Crash of a Martin 202 near Winona: 37 killed

Date & Time: Aug 29, 1948 at 1705 LT
Type of aircraft:
Operator:
Registration:
NC93044
Flight Phase:
Survivors:
No
Schedule:
Chicago – Minneapolis
MSN:
9165
YOM:
1947
Flight number:
NW421
Crew on board:
4
Crew fatalities:
Pax on board:
33
Pax fatalities:
Other fatalities:
Total fatalities:
37
Captain / Total flying hours:
5502
Captain / Total hours on type:
311.00
Copilot / Total flying hours:
2380
Copilot / Total hours on type:
155
Aircraft flight hours:
1321
Circumstances:
Northwest Airlines' Flight 421 departed from Chicago for Minneapolis at 1550, August 29, 1948. On board were 33 passengers, four crew members, 800 gallons of fuel, and 1,038 pounds of baggage. Total aircraft weight was 38,015 pounds which was within the certificated limit and it was properly loaded in reference to the center of gravity. Weather information available to the flight prior to departure indicated that relatively good flying conditions existed en route with the exception of scattered rain showers and thunderstorms which were in the vicinity of La Crosse, Wisconsin and Rochester, Minnesota. Routine position reports were received from the flight as it progressed on course at Its flight plan altitude of 8,000 feet. At 1655, one hour and five minutes after takeoff from Chicago, the flight reported over La Crosse, 125 miles southeast of Minneapolis, and was at that time cleared to start an en route descent. Four minutes later, at 1659, the flight reported passing through the 7,000-foot altitude level. No indication of any trouble was contained in this transmission. This was the last word beard from the flight. Between 1645 and 1700 several persons in the vicinity of Winona, Minnesota, approximately 95 miles southeast of Minneapolis were watching a thunderstorm which was approaching from the northwest, AS the storm moved over Winona, the wind increased in intensity and considerable lightning and thunder were observed. At this time, about 1705, Flight 421 was seen flying below the overcast. As it passed over Winona, the aircraft appeared to enter the roll cloud or the leading edge of the thunderstorm at which time it was lost from view. Seconds later parts of the airplane were observed falling. It was later found that the flight had crashed approximately 4 miles northwest of Winona on a bluff on the east side of the Mississippi River. All 37 occupants were killed.
Probable cause:
The Board determines that the probable cause of this accident was the loss of the outer panel of the left wing which separated from the aircraft as a result of a fatigue crack in the left front outer panel attachment fitting which had been induced by a faulty design of that fitting, the fatigue crack having been aggravated by severe turbulence encountered in the thunderstorm.
Final Report:

Crash of a Douglas DC-6 in Mount Carmel: 43 killed

Date & Time: Jun 17, 1948 at 1241 LT
Type of aircraft:
Operator:
Registration:
NC37506
Flight Phase:
Survivors:
No
Schedule:
San Diego – Los Angeles – Chicago – New York
MSN:
42871
YOM:
1947
Flight number:
UA624
Crew on board:
4
Crew fatalities:
Pax on board:
39
Pax fatalities:
Other fatalities:
Total fatalities:
43
Captain / Total flying hours:
7310
Captain / Total hours on type:
30.00
Copilot / Total flying hours:
3289
Copilot / Total hours on type:
129
Aircraft flight hours:
1245
Circumstances:
The airplane arrived in Chicago at 0952LT, en route from Los Angeles to New York City. At Chicago, the airplane was given a routine station inspection, serviced, loaded, and the flight departed for New York with a new crew at 1044. Aboard were 39 passengers, a crew of four, 2,568 pounds of cargo and 1,800 gallons of fuel, all properly loaded. The resulting total airplane weight was within the certificated gross weight. The airplane climbed en route to its planned altitude of 17,000 feet, proceeding on course, and at 1155 the captain reported to the company radio at LaGuardia Field, that the airplane was mechanically "okay” for a return trip. A routine report was made over Phillipsburg, PA, approximately 500 miles east of Chicago, at 1223, and at 1227 the crew made a routine acknowledgment of a clearance to descend en route to an altitude between 13,000 and 11,000 feet. Four minutes later, at 1231, the company radio operator at LaGuardia Field heard a voice which did not identify itself calling loudly and urgently. Another United crew in a DC-3, flying over the same route behind Flight 624 and at a different altitude, heard what they termed “screaming voices” calling "New York." Then, after an unintelligible transmission, “This is an emergency descent." Inasmuch as all other air carrier flights in the vicinity at this time were accounted for, this transmission undoubtedly emanated from Flight 624. The airplane was first observed by ground witnesses 31 miles northwest of the scene of the accident flying a southeasterly heading toward Shamokin, PA. The airplane flew over the Sunbury Airport, at approximately 4,000 feet above the ground on a southeasterly heading. Immediately north of Shamokin the airplane, then only 500 to 1,000 feet above the ground, described a shallow left turn. The course was toward constantly rising terrain, the hills around Sunbury being 900 feet in elevation and the hills around Shamokin being approximately 1,600 feet in elevation. Five miles east or beyond Shamokin the airplane, flying only 200 feet above the ground, entered a right climbing turn. As it passed to the north of Mount Carmel, the climbing turning attitude increased sharply. The airplane then struck a hillside at an elevation of 1,649 feet. The aircraft disintegrated on impact and all 43 occupants were killed.
Probable cause:
The Board determines that the probable cause of this accident was the incapacitation of the crew by a concentration of CO2 gas in the cockpit.
The following factors were considered as contributing:
- A fire warning caused the crew to discharge at least one bank of the CO2 fire extinguisher bottles in the forward cargo pit (the forward underfloor baggage compartment),
- Six 15-pound CO2 bottles and six discharge valves were found in the wreckage, however, both the bottles and the valves (which had become separated from their respective bottles upon impact) were so damaged that no conclusions could be drawn as to how many of such bottles had been discharged prior to impact,
- At the time of impact, the emergency cabin pressure relief valves were closed, and the control mechanism for such valves was in the closed position,
- Except for the apparent failure of the fire detection instrument referred to in finding No. 5, supra, the investigation revealed no mechanical failure of the aircraft or fire in flight,
- The emergency procedure for the operation of the DC-6 fire extinguisher system was established after flight tests were conducted in a descent configuration of 300 miles per hour, with landing gear and flaps up, no flight tests were conducted prior to the accident in a descent configuration of 160 miles per hour with gear and flaps down, which configuration was also approved for DC-6 operations,
- At the time of impact the landing gear was in the “up" position, thus indicating that the aircraft had descended in the configuration of 300 miles per hour. The extensive breakage of the aircraft precluded any positive determination as to the position of the flaps,
- After the release of CO2 gas hazardous concentrations of the gas entered into the cockpit,
- Due to the physiological and toxic effects of high concentrations of CO2 gas in the cockpit, which would probably not have occurred had the cabin pressure relief valves been open, the members of the flight crew of the aircraft were rendered physically and mentally incapable of performing their duties.
The following comment was added to the conclusion:
A fire in flight permits little opportunity for the exercise of detached and thoughtful consideration of emergency procedure. Immediate action is required if a fire is to be controlled. Too little consideration has been given to the psychological and physical limitations of crew members in time of stress and danger as related to the complexity of emergency fire procedure. It is not safe to assume that the pilot and co-pilot, under emergency pressure, will always adhere rigidly to the sequence of steps outlined in the CAA Approved Airplane Operating Manual. The possibility of human error under great mental stress is well documented in air transport experience and the design of aircraft controls, especially those of an emergency character, should take into consideration the natural limitations of human nature. These limitations argue against involved procedures applicable in emergencies. In harmony with this objective, the Douglas Aircraft Company has designed and is testing a modified fire extinguishing system which will permit all necessary steps to be executed by the movement of one control. An additional vent is also being designed to reduce CO2 concentration in the cockpit. Seven days after the Mt Carmel accident, the Director of Aviation Safety of the CAA directed telegrams to all CAA regional administrators calling attention to his telegram of June 10, 1948, referred to above, and advising that further investigation had disclosed the existence of the CO2 concentration condition found in Constellation aircraft by the Chillicothe tests in other makes of aircraft. The telegram concluded "Hence, flight crews of all aircraft should be advised to wear oxygen masks and utilize emergency cockpit smoke clearance procedures when carbon dioxide is released into any fuselage compartment from other than portable extinguishers.” All scheduled U S air carriers operating DC-6s have equipped the airplanes with demand type full face oxygen masks for the use of the crew.
Final Report:

Crash of a Curtiss C-46E-1-CS in Columbus: 2 killed

Date & Time: May 16, 1948 at 2042 LT
Type of aircraft:
Operator:
Registration:
NC59489
Flight Type:
Survivors:
No
Schedule:
Newark – Chicago – Denver – Burbank – San Francisco
MSN:
2938
YOM:
1945
Crew on board:
2
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
2
Captain / Total flying hours:
2580
Captain / Total hours on type:
600.00
Copilot / Total flying hours:
4675
Copilot / Total hours on type:
1354
Aircraft flight hours:
5641
Circumstances:
The flight departed from Newark, New Jersey, at 1733 May 16, 1948, for Chicago, Illinois, Denver, Colorado, Burbank, and San Francisco, California. In addition to a crew consisting of Captain William R. McCauley and Copilot Jack R. Foote, the flight carried 5,280 pounds of fuel, and 10,263 pounds of cargo. According to the hourly weather reports available to the crew in Newark prior to departure, thunderstorm activity which existed over the vicinity of Goshen and Fort Wayne, Indiana, was moving eastward. Chicago Municipal Airport was reported to have a ceiling of 2,000 feet. The flight plan specified a cruising altitude of 4,000 feet to Chicago, the first intended point of landing. South Bend, Indiana, was designated as the alternate airport. No unusual incident was reported for approximately the first two hours of the trip, then, at 1931 the flight reported over Cleveland, Ohio, at 4,000 feet, stating that there was extreme turbulence approximately five miles east of the Cleveland Airport. At this time the flight acknowledged receipt of a weather report from Toledo, Ohio, to the effect that light thunderstorms with cloud to cloud lightning were moving northeasterly from Toledo. At 2013 the flight reported at 4,000 feet over Mansfield, Ohio, 58 miles south southwest of Cleveland. The crew stated that they had changed course to the south to avoid thunderstorms, and intended to proceed to Columbus, Ohio, in accordance with visual flight rules. A special weather observation taken at Cleveland at 2003 which reported a ceiling of 2,000 feet, visibility 10 miles, light rain, wind from the northwest at 30 miles per hour with strong gusts, and cloud to cloud and cloud to ground lightning was transmitted to the flight Cleveland Radio also transmitted a weather observation taken at Columbus at 1930 which reported an unlimited ceiling, visibility of 15 miles, and wind from the south at 14 miles per hour. After acknowledging receipt of this weather information, the flight stated "For your information advise no one to go through the turbulence we just went through." The next position report was received at 2032 at which time the flight reported being five miles north of Columbus. Following this report it was cleared by Columbus Tower for landing. In reply the flight stated to the tower, "We are declaring an emergency. Our rudder is locked, and I don’t think we will have any directional control on the ground." A landing approach was made for runway twenty-three, 4,490 feet long. Information concerning wind direction and velocity was transmitted repeatedly by the tower to the flight throughout the course of the approach. Although the first touchdown on runway 23 appeared normal, power was immediately applied and the aircraft took off. The crew then informed the tower that they wished to land directly into the wind, which at that time was from the south at five to ten miles per hour. They were accordingly cleared to land on runway eighteen, 3,580 feet long. The second approach appeared normal, and a touchdown was made on the runway without any apparent difficulty, but power was again applied and the flight took off again. When the flight reached a point 2 1/2 miles east of the field in its left circle of the field, it was observed to spin to the ground. Flames were observed immediately after the crash.
Probable cause:
The Board determines that the probable cause of this accident was the in-flight failure of the fuselage carry-in structure beneath the fin, due to extreme turbulence.
The following factors were considered as contributory:
- The aircraft was flown through severe turbulence approximately one-half hour before the accident,
- The rivets and fuselage skin immediately beneath the vertical fin failed during flight,
- The separation of the fuselage skin allowed the vertical fin to rock across its longitudinal axis until the fuselage carry-in structure beneath the fin failed completely,
- The failure of the vertical fin caused loss of control of the aircraft, and it crashed.
Final Report:

Crash of a North American TB-25J-25-NC Mitchell in Mt Magazine: 6 killed

Date & Time: Nov 17, 1947
Operator:
Registration:
44-30007
Flight Phase:
Flight Type:
Survivors:
No
Site:
Schedule:
Chicago – Barksdale
MSN:
108-33282
Crew on board:
6
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
6
Circumstances:
While cruising in a thunderstorm area, the aircraft went out of control and crashed in Mt Magazine, about five miles northwest of Havana, Arkansas. All six crew members were killed.

Crash of a Douglas DC-6 in Gallup

Date & Time: Nov 11, 1947
Type of aircraft:
Operator:
Registration:
NC90741
Survivors:
Yes
Schedule:
San Francisco – Chicago
MSN:
43046
YOM:
1947
Crew on board:
5
Crew fatalities:
Pax on board:
20
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
9747
Captain / Total hours on type:
435.00
Copilot / Total flying hours:
3572
Copilot / Total hours on type:
417
Aircraft flight hours:
142
Circumstances:
Enroute from San Francisco to Chicago, the crew informed ATC that a fire erupted in the rear compartment of the aircraft and decided to divert to Gallup Airport for an emergency landing. The aircraft was difficult to maneuver and landed in flames. After it came to a halt, all 25 occupants were quickly disembarked and helped by local rescuers before the aircraft being totally destroyed by fire.
Probable cause:
The Board determines that the probable cause of these accidents was the combustion of gasoline which had entered the cabin heater combustion air intake scoop from the No 3 alternate tank vent due to inadvertent overflow during the transfer of fuel from the No 4 alternate tank.
The failure of the manufacturer and the Civil Aeronautics Administration to exercise full caution in the analysis of the fuel system of the DC-6 relative to proper location of fuel tank vents to provide non-hazardous location for fuel drainage, as required by existing regulations, and the insufficient attentiveness on the part of the manufacturer, the Civil Aeronautics Administration, and the air carriers to the procedures of fuel management employed by pilots operating DC-6 aircraft, were contributing factors.
This case was categorized as similar as the United Airlines' DC-6 that crashed in Bryce Canyon on October 24, 1947, killing all 52 occupants.
Final Report:

Crash of a Douglas C-50A-DO near Michigan City: 2 killed

Date & Time: Dec 28, 1946 at 0919 LT
Type of aircraft:
Operator:
Registration:
NC15577
Flight Phase:
Survivors:
Yes
Schedule:
Buffalo – Detroit – Chicago
MSN:
4805
YOM:
1941
Flight number:
AA2207
Crew on board:
3
Crew fatalities:
Pax on board:
18
Pax fatalities:
Other fatalities:
Total fatalities:
2
Captain / Total flying hours:
3559
Captain / Total hours on type:
3550.00
Copilot / Total flying hours:
2000
Copilot / Total hours on type:
1000
Aircraft flight hours:
11920
Circumstances:
This flight originated at Buffalo and proceeded uneventfully to a scheduled stop at Detroit, Michigan. Departure from Detroit was at 0748, about six minutes behind schedule, with eighteen passengers, 550 gallons of fuel and on an instrument flight plan to cruise at 2,500 feet sea level. Routine position reports were made at 0800, 0807 and 0822. At 0840 the flight was instructed by Air Route Traffic Control at Chicago to climb to 4,000 feet sea level which it did immediately. At 0859 Chicago Air Route Traffic Control cleared the flight from South Bend, Indiana, to the Chicago Tower to maintain 4,000 feet sea level until ten minutes after passing South Bend. At 0902 the flight reported passing South Bend. There were no further radio contacts with the flight until 0918 when it transmitted, "Both engines going bad descending at 1,000 feet per minute looking for opening." This was followed almost immediately by, "Altitude is at present 900 feet." Chicago immediately replied, "Suggest proceed to South Bend immediately if able." This was not acknowledged. The plane crashed at or about that time in the northeastern part of Michigan City at a point approximately two miles from Lake Michigan. The direction of Initial impact was just south of east or about opposite the course from Detroit to Chicago.
Probable cause:
The probable cause of this accident was the accumulation of carburetor ice following the loss of power in both engines as a result of fuel starvation. The reason for fuel starvation has not been determined.
Final Report:

Crash of a Douglas C-53D-DO in Cleveland: 2 killed

Date & Time: Nov 11, 1946 at 0330 LT
Operator:
Registration:
NC19947
Survivors:
Yes
Schedule:
Chicago – Cleveland
MSN:
4873
YOM:
1942
Flight number:
UA404
Location:
Crew on board:
3
Crew fatalities:
Pax on board:
18
Pax fatalities:
Other fatalities:
Total fatalities:
2
Captain / Total flying hours:
8340
Captain / Total hours on type:
967.00
Copilot / Total flying hours:
2268
Copilot / Total hours on type:
116
Aircraft flight hours:
11684
Circumstances:
The aircraft was heard southwest of the airport at 0327 and at this time Cleveland Tower cleared the flight to land on Runway 36-Left. At 0328 the air-craft was observed over the airport at an altitude of between 200 and 400 feet flying In a northeasterly direction. When approximately over the north boundary, the aircraft disappeared from view in what appeared to be a low cloud formation. At this time Cleveland Tower advised the flight that It was cleared to use Runway 36-Left, Runway 36-Right, or Runway 31, at the captain's discretion. The aircraft was next seen re-approaching the airport from the northeast in a right turn, during which turn the landing lights were switched on. In the latter part of the turn, a descent was established and this descent was continued in a northwesterly direction toward the dark, undeveloped area north of the airport. With the exception of the fact that the aircraft was heading toward an area not within the boundary of the airport, its appearance was that of an aircraft in a normal landing approach. When at an altitude of approximately 30 feet, the aircraft banked slightly to the left and, immediately thereafter it struck trees and high tension lines paralleling the north boundary of the airport. The aircraft veered sharply to the right and dived into the ground, coming to rest approximately 550 feet beyond the point of initial contact.
Probable cause:
On the basis of the foregoing, the Board determines that the probable cause of this accident was the error of the pilot in establishing an approach toward an area not cleared for landing as a result of having mistaken the end markers of Runway 23 for those of Runway 31. A contributing factor was the failure of the pilot to abandon his attempt to land at Cleveland Airport when confronted with weather conditions below the minimums prescribed for that airport.
Final Report:

Crash of a Douglas C-47-DL in Moline: 2 killed

Date & Time: Aug 21, 1946 at 0419 LT
Registration:
NC51878
Survivors:
Yes
Schedule:
Chicago – Omaha
MSN:
4542
YOM:
1942
Crew on board:
3
Crew fatalities:
Pax on board:
22
Pax fatalities:
Other fatalities:
Total fatalities:
2
Captain / Total flying hours:
2589
Copilot / Total flying hours:
3452
Copilot / Total hours on type:
1500
Aircraft flight hours:
4121
Circumstances:
The aircraft left Chicago Airport at 0303LT bound for Omaha on a charter flight with 22 passengers and a crew of three on board. Less than one hour into the flight, while cruising at an altitude of 4,000 feet via the route Green 3, a small explosion occurred in the left engine, forcing the crew to shut this engine down and to feather the propeller. The captain informed ATC of his situation and obtained the permission to divert to Moline Airport located 35 miles from his position. On final approach to runway 22, the captain realized that his position to the runway centerline was wrong and elected to make a go around. With undercarriage and flaps down, he made a turn to the left when the left wing tip hit the ground, causing the aircraft to crash in a field. Both pilots were killed while 23 other occupants were injured, some of them seriously. The aircraft was destroyed.
Probable cause:
On the basis of the foregoing, the Board determines that the probable cause of the accident was the faulty execution of an emergency single engine approach following failure of the left engine in flight. A contributing factor was the failure of the pilot to exercise sufficient caution by having, a qualified mechanic determine the reasons for oil leakage in the left engine prior to departure from Chicago. Investigations revealed that the failure of the left engine was caused by a fracture of the cylinder number 5.
Final Report:

Crash of a Douglas C-47B-1-DL in Blue Mounds: 4 killed

Date & Time: Nov 25, 1944 at 2350 LT
Operator:
Registration:
43-16407
Flight Phase:
Flight Type:
Survivors:
No
Site:
Schedule:
Chicago – Minneapolis
MSN:
20873
YOM:
1944
Crew on board:
4
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
4
Circumstances:
While cruising by night bound for Minneapolis, the crew encountered poor weather and icing conditions. Unable to maintain a sage height, the captain decided to descend at 2,000 feet and elected to return to Chicago when the aircraft hit a mountain slope (1,716 feet high) located in Blue Mounds. All four crew members were killed.

Crash of a Consolidated B-24E-1-DT Liberator in Merna: 10 killed

Date & Time: Apr 29, 1944
Operator:
Registration:
41-28413
Flight Phase:
Flight Type:
Survivors:
No
Site:
Schedule:
Chicago – Denver
MSN:
5
Location:
Crew on board:
10
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
10
Circumstances:
En route, while overflying Nebraska, the aircraft went out of control and crashed in a canyon located some 15 miles southwest of Merna. All 10 occupants were killed.