Crash of a Cessna 402B in Fort Lauderdale

Date & Time: Nov 2, 1997 at 1745 LT
Type of aircraft:
Operator:
Registration:
N69312
Survivors:
Yes
Schedule:
Andros Town - Fort Lauderdale
MSN:
402B-0430
YOM:
1973
Crew on board:
1
Crew fatalities:
Pax on board:
6
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
5017
Captain / Total hours on type:
2175.00
Aircraft flight hours:
7482
Circumstances:
The pilot was on approach for landing when the right main landing gear did not indicate that it was down. The pilot made a go-around and remained in left closed traffic performing emergency gear extension procedures with negative results. The pilot departed closed traffic and proceeded offshore to burn off fuel before attempting an emergency landing. A company airplane was dispatched to verify the landing gear position. The pilot started a straight in approach for landing five miles from the airport. The right engine started surging and quit. The left engine started surging one mile from the runway. He switched fuel tanks. The engine started and quit. He made a forced landing straight ahead and collided with runway approach lights about 1/4 mile from the end of the runway. The pilot stated he ran out of fuel.
Probable cause:
The pilot's improper management of fuel resulting in a total loss of engine power on both engines due to fuel exhaustion.
Final Report:

Crash of a Learjet 35A in Avon Park

Date & Time: Jul 15, 1997 at 1953 LT
Type of aircraft:
Registration:
N19LH
Flight Type:
Survivors:
Yes
Schedule:
Fort Lauderdale - Avon Park
MSN:
35-279
YOM:
1980
Crew on board:
2
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
20076
Captain / Total hours on type:
1500.00
Aircraft flight hours:
13726
Circumstances:
Witnesses near the airport saw the flight approach on a left base to runway 4, touchdown on the runway, and takeoff again. One witness, a pilot, said the airplane turned onto final to the 'south' (right) of the runway centerline.' The airplane made a 'sharp' turn to the left to realign with the runway center, slightly overshot the runway to the left, turned to the right 'sharply,' and touched down on the runway. The witness further stated, '...by the time the pilot was on the runway he had wasted approximately 1,200 to 1,500 feet of runway 4, they hit reverse thrusters [sic] and were on full bore till they crossed runway 27 and 9.' The witness saw heat come out of both engine thrust reversers, the nose gear touched down and then came up again. He then saw the airplane come off the ground about 30 to 40 feet, wobble left and right at a 'slow airspeed,' crossover a highway at a low altitude, right wing low, strike some wires, go into a field, and catch fire. The pilot said, when he touched down on the runway, the airplane seemed to 'lurch' to the side. He said at this point his airspeed was 126 knots. He elected to abort the landing, and applied full power. He said the engines would not develop thrust and he elected to land in a field less than 1/4 mile in front of him. Examination of the left thrust reverser revealed that the translator was in the deployed position, with the blocker doors fully open. Both the left and right pneumatic latches were found in the unlocked position. Examination of the right thrust reverser revealed that the translator was in the deployed position, with the blocker doors fully closed. The left pneumatic latch was found in the locked position. The right pneumatic latch was found in the unlocked position. The inboard sequence latches were found about 2 inches forward of full aft travel. The thrust reverser switch was found in the 'NORMAL' position. According to Gates Lear Jet Airworthiness Directive (AD) 79-08-01, '...to preclude inadvertent thrust reverser deployment and possible loss of aircraft control....,' the following limitations apply to all gates Lear Jet Model 35, 36, 35A, 36A, aircraft equipped with Aeronca Thrust reversers. According to the AD, Section I-LIMITATION; '....Thrust Reversers must not be operated prior to takeoff...Thrust Reversers must not be used for touch and go landings...After Thrust Reversers have been deployed, a visual check of proper door stowing must be made prior to takeoff...Operational Procedures in this Thrust Reverser Supplement are mandatory.' According to Lear Jet and FlightSafety International, the procedures that are taught to Lear Jet pilots in the use of thrust reverse and spoilers during landings are; '...pilots [are] to use thrust reverse only on full stop Lear Jet landings. Pilot are trained not to deploy spoilers or thrust reverse during touch and go's or during balked landings.' The pilot-in-command of N19LH at the time of the accident, told the NTSB investigator-in-charge (IIC) that he was 'aware' of the limitations on the Aeronca Thrust Reverser and he knew that once the Thrust Reverser was deployed that he was 'committed' to land. The pilot told the IIC that he knew of the limitations and that he was committed to land.
Probable cause:
A loss of engine power as a result of the thrust reversers being deployed and subsequent inflight collision was wires. Factors in this accident were the pilot's disregard for procedures, and the improper use of the thrust reversers.
Final Report:

Crash of a Beechcraft E18S off Walker's Cay

Date & Time: Mar 23, 1995 at 1500 LT
Type of aircraft:
Registration:
N8111
Flight Type:
Survivors:
Yes
Schedule:
Fort Lauderdale - Walker's Cay
MSN:
BA-113
YOM:
1955
Country:
Crew on board:
1
Crew fatalities:
Pax on board:
1
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
Following a wrong approach configuration, the twin engine aircraft landed too far down the runway at Walker's Cay Airfield. After touchdown, the pilot realized his mistake and initiated a go-around procedure. He asked the passenger seating on the right seat (a pilot rated passenger) to retract the flaps. Mistakenly, the passenger raised the landing gear instead. The aircraft sank on its belly, causing both propellers to struck the runway surface. The aircraft caught fire and the pilot elected to continue. During initial climb, he eventually ditched the airplane few dozen metres offshore. Both occupants were seriously injured and the aircraft was destroyed.

Crash of a Convair CV-440 Metropolitan in Cap Haïtien

Date & Time: Mar 18, 1995 at 1321 LT
Registration:
N137CA
Survivors:
Yes
Schedule:
Fort Lauderdale - Cap Haïtien
MSN:
317
YOM:
1956
Country:
Crew on board:
2
Crew fatalities:
Pax on board:
29
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
Leased from Winemiller Aviation, the aircraft was completing a charter flight from Fort Lauderdale to Cap Haïtien on behalf of the Metro Nord Travel Club. On approach to Cap Haïtien, flaps and undercarriage were selected down when the hydraulic pressure dropped. The crew continued the approach and the emergency air brake was armed. Upon touchdown, both tyres on the left main gear burst after the brakes locked. The aircraft veered off runway to the left and eventually collided with a parked UH-60 helicopter. All 31 occupants were evacuated safely and the aircraft was damaged beyond repair.
Probable cause:
It was determined that both tyres on the left main gear burst after the brakes locked due to a reported malfunction of the air brake system.

Crash of a Beechcraft G18S in Fort Lauderdale

Date & Time: Feb 16, 1994 at 0921 LT
Type of aircraft:
Registration:
N49K
Flight Type:
Survivors:
Yes
Schedule:
Fort Lauderdale - Freeport
MSN:
BA-519
YOM:
1960
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
8700
Captain / Total hours on type:
5000.00
Aircraft flight hours:
12099
Circumstances:
The pilot stated the left engine backfired and began to run rough shortly after takeoff. The engine was shut down and the propeller was feathered. He decided to return and land on the departure runway. Witnesses observed the aircraft on the downwind leg at 800 to 1,000 feet with the landing gear extended. As the aircraft turned to base leg it yawed sharply to the left and the left wing dropped. The aircraft descended rapidly. The pilot stated that as he turned from base to final leg at 75 to 100 feet the aircraft was buffeting and beginning to stall. He realized he would not make the runway and crash landed in a vacant lot. Examination of the left engine after the accident revealed no evidence to indicate precrash failure or malfunction of the engine.
Probable cause:
The pilot-in-command's improper approach planning and premature extension of the landing gear, resulting in the flight being unable to maintain sufficient altitude and airspeed to reach the runway. The loss of engine power on one engine was a factor.
Final Report:

Crash of a Cessna 402C near Andytown

Date & Time: Aug 25, 1993 at 0855 LT
Type of aircraft:
Operator:
Registration:
N206RH
Flight Phase:
Survivors:
Yes
Schedule:
Sarasota - Fort Lauderdale
MSN:
402C-0206
YOM:
1979
Crew on board:
1
Crew fatalities:
Pax on board:
4
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
3000
Captain / Total hours on type:
2400.00
Aircraft flight hours:
12918
Circumstances:
The pilot was deviating around weather during descent when he noted the fuel flow and manifold pressure on the left engine oscillating. Because the propeller was still turning he elected not to feather the left propeller. The airplane would not maintain altitude so he lowered the landing gear and ditched the airplane in a swamp. Examination of the left fuel tank revealed the fuel float valve actuators and float arms excessively worn. This condition would allow unmetered air into the fuel lines. Also noted was the condition of one of the left fuel valves that could jam open allowing the fuel pickup to unport and induce excessive air into the fuel lines.
Probable cause:
The failure of the pilot to feather the propeller when the engine lost power, and his failure to follow the emergency procedure checklist. Contributing to the accident was the inadequate design of the fuel tank float valves which allowed for excessive wear and subsequent induction of unmetered air into the fuel lines.
Final Report:

Crash of a Piper PA-31-350 Navajo Chieftain in South Bimini

Date & Time: Jan 2, 1993 at 0945 LT
Registration:
N4107V
Flight Type:
Survivors:
Yes
Schedule:
Fort Lauderdale - South Bimini
MSN:
31-8253010
YOM:
1982
Country:
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
Crashed in unknown circumstances upon landing at South Bimini Airport. The pilot, sole on board, was uninjured.

Crash of a Douglas DC-7CF off Fort Lauderdale

Date & Time: Nov 6, 1992 at 0225 LT
Type of aircraft:
Operator:
Registration:
HI-619SP
Flight Phase:
Flight Type:
Survivors:
Yes
Schedule:
Fort Lauderdale - Santo Domingo
MSN:
45158
YOM:
1956
Crew on board:
3
Crew fatalities:
Pax on board:
2
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
The crew reported over radio that the #4 engine failed shortly after takeoff, and they were attempting to dump fuel when the #2 engine overheated. They then intentionally ditched the airplane. The wreckage was recovered about 2 weeks afterward, and the airplane was about 50% corroded away. Due to massive salt water corrosion, no preimpact failure/malfunction of the #4 engine could be identified. No record of airplane/operator being granted cfr part 129 certificate authority. No substantiation of the times in service for the airplane, engines, propellers, and time change components or airworthiness directives could be determined.
Probable cause:
Failure of the #4 engine for an undetermined reasons(s), and the inability of the airplane to remain airborne due to the over gross weight takeoff performed by the pilot. Factors which contributed to the accident were: the questionable airworthiness of the airplane and engines due to the lack of records, and the failure of the federal aviation administration to adequately surveil the operator.
Final Report:

Crash of a Rockwell Grand Commander 690B in Konawa: 1 killed

Date & Time: Jun 25, 1992 at 0833 LT
Registration:
N690JC
Flight Phase:
Flight Type:
Survivors:
No
Schedule:
Norman - Fort Lauderdale
MSN:
690-11479
YOM:
1978
Location:
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
1
Captain / Total flying hours:
8857
Captain / Total hours on type:
98.00
Aircraft flight hours:
3355
Circumstances:
As the airplane was deviating around low intensity weather returns, and passing through 20,500 feet during climb out, it departed controlled flight and entered a right spiral. Descent rates exceeded 16,600 fpm during the descent from 18,300 feet to 3,900 feet and then slowed. Witnesses stated they saw the airplane descend from the clouds in a right flap spin. The empennage had separated from the airplane in pieces. Pieces of the wreckage were found up to 1.5 mile from the primary impact point. Both wings remained attached. The right engine was flamed out, and the propeller was feathered at impact. No mechanical reason for the flameout could be determined. At no time did the pilot indicate he was having difficulties. The NTSB weather study indicated that moderate turbulence was present in the area. The pilot's toxicology tests found 0.151 ug/ml of chlorpheniramine in the blood; normal therapeutic concentration is 0.01 to 0.04. Effects of overdosage include sedation, diminished mental alertness, and cardiovascular collapse to stimulation. The pilot, sole on board, was killed.
Probable cause:
The pilot's failure to maintain control of the airplane which resulted in an inadvertent spiral and subsequent rapid descent. The design stress limits of the airframe were exceeded resulting in an overload failure of the empennage. Factors related to the accident were: turbulence and the pilot's physical impairment due to drugs.
Final Report:

Crash of a Cessna 402B off The Bahamas

Date & Time: Jun 13, 1992 at 1115 LT
Type of aircraft:
Operator:
Registration:
N402PB
Flight Phase:
Flight Type:
Survivors:
Yes
Schedule:
Treasure Cay - Fort Lauderdale
MSN:
402B-0245
YOM:
1972
Country:
Crew on board:
1
Crew fatalities:
Pax on board:
1
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
6574
Captain / Total hours on type:
231.00
Aircraft flight hours:
9097
Circumstances:
During cruise flight, the pilot reported that the right engine cowling partially separated and the left forward cylinder of that engine separated, followed by an engine compartment fire. He attempted to feather the propeller but was unable. He initiated a descent to extinguish the fire and was successful but after leveling off, was unable to maintain directional control. He ditched the airplane and both he and the passenger exited the aircraft. The pilot dragged the seriously injured passenger with him to a nearby island where they were rescued the following day. The aircraft was not recovered; therefore, no determination could be made as to the reason for the separation of the cylinder. Review of the aircraft logbook indicates that on 8/27/91, the n°5 cylinder of the right engine was removed and replaced. Also, the n°1 cylinder was removed and reinstalled following repair. There were no further entries in the aircraft logbook regarding cylinder removal or replacement to the right engine.
Probable cause:
For undetermined reason(s), the right engine failed and the right propeller would not feather.
Final Report: