Ground accident of a De Havilland DHC-8-402Q Dash-8 in Xi'an

Date & Time: Dec 7, 2002
Operator:
Registration:
B-3567
Flight Phase:
Flight Type:
Survivors:
Yes
MSN:
4005
YOM:
2000
Location:
Country:
Region:
Crew on board:
2
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
Two engineers took over the airplane for an engine test run at Xi'an Airport. While parked on the apron, the aircraft started to roll on a slippery ground and eventually collided with the main terminal. Both occupants escaped uninjured while the aircraft was damaged beyond repair. It was reported that snow fell during the preceding days and that the tarmac was slippery.

Crash of a Caudron C.635 Simoun in Roanne: 1 killed

Date & Time: Sep 6, 2002 at 0930 LT
Type of aircraft:
Operator:
Registration:
F-AZAM
Flight Phase:
Flight Type:
Survivors:
No
Schedule:
Roanne - Roanne
MSN:
7863
YOM:
1937
Location:
Country:
Region:
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
1
Captain / Total flying hours:
3219
Captain / Total hours on type:
193.00
Circumstances:
The pilot, sole on board, was completing a post maintenance check flight after the engine was subject to several modifications. After takeoff from Roanne-Renaison Airport, while climbing to a height of 300 feet, the pilot initiated a left turn in a relative flat attitude and followed a perpendicular trajectory from the runway. Suddenly, it collided with a weather pylon (8 meters high), overturned and crashed, bursting into flames. The aircraft was destroyed and the pilot was killed.
Probable cause:
The exact cause of the accident could not be determined with certainty. However, it was reported that the engine was running at near full power at the time of impact.
Final Report:

Crash of a Shaanxi Y-8B in Colombo: 5 killed

Date & Time: Aug 15, 2002 at 1235 LT
Type of aircraft:
Operator:
Registration:
CR-873
Flight Phase:
Flight Type:
Survivors:
No
Schedule:
Colombo - Colombo
MSN:
07 08 02
YOM:
1993
Country:
Region:
Crew on board:
5
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
5
Circumstances:
The crew departed Colombo-Ratmalana Airport for a local post maintenance test flight as one of the engine has been changed. During climbout, an engine caught fire. The crew was cleared to return for an emergency landing when the engine exploded and separated from the aircraft. Out of control, the airplane crashed in an open field, bursting into flames. All five crew members were killed. It was reported that the engine that caught fire was not the one that has been changed.
Probable cause:
Engine fire and explosion for unknown reasons.

Crash of a Rockwell Shrike Commander 500S in Fortaleza

Date & Time: Jul 2, 2002 at 1640 LT
Operator:
Registration:
PT-KZD
Flight Phase:
Flight Type:
Survivors:
Yes
Site:
Schedule:
Fortaleza - Fortaleza
MSN:
500-3140
YOM:
1972
Country:
Crew on board:
1
Crew fatalities:
Pax on board:
2
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
8000
Captain / Total hours on type:
2900.00
Aircraft flight hours:
9960
Circumstances:
The twin engine aircraft departed Fortaleza-Pinto Martins Airport on a local post maintenance test flight (50 hours), carrying two passengers and one pilot. After takeoff, while climbing to a height of 200 feet, the power on the left engine fluctuated. The pilot modified the position of the fuel selector but the situation did not change. As the aircraft was losing height, the pilot shut down the left engine and feathered its propeller when the aircraft rolled to the left, causing the left wing to struck a concrete wall. Out of control, the aircraft struck the roof of a house, then a second one and eventually crashed on a third residence. All three occupants were injured as well as one people on the ground.
Probable cause:
The fuel pump and the servo-injectors had faults which certainly contributed to the accident as the left engine was not properly supplied with fuel.
Final Report:

Crash of a Douglas DC-3A-197D in Laredo

Date & Time: May 21, 2002 at 1100 LT
Type of aircraft:
Operator:
Registration:
XB-JBR
Flight Phase:
Flight Type:
Survivors:
Yes
Schedule:
Laredo - Laredo
MSN:
3261
YOM:
1940
Location:
Crew on board:
3
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
The crew was completing a local post maintenance test flight at Laredo Airport. After several touch-and-goes, the aircraft was in initial climb when the left engine lost power, followed shortly later by the right engine. The crew reduced his altitude and ditched the aircraft in the Casa Blanca Lake, about 50 feet from the shore. All three crew members were evacuated safely while the aircraft sank in six feet of water.

Crash of a Boeing 307 Stratoliner in Seattle

Date & Time: Mar 28, 2002 at 1310 LT
Type of aircraft:
Operator:
Registration:
NC19903
Flight Type:
Survivors:
Yes
Schedule:
Seattle - Seattle
MSN:
2003
YOM:
1940
Crew on board:
4
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
15000
Captain / Total hours on type:
62.00
Aircraft flight hours:
20577
Circumstances:
The crew had originally planned to practice landings at an airport about 20 minutes away, then stop, refuel the airplane, and subsequently return to the original departure airport. Prior to the flight, the crew discussed fuel endurance, which was calculated to be 2 hours based on the captain's knowledge of the airplane's fuel consumption, and the quantity of fuel indicated on the gauges. The fuel tanks were not dipped. The flight was made at 1,500 feet msl. Upon reaching the practice airport, the crew conducted one full stop landing, then taxied back for takeoff. During takeoff, an engine had a momentary overspeed, and the crew decided to return to the original departure airport without refueling. Approaching the original departure airport, the airplane had to delay landing for about 7 minutes for a manual gear extension. Upon completion, it turned back toward the airport, and was about 6 miles from the runway when fuel pressure for one of the engines dropped. The boost pumps were turned on; however, the engine lost power. A low fuel pressure light then illuminated for another engine. The captain called for the flight engineer to switch fuel feed to another tank, but the flight engineer responded, "we're out of fuel." The remaining engines subsequently lost power, and the captain ditched the airplane into a bay. The time from first takeoff until ditching was 1 hour, 19 minutes. The airplane had flown 39 hours since restoration, and exact fuel capacities, fuel flow calculations and unusable fuel amounts had not been established. A dipping chart had been prepared, with one person in the cockpit and one person with a yardstick putting fuel in a main tank in 25-gallon increments. However, the data had not been verified, and dipping was not considered to be part of the pre-flight inspection.
Probable cause:
Loss of all engine power due to fuel exhaustion that resulted from the flight crew's failure to accurately determine onboard fuel during the pre-flight inspection. A factor contributing to the accident was a lack of adequate crew communication regarding the fuel status.
Final Report:

Ground accident of an Airbus A300B2-101 in New Delhi

Date & Time: Mar 8, 2002 at 0315 LT
Type of aircraft:
Operator:
Registration:
VT-EFW
Flight Phase:
Flight Type:
Survivors:
Yes
MSN:
111
YOM:
1980
Country:
Region:
Crew on board:
5
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
A group of five technicians/engineers of the company was preparing the aircraft to be transferred to a hangar for maintenance. After engine startup, the power was reduced to idle after someone inadvertently pulled out the circuit breaker. The aircraft jumped the chocks and started to roll. Since the engine's power was in idle, the brakes and the nosewheel steering system were inoperative. The crew elected to reduce power on the left engine but mistakenly increased the power on the right engine by 90%. This caused the aircraft to rotate 80° when control was lost. The airplane rolled through a perimeter wall, causing the nose gear to collapse. All five occupants escaped uninjured while the aircraft was damaged beyond repair.

Crash of a Learjet 25D in Salina

Date & Time: Jun 12, 2001 at 1300 LT
Type of aircraft:
Operator:
Registration:
N333CG
Flight Type:
Survivors:
Yes
Schedule:
Newton - Salina
MSN:
25-262
YOM:
1978
Location:
Crew on board:
2
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
19000
Captain / Total hours on type:
1500.00
Copilot / Total flying hours:
5168
Copilot / Total hours on type:
470
Aircraft flight hours:
8419
Circumstances:
During a test flight, the airplane encountered an elevator system oscillation while in a high speed dive outside the normal operating envelope. The 17 second oscillation was recorded on the cockpit voice recorder and had an average frequency of 28 Hz. The aft elevator sector clevis (p/n 2331510-32) fractured due to reverse bending fatigue caused by vibration, resulting in a complete loss of elevator control. The flight crew reported that pitch control was established by using horizontal stabilizer pitch trim. The flightcrew stated that during final approach to runway 17 (13,337 feet by 200 feet, dry/asphalt) the aircraft's nose began to drop and that the flying pilot was unable to raise the nose using a combination of horizontal stabilizer trim and engine power. The aircraft landed short of the runway, striking an airport perimeter fence and a berm. The surface winds were from the south at 23 knots, gusting to 32 knots.
Probable cause:
The PIC's delayed remedial action during the elevator system oscillation, resulting in the failure of the aft elevator sector clevis due to reverse bending fatigue caused by vibration, and subsequent loss of elevator control. Factors contributing to the accident were high and gusting winds, the crosswind, the airport perimeter fence, and the berm.
Final Report:

Crash of a Casa-Nurtanio CN235-100M (IPTN) in Ankara: 4 killed

Date & Time: May 18, 2001
Operator:
Registration:
TCSG-552
Flight Phase:
Flight Type:
Survivors:
No
Schedule:
Ankara - Ankara
MSN:
C-153
YOM:
2000
Country:
Region:
Crew on board:
4
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
4
Circumstances:
The crew was engaged in a local test flight at Ankara-Mürted AFB. Shortly after takeoff, while climbing to a height of about 100 feet, the aircraft went out of control and crashed, bursting into flames. All four crew members were killed. According to Turkish Authorities, this aircraft was the last of a series of eight CN-235 intended for the Turkish Navy and was still operated under the Turkish Coast Guard, taking part to a certification program. Several modifications have been made on this model by technicians from Turkish Aerospace Industries (TAI) and the crew consisted of four pilots, one Turkish and three Spanish from the Casa/EADS Consortium.
Probable cause:
In a report published at the end of June 2001, the Turkish and Spanish Authorities confirmed that despite the care taken in the quality control systems, the Turkish engineers were unable to detect a malfunction of the aileron control system probably stemming from an error made during the mounting. Despite the fact that the accident was attributable to the negligence of engineers at Turkish Aerospace Industries (TAI), investigators believe that the three accidents involving Casa CN-235s in Turkey in five months are likely to have resulted from three different causes.

Crash of an Antonov AN-70 in Omsk

Date & Time: Jan 27, 2001
Type of aircraft:
Operator:
Registration:
UR-NTK
Flight Phase:
Flight Type:
Survivors:
Yes
Schedule:
Omsk - Yakutsk
MSN:
77 01 02
YOM:
1997
Country:
Region:
Crew on board:
11
Crew fatalities:
Pax on board:
22
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
The aircraft departed Omsk Airport on a test flight to Yakutsk, carrying 22 passengers and a crew of 11 in order to perform a test flight in low-temperature flight conditions, as part of the Ukrainian manufacturer's certification program. During initial climb, at a height of 20 metres, the engine n°3 lost power. The crew increased power on all three other engines and continued to climb. Less than 25 seconds laters, at a height of about 60 metres, the engine n°1 failed. The captain attempted an emergency landing in a snow covered terrain located 660 metres past the runway end. The aircraft belly landed and came to rest with severe damages to the fuselage (almost broke in two at wings level) and engines. All 33 occupants were rescued, among them four were injured, two seriously.
Probable cause:
The loss of power on engine n°3 was the result of the rupture of a hydraulic line located near the rotor. This failure caused a reduction of the blades' rotation on both propellers (counter-rotating system), creating severe vibrations. The crew increased power on all three remaining engines when a technical malfunction occurred on an electric sensor coupled to the turbine of the engine n°1, causing the automatic control unit to fail and the engine n°1 to stop.