA
Flight Type:
Survivors:
No
Schedule:
Gdansk – Copenhagen – Keflavik – Narsarsuaq – Seven Islands – Louisville
MSN:
63
YOM:
1967
Country:
Region:
Crew on board:
2
Crew fatalities:
Pax on board:
1
Pax fatalities:
Other fatalities:
Total fatalities:
3
Circumstances:
The flight, during which the accident occurred, was part of a non-scheduled international cargo flight from Gdansk (EPGD) to Louisville (KSDF). The flight crew had previously on August 4, 2001, on another charter flight, flown the aircraft from Hanover (EDDV) to Palma de Mallorca (LEPA) and then to EPGD in order to bring the aircraft in position for the cargo flight. The flight was chartered by a cargo courier to depart EPGD at 2000 hrs on August 4, 2001, and arrive at KSDF at 0900 hrs on August 5, 2001. Technical landings (fuel uplift) were planned at EKCH in Denmark, at Keflavik (BIKF) in Iceland, at BGBW in Greenland and at Sept-Iles (CYZV) in Canada. The aircraft had a two hour delay at LEPA due to a slot time. For that reason, the aircraft did not arrive at EPGD until 2106 hrs. The aircraft was refuelled and the flight crew loaded the cargo themselves. The aircraft departed EPGD at 2218 hrs and arrived at EKCH at 2238 hrs. Then the aircraft departed EKCH at 2313 hrs and arrived at BIKF at 0202 hrs. At BIKF, the aircraft was refuelled with 1034 USG of JET A1. The commander filed an ATC flight plan for BGBW with Kangerlussuaq (BGSF) in Greenland as destination alternate. At BIKF no weather reports for BGBW were valid for the flight crew’s flight planning. The handling agent directed the Commander’s attention to the lack of updated weather reports for BGBW, but the Commander seemed not to be concerned. It was the general opinion of the handling agent that the Commander seemed stressed. At 0246 hrs, the flight crew requested start up and shortly after they got an ATC clearance to BGBW via EMBLA, 63N 30W, 62N 40W and NA at FL 240 with cruise Mach at 0.76. The aircraft departed BIKF at 0300 hrs and the flight crew got an ATC clearance with FL 260 as the final cruising level inbound BGBW. The First Officer was the pilot flying and the Commander was the pilot non-flying. At 0423:24 hrs, the Commander contacted Narsarsuaq Flight Information Service (FIS) on frequency 121.300 MHz. The Commander reported that they expected to be overhead NA (358 KHz) at 0438 hrs. At this time, the aircraft was cruising at FL 260 and was inbound NA on a magnetic track of 280° approximately 50 nm east of the aerodrome. Through link to Gander ATC, Narsarsuaq FIS cleared the aircraft to descend out of controlled airspace on QNH 1004 and to report FL 195 descending. The Commander was now the pilot flying and the First Officer was the pilot non-flying. The Commander had experience of flying to BGBW. The aircraft left FL 260, and at 0434:27 hrs, the First Officer reported that the aircraft was passing FL 195. Narsarsuaq FIS requested the flight crew to report 10 nm from the aerodrome. While descending, the flight crew made a briefing on the NDB/DME approach procedure to runway 07. At 0437:00 hrs, the First Officer reported that the aircraft was 10 NM from NA. Narsarsuaq FIS requested the flight crew to contact Narsarsuaq AFIS on frequency 119.100 MHz. At 0437:17 hrs, the flight crew was in contact with Narsarsuaq AFIS and the First Officer reported passing FL 130. The AFIS Operator reported that there was no reported traffic in the TIZ and that the flight crew could make an approach by their own discretion. The weather was reported to be a wind direction and speed of 080° at 24 knots, visibility 10 kilometres with broken clouds at 6000 feet and overcast at 9000 feet, light rain, temperature +14°C, dew point +3°C and the QNH 1004 hPa. At 0440:26 hrs and at 0440:52 hrs, one of the flight crewmembers made cockpit call outs of passing 6 nm and 8 nm respectively outbound from NA. At 0441:45 hrs, one of the flight crewmembers made a cockpit call out of the aircraft being on base. The Commander ordered the extension of the landing gear. With reference to the CVR read out, there were no audible flight crew call outs concerning the use of checklists, altitude checks and Standard Operating Procedures (SOP) during the descent, the initial and the final approach phase. At 0442:29 hrs, the First Officer reported that the aircraft was on final to runway 07. The AFIS operator reported the threshold wind for runway 07 to be 070° at 22 knots gusting to 29 knots and the runway to be free. The AFIS operator made a visual scan of the approach sector, but he did not see the aircraft, as he normally would have, when an aircraft was established on final in dark night and under similar weather conditions. At approximately 0443:07 hrs, the aircraft impacted in landing configuration mountainous terrain at approximately 700 feet msl. The accident occurred 4.5 nm southwest of the aerodrome. On the CVR read out, there were no audible flight crew call outs immediately before the impact. Several times from 0452 hrs until 0459 hrs, Narsarsuaq AFIS tried to get in radio contact with the aircraft, but there was no reply.
Probable cause:
A combination of non-adherence to the approach procedure and the lack of vertical position awareness was the causal factor to this Controlled Flight Into Terrain (CFIT) accident. Several of the most common factors found in CFIT accidents were present in this accident. The flight crew did not follow SOPs (adherence to the approach procedure, altitude calls, checklist reading). Furthermore the GPWS was inoperative and the flight crew were exposed to peak fatigue. The absence of CRM and non-adherence to SOPs removed important defences in preventing CFIT. In this accident, the aircraft was capable of being controlled and was under control of the flight crew until impact. Nothing indicated that the flight crew were aware of their proximity to the mountainous terrain. Consequently, this is considered to be a CFIT accident.
Final Report:

Crash of a Dornier DO.28D Skyservant in Nuuk

Date & Time: Dec 5, 1994 at 1223 LT
Type of aircraft:
Operator:
Registration:
D-IDNG
Flight Type:
Survivors:
Yes
Schedule:
Reykjavik - Goose Bay
MSN:
4112
YOM:
1971
Country:
Region:
Crew on board:
1
Crew fatalities:
Pax on board:
1
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
The twin engine aircraft was on a delivery flight from Germany to Colombia via Iceland and Canada, carrying one passenger and one pilot. On the leg from Reykjavik to Goose Bay, about 20 minutes into the flight, the right engine failed. As the pilot was unable to restart it, he decided to divert to Nuuk for an emergency landing. On short final, at a height of about 100 metres, the aircraft entered a right turn and struck the ground. Upon impact, the undercarriage were torn off and the aircraft came to rest against an embankment. Both occupants were slightly injured and the aircraft was damaged beyond repair.
Probable cause:
The exact cause of the engine failure could not be determined. Except the fact that a hinge pin was missing in the injector air heating system, no technical malfunction was found. It was reported that the pilot was not certified to perform such flight and the passenger was not allowed to take part to such mission according to the provisional airworthiness certificate that was valid till the day of the occurrence. The possible presence of windshear on final approach was not ruled out and it was also reported that the approach was completed with a speed that was approximately 10 to 15 knots below the prescribed approach speed.