Country
Operator Image

Crash of a Boeing 707-138B in Vancouver: 2 killed

Date & Time: Feb 7, 1968 at 0558 LT
Type of aircraft:
Operator:
Registration:
N791SA
Survivors:
Yes
Schedule:
Honolulu - Vancouver
MSN:
17698
YOM:
1959
Flight number:
CP322
Country:
Crew on board:
9
Crew fatalities:
Pax on board:
52
Pax fatalities:
Other fatalities:
Total fatalities:
2
Copilot / Total hours on type:
344
Circumstances:
The approach to Vancouver Airport was completed in poor visibility due to foggy conditions. Following a wrong approach configuration, the aircraft landed 1,000 feet past the runway threshold and to the right of the centerline. After touchdown, the captain decided to make a go-around when control was lost. The airplane veered off runway to the right, went through the tarmac and eventually collided with a terminal building. Seventeen occupants were injured while 43 others were unhurt. The copilot and one person in the terminal were killed. The aircraft was considered as damaged beyond repair. At the time of the accident, the horizontal visibility was limited to 200 meters due to fog with strong winds.
Probable cause:
It was determined that the approach configuration on part of the flying crew was wrong. At the time of the accident, both pilots were on duty since more than 21 hours and their concentration and performances were diminished due to intense fatigue. It was reported that the approach speed was too high while the rate of descent was too low.

Crash of a Douglas DC-8-43 in Tokyo: 64 killed

Date & Time: Mar 4, 1966 at 2015 LT
Type of aircraft:
Operator:
Registration:
CF-CPK
Survivors:
Yes
Schedule:
Hong Kong – Tokyo – Vancouver
MSN:
45761
YOM:
1965
Flight number:
CP402
Country:
Region:
Crew on board:
10
Crew fatalities:
Pax on board:
62
Pax fatalities:
Other fatalities:
Total fatalities:
64
Captain / Total flying hours:
26564
Captain / Total hours on type:
4089.00
Copilot / Total flying hours:
19789
Copilot / Total hours on type:
3071
Aircraft flight hours:
1792
Circumstances:
Flight 402 was a scheduled international flight from Hong Kong to Tokyo and Vancouver. It took off from Hong Kong at 1614 hours Japan Standard Time and was routed via Taipei, Kagoshima and Ohshima. At 1908 hours it flew over "Spencer Victor" at 25 000 ft and started to descend gradually; at 1912 hours it crossed "Rice Victor" at 18 000 it and two minutes later entered the Kisarazu holding pattern at 14 000 ft where it waited for an improvement of the weather conditions at Tokyo International Airport (TIA). At 1942 hours the flight notified Tokyo air traffic control that if the weather conditions failed to improve within 15 minutes, it would divert to Taipei (alternate airport). Ten minutes later, at 1952 hours the flight was advised by Tokyo ATC that the RVR was 2 400 ft and the pilot then asked for a clearance for approach and landing. The approach clearance was given and the aircraft proceeded to descend to 3 000 ft, in the holding pattern. However, the weather conditions at TIA worsened and the aircraft did not proceed with the approach. The pilot requested a clearance to divert to Taipei at 1958 hours and commenced climbing. At 2005 hours, while heading for Tateyama en route to Taipei the flight was advised by Tokyo air traffic control that visibility at TIA had improved to 4 mile with RVR 3 000 ft. Consequently, the pilot requested a clearance to return to Kisarazu and began descending from 11 500 ft. At 2011 hours the aircraft arrived over Kisarazu at 3 000 ft and began another approach under instructions of the GCA. At this time the flight was quite normal. When the aircraft was 8 NM from touchdown at an altitude of 1 500 ft, it was advised that there was a light tailwind 150015 kt and was cleared to land on runway 33R. The rate of descent for final approach was begun about 5.3 NM from touchdown at approximately 2012:58 hours. The aircraft was on course and on the glide path with a ground speed of approximately 174 kt, gradually decreasing to approximately 140 kt at 2 NM and 114 kt after passing 1 NM. When the aircraft reached one mile from touchdown, the GCA final controller noted that the aircraft was slightly below the GCA glide path and advised "20 ft low, level off momentarily". Nevertheless, the aircraft continued its approach 20 ft below and in parallel with the GCA glide path. After the aircraft passed the P.M. (precision minimum), the aircraft requested the intensity of the lights to be reduced. Shortly thereafter, the aircraft made a sharp descent and its main landing gear wheel struck No. 14 approach light 2 800 ft from touch- down point approximately in an attitude of level flight. Following this first contact, the aircraft struck the approach lights one by one until No. 3 damaging or destroying them, and at approximately 2015 hours crashed against the sea wall with the bottom of the fore-fuselage. Then, the aircraft was thrown over near the end of runway 33R, destroyed and caught fire. All 10 crew members and 54 passengers were killed while eight others were injured.
Probable cause:
The pilot misjudged landing approach under unusually difficult weather conditions. The visibility at Tokyo International Airport was reduced at the time of landing to less than half a mile by fog and smoke, RVR was in the order of 3 000 it. The aircraft carried out a GCA approach to runway 33R under very difficult conditions. It was considered that the approach was normal until a point located between 3 900 and 3 600 ft before the touchdown point. It then entered a steep rate of descent between 3 900 and 3 600 it before the touchdown point, it first struck an approach light 2 800 ft from the touchdown point in an attitude of level flight, then broke several approach light piers and crashed against the sea wall of the airport. The wreckage was thrown over the sea wall near the runway threshold and completely destroyed by the ensuing fire. The steep rate of descent was considered to be the result of an intentional manoeuvre of the aircraft by the pilot-in-command with a view to executing a final approach at a lower altitude than normal. Although no certain cause for the excessive descent which led to striking the approach lights could be determined, it was considered that the poor visibility due to illusive fog conditions that night misled the pilot-in-command in his judgement.
Final Report:

Crash of a Douglas DC-6B near Hundred Mile House: 52 killed

Date & Time: Jul 8, 1965 at 1541 LT
Type of aircraft:
Operator:
Registration:
CF-CUQ
Flight Phase:
Survivors:
No
Schedule:
Vancouver – Prince George – Fort Saint John – Fort Nelson – Watson Lake – Whitehorse
MSN:
43844
YOM:
1953
Flight number:
CP021
Country:
Crew on board:
6
Crew fatalities:
Pax on board:
46
Pax fatalities:
Other fatalities:
Total fatalities:
52
Captain / Total flying hours:
13218
Captain / Total hours on type:
2690.00
Copilot / Total flying hours:
2657
Copilot / Total hours on type:
982
Aircraft flight hours:
29998
Circumstances:
Flight 21 was a scheduled domestic flight from Vancouver, British Columbia, to Whitehorse, Yukon Territory via Prince George, Fort St. John, Fort Nelson in British Columbia and Watson Lake, Yukon Territory. At 1442 hours PST, the aircraft took off on an instrument flight plan for Prince George, via Victor 300 and Blue 22 airways. In the vicinity of Hope, north-bound on Blue 22 airway, it was sighted by CPA Flight 22 and communication was established. Shortly afterwards at 1517 hours Flight 21 requested and received clearance to proceed from its position north of Hope direct to Williams Lake, which track would pass to the west of Ashcroft. At 1529 hours, it reported to the Vancouver Air Traffic Control Centre that it had passed Ashcroft at 1527 hours at 16 000 ft and was estimating William Lake at 1548 hours. This transmission was acknowledged by the Vancouver Centre. At 1538 hours, Vancouver Centre called Flight 21 and did not receive a reply. About two minutes later, three "mayday" calls were heard by Vancouver Centre. At approximately the same time a four-engined aircraft, subsequently identified as Flight 21, was observed by witnesses flying in the clear over the Gustafson Lake area about 20 miles west of 100 Mile House, B.C. The aircraft appeared to be in normal flight when an explosion was heard, following which smoke was observed and the tail separated from the fuselage. The main portion of the wreckage assumed a nose down attitude and spiraled to the left until it crashed into a wooded area about 4.5 miles north of Gustafson Lake. The accident occurred at 1541 hours. There were no survivors among the 52 occupants.
Probable cause:
Explosion of a device which resulted in aerial disintegration.
Final Report:

Crash of a Bristol 175 Britannia 314 in Honolulu: 27 killed

Date & Time: Jul 22, 1962 at 2319 LT
Type of aircraft:
Operator:
Registration:
CF-CZB
Survivors:
Yes
Schedule:
Vancouver – Honolulu – Nadi – Auckland – Sydney
MSN:
13394
YOM:
1958
Flight number:
CP301
Location:
Crew on board:
11
Crew fatalities:
Pax on board:
29
Pax fatalities:
Other fatalities:
Total fatalities:
27
Captain / Total flying hours:
13250
Captain / Total hours on type:
920.00
Copilot / Total flying hours:
16073
Copilot / Total hours on type:
1628
Circumstances:
The aircraft had arrived in Honolulu at 0507 hours Hawaiian standard time on 21 July as CPA Flight 323 from Vancouver, British Columbia, Canada. It was departing, the evening of 22 July, as Empress Flight 301 on a scheduled international flight for Nadi (Fiji Islands), Auckland (New Zealand) and Sydney (Australia). The night takeoff was commenced at 22:38 hours local time and approximately two minutes after becoming airborne and during the climbout a fire warning indication for No 1 engine was received in the cockpit. The No. 1 propeller was feathered and the tower controller was advised that the aircraft was returning to Honolulu. As an over-gross landing weight condition existed, fuel jettisoning in the amount of 35000 lb was carried out The jettisoning operation was completed at 23:06 hours following which the flight was vectored west of the outer marker to Intercept the ILS final approach course for runway 08. The three-engine landing approach appeared normal until the aircraft had proceeded beyond the runway threshold and had commenced its landing flare at an altitude of approximately 20 feet above the runway centreline. A go-around was attempted from this position, and the aircraft banked and veered sharply to the left. Initial ground contact was made by the left wing tip approximately 550 feet to the left of the runway centreline and approximately 700 feet beyond the threshold of the runway. The aircraft progressively disintegrated as it moved across the ground, then struck heavy earth-moving equipment parked approximately 970 feet from the runway centreline.
Probable cause:
The attempted three-engine go-around, when the aircraft was in a full landing configuration, at insufficient airspeed and altitude to maintain control.
Final Report:

Crash of a Douglas DC-6B in Cold Bay: 15 killed

Date & Time: Aug 29, 1956 at 2045 LT
Type of aircraft:
Operator:
Registration:
CF-CUP
Survivors:
Yes
Schedule:
Vancouver – Cold Bay – Tokyo – Hong Kong
MSN:
43843
YOM:
1953
Flight number:
CP307
Location:
Crew on board:
8
Crew fatalities:
Pax on board:
14
Pax fatalities:
Other fatalities:
Total fatalities:
15
Captain / Total flying hours:
9522
Captain / Total hours on type:
2906.00
Copilot / Total flying hours:
12782
Copilot / Total hours on type:
465
Aircraft flight hours:
10513
Circumstances:
Flight 307 departed Vancouver, British Columbia at 1347 Bering standard time en route to Hong Kong, China, with a refueling stop at Cold Bay, Alaska and an intermediate stop at Tokyo, Japan, carrying a crew of 8 and 14 passengers. At 2011 the flight reported 100 miles out, estimating Cold Bay at 2036. It reported being over the Cold Bay range station outbound on a standard instrument approach at 2035, and at 2042 as completing a procedure turn and proceeding inbound. This was the last transmission from the flight. At 2045 the aircraft was observed to descend from the overcast north of the airport for a landing on runway 14 and cross the field at low altitude to the intersection of the two runways. At this point a shallow left turn was started and the aircraft went out of sight southeast of the airport. Shortly afterwards a fire was observed and it was ascertained that the aircraft had crashed. Eleven passengers and 4 crew members were fatally injured. The aircraft was destroyed by impact forces and a post crash fire.
Probable cause:
The probable cause of this accident was the full retraction of the wing flaps at low altitude during a circling approach without necessary corrective action being taken by the crew. Considering that very little altitude was gained after the application of power it is probable that a circling approach had been decided upon when the left turn from runway 14 was made. Since the wing flaps during the circling approach would be extended 20 degrees, and since they were found in the fully retracted position, it is believed that they were retracted shortly before impact. Fully retracted wing flaps at this time would explain the feeling of experienced by the off-duty flight crew member.
Final Report:

Crash of a Consolidated PB2B-1 Canso off Prince Rupert: 2 killed

Date & Time: May 11, 1953
Type of aircraft:
Operator:
Registration:
CF-CRV
Survivors:
Yes
Schedule:
Sandspit – Prince Rupert
MSN:
21984
YOM:
1943
Country:
Crew on board:
3
Crew fatalities:
Pax on board:
16
Pax fatalities:
Other fatalities:
Total fatalities:
2
Circumstances:
The seaplane bounced on landing off Prince Rupert, plunged into the water and came to rest, broken in two. A pilot and a passenger were killed while 17 other occupants were injured. The aircraft sank but was later recovered. Written off.
Probable cause:
It would appear that through misuse of the controls in the air after the aircraft touched down on the water, it bounced several times, the final bounce being so severe that the nose section was torn off.

Crash of a De Havilland DH.106 Comet 1A in Mauripur: 11 killed

Date & Time: Mar 3, 1953 at 0335 LT
Type of aircraft:
Operator:
Registration:
CF-CUN
Flight Phase:
Flight Type:
Survivors:
No
Schedule:
London – Rome – Beirut – Karachi – Yangon – Jakarta – Darwin – Sydney
MSN:
6014
YOM:
1952
Country:
Region:
Crew on board:
5
Crew fatalities:
Pax on board:
6
Pax fatalities:
Other fatalities:
Total fatalities:
11
Aircraft flight hours:
51
Circumstances:
The crew (five flying crew and six De Havilland engineers) were conducting a demo flight from London to Sydney to show this new jetliner to potential clients in Southeast Asia and Oceania. While taking off from runway 25 (2,500 meters long) at Mauripur Airbase, the airplane failed to get airborne, overran, hit several obstacles, went through a perimeter fence and eventually crashed in flames in a small river. The aircraft was destroyed by a post crash fire and all 11 occupants were killed.
Probable cause:
The accident was caused by the fact that the nose of the aircraft was lifted too high during the takeoff run, resulting in a partially stalled condition and excessive drag. This did not permit normal acceleration and prevented the aircraft from becoming airborne within the prescribed distance. The pilot appears to have realised that the nose was excessively high and took corrective action, but this was done too late to prevent the aircraft striking an obstruction immediately beyond the perimeter fence before it became airborne. The following factor was considered as contributory: the pilot, who had only limited experience in the Comet aircraft, elected to takeoff at night at the maximum permissible takeoff for the prevailing conditions. The circumstances required strict adherence to the prescribed takeoff technique, which was not complied with.

Crash of a Douglas C-54A-10-DC into the Pacific Ocean: 37 killed

Date & Time: Jul 21, 1951 at 2255 LT
Type of aircraft:
Operator:
Registration:
CF-CPC
Flight Phase:
Survivors:
No
Schedule:
Vancouver – Anchorage – Tokyo
MSN:
10327
YOM:
1944
Country:
Region:
Crew on board:
6
Crew fatalities:
Pax on board:
31
Pax fatalities:
Other fatalities:
Total fatalities:
37
Circumstances:
The four engine aircraft left Vancouver at 1853LT bound for Tokyo-Haneda with an intermediate stop in Elmendorf AFB in Anchorage. While cruising along the Alaskan shore, vertical to the Cape Spencer, near Elfin Cove, the crew informed ground about his position and gave an estimate about 0000LT vertical to Yakutat. This was the last message as the airplane disappeared few minutes later. As the aircraft failed to arrive in Anchorage, SAR operations were conducted but no trace of the aircraft nor the 37 occupants was found. All operations were eventually suspended on October 31, 1951.
Probable cause:
As no trace of the aircraft was found, the board was unable to determine conclusively the cause of the accident. At the time of the accident, weather conditions were poor with rain falls, icing conditions and a visibility of 500 feet.
Final Report:

Crash of a Douglas C-47A-20-DK near Penticton: 2 killed

Date & Time: Dec 22, 1950 at 1353 LT
Operator:
Registration:
CF-CUF
Survivors:
Yes
Site:
Schedule:
Vancouver – Penticton
MSN:
12855
YOM:
1944
Flight number:
CP004
Country:
Crew on board:
3
Crew fatalities:
Pax on board:
15
Pax fatalities:
Other fatalities:
Total fatalities:
2
Circumstances:
The approach to Penticton was started in marginal weather conditions when the aircraft hit several trees. While contacting trees, the left wing was sheared off, the aircraft rotated to the left and crashed in a snow covered and wooded area located on the Mt Okanagan, about 27 km north of the Penticton Airport. Sixteen occupants were evacuated, some of them were injured. Unfortunately, both pilots were killed in the accident.
Probable cause:
It was determined that the crew started the descent prematurely, causing the aircraft to fly below the minimum safe altitude of 6,500 feet fixed to clear the Mt Okanagan. The aircraft struck Okanagan Mountain as a result of being below the minimum altitude permissible when passing through the Greata fan marker during an instrument approach procedure on the Penticton Radio Range.

Crash of a Canadair C-4 North Star in Tokyo

Date & Time: Feb 9, 1950
Type of aircraft:
Operator:
Registration:
CF-CPR
Survivors:
Yes
Schedule:
Vancouver – Tokyo
MSN:
148
YOM:
1949
Country:
Region:
Crew on board:
5
Crew fatalities:
Pax on board:
10
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
After touchdown in Haneda Airport, the four engine aircraft christened 'Empress of Vancouver' encountered difficulties to stop. It overran and eventually plunged into the bay of Tokyo. All 15 occupants were quickly rescued while the aircraft was lost.