Crash of a Cessna 425 Conquest in Ronkonkoma: 3 killed

Date & Time: Dec 16, 1996 at 1840 LT
Type of aircraft:
Registration:
N425EW
Survivors:
No
Schedule:
Macon – Ronkonkoma
MSN:
425-0150
YOM:
1983
Crew on board:
1
Crew fatalities:
Pax on board:
2
Pax fatalities:
Other fatalities:
Total fatalities:
3
Captain / Total flying hours:
10846
Captain / Total hours on type:
2089.00
Circumstances:
The pilot had received clearance for the ILS Runway 6 approach and was advised that the previous landing traffic reported '...breaking out at minimums.' Radar data revealed that the airplane descended in instrument meteorological conditions to the decision height altitude of 294 feet, approximately 3 miles from the missed approach point. The pilot did not perform the missed approach procedure. The airplane leveled off and continued at or below decision height altitude for approximately 28 seconds, traveling a distance of approximately 1 mile. Four low altitude alerts appeared on the tower controller's display. The controller stated he withheld the alert because '...it was a critical phase of flight and the aircraft appeared to be climbing...' The airplane collided with trees and terrain approximately 1.5 miles from the approach end of the landing runway.
Probable cause:
The pilot's early descent to decision height and his failure to perform the missed approach procedure. A factor was the failure of air traffic control to issue a safety advisory.
Final Report:

Crash of a Gulfstream GIV in Chicago: 4 killed

Date & Time: Oct 30, 1996 at 1300 LT
Type of aircraft:
Operator:
Registration:
N23AC
Flight Phase:
Survivors:
No
Schedule:
Chicago - Burbank
MSN:
1047
YOM:
1988
Crew on board:
3
Crew fatalities:
Pax on board:
1
Pax fatalities:
Other fatalities:
Total fatalities:
4
Captain / Total flying hours:
17086
Captain / Total hours on type:
496.00
Aircraft flight hours:
2938
Aircraft flight cycles:
1219
Circumstances:
The flightcrew of a Gulfstream G-IV began taking off on Runway 34 with a crosswind from 280° at 24 knots. About 1,340 feet after the takeoff roll began, the airplane veered left 5.14° to a heading of 335°. It departed the runway, and tire marks indicated no braking action was applied. One of the pilots said, "Reverse," then one said, "No, no, no, go, go, go, go, go." The airplane traversed a shallow ditch that paralleled the runway, which resulted in separation of both main landing gear, the left and right flaps, and a piece of left aileron control cable from the airplane. The airplane became airborne after it encountered a small berm at the departure end of the runway. Reportedly, the left wing fuel tank exploded. The main wreckage was located about 6,650 feet from the start of the takeoff roll. Examination of the airplane indicated no preexisting anomalies of the engines, flight controls, or aircraft systems. The Nose Wheel Steering Select Control Switch was found in the "Handwheel Only" position, and not in the "Normal" position. The pilot-in-command (PIC) routinely flew with the switch in the "Normal" position. The PIC and copilot (pilot-not-flying) comprised a mix crew in accordance with an Interchange Agreement between two companies which operated G-IV's. The companies' operation manuals and the Interchange Agreement did not address mixed crews, procedural differences, or aircraft difference training.
Probable cause:
Failure of the pilot-in-command (PIC) to maintain directional control of the airplane during the takeoff roll in a gusty crosswind, his failure to abort the takeoff, and failure of the copilot to adequately monitor and/or take sufficient remedial action to help avoid the occurrence. Factors relating to the accident included the gusty crosswind condition, the drainage ditch, the flight crew's inadequate preflight, the Nose Wheel Steering Control Select Switch in the "Handwheel Only" position, and the lack of standardization of the two companies' operations manuals and Interchange Agreement.
Final Report:

Crash of a Dassault Falcon 10 in Offenburg: 4 killed

Date & Time: Aug 8, 1996 at 0940 LT
Type of aircraft:
Operator:
Registration:
D-CBUR
Survivors:
No
Schedule:
Munich - Offenburg
MSN:
98
YOM:
1977
Country:
Region:
Crew on board:
2
Crew fatalities:
Pax on board:
2
Pax fatalities:
Other fatalities:
Total fatalities:
4
Aircraft flight hours:
5797
Circumstances:
On approach to Offenburg Airport runway 02, the crew encountered limited visibility due to low clouds. Under VFR mode in IMC conditions, the crew failed to realize his altitude was too low when the aircraft collided with trees and crashed in a hilly terrain located about 7,2 km southeast of runway 02 threshold, near Friesenheim. The aircraft was destroyed by impact forces and a post crash fire and all four occupants were killed.
Probable cause:
Controlled flight into terrain after the crew continued the approach under VFR mode in IMC conditions until the aircraft impacted terrain.

Crash of a Gulfstream GII in Jos: 12 killed

Date & Time: Jun 20, 1996 at 0736 LT
Type of aircraft:
Operator:
Registration:
VR-BLJ
Survivors:
No
Schedule:
Kaduna - Jos
MSN:
40
YOM:
1968
Location:
Country:
Region:
Crew on board:
4
Crew fatalities:
Pax on board:
8
Pax fatalities:
Other fatalities:
Total fatalities:
12
Circumstances:
The crew was completing an executive flight from Kaduna to Jos, carrying four crew members and eight passengers, among them Colonel Mohammed Wase. On approach to Jos Airport, the crew encountered limited visibility due to marginal weather conditions when the aircraft collided with a telecommunication antenna and crashed, bursting into flames. The aircraft was totally destroyed and all 12 occupants were killed.
Probable cause:
The following findings were reported:
- The antenna has been recently installed by the company Nitel in a prohibited area,
- The crew was unable to see and avoid the obstacles due to poor weather conditions,
- The aircraft was not properly aligned on the approach path due to a wrong calibration of the Jos VOR by 10°.

Crash of a Beechcraft E90 King Air in Wiscasset: 2 killed

Date & Time: Jun 10, 1996 at 0600 LT
Type of aircraft:
Registration:
N916PA
Flight Phase:
Survivors:
No
Schedule:
Wiscasset - Philadelphia
MSN:
LW-313
YOM:
1979
Location:
Crew on board:
2
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
2
Captain / Total flying hours:
10516
Captain / Total hours on type:
1138.00
Aircraft flight hours:
6230
Circumstances:
The pilot took off on runway 07 and was cleared direct to the Wiscasset NDB, east of the airport. Shortly after takeoff, the airplane began turning to the left. The pilot then asked the controller, '. . . can you tell if I'm in a turn? I have a problem here.' Soon thereafter, the airplane collided with terrain in an uncontrolled descent, about 1.6 miles north of the airport. Investigation revealed that three days before the accident, a refueler had fueled the airplane's left wing with 840 pounds of fuel, then the fuel farm ran out of fuel. No further fueling was accomplished, and the pilot was not advised of the uneven fuel load. Procedures in the Beech E90 Pilot's Operating Manual (POM) included a check of the fuel tanks during preflight. The Beech C90 POM specified a maximum fuel imbalance of 200 pounds, but the E90 POM did not specify a maximum fuel imbalance. During examination of the wreckage, no preimpact malfunction or failure was found.
Probable cause:
Failure of the pilot to maintain control of the airplane while climbing after takeoff, due to spatial disorientation, which resulted in an uncontrolled descent and subsequent collision with terrain. Factors relating to the accident were: the improper refueling (servicing of the aircraft) by FBO personnel, and failure of the pilot to note the excessive lateral imbalance of the airplane during preflight.
Final Report:

Crash of a Socata TBM-700 in Kushiro: 6 killed

Date & Time: Apr 26, 1996 at 1108 LT
Type of aircraft:
Operator:
Registration:
JA8896
Survivors:
No
Schedule:
Sapporo - Kushiro
MSN:
68
YOM:
1993
Country:
Region:
Crew on board:
1
Crew fatalities:
Pax on board:
5
Pax fatalities:
Other fatalities:
Total fatalities:
6
Circumstances:
The pilot encountered poor visibility on approach to Kushiro Airport due to foggy conditions. Too low on final, the single engine aircraft collided with elements of the ILS systems and crashed 200 metres short of runway 17, bursting into flames. The aircraft was destroyed by a post crash fire and all six occupants were killed.

Crash of a Dassault Falcon 10 in Detroit

Date & Time: Jan 24, 1996 at 1018 LT
Type of aircraft:
Operator:
Registration:
N191MC
Survivors:
Yes
Schedule:
Philadelphia - Flint
MSN:
30
YOM:
1974
Crew on board:
2
Crew fatalities:
Pax on board:
6
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
11163
Captain / Total hours on type:
1330.00
Aircraft flight hours:
9829
Circumstances:
The pilot reported getting an unsafe indication on the right main landing gear when the landing gear was lowered. The crew recycled the landing gear and got the same unsafe indication. The crew retracted the gear and diverted to Detroit. On arrival, the crew performed the 'landing gear abnormal extension checklist,' but the unsafe indication remained. The air traffic control tower reported that the gear appeared normal. During the landing, the right main landing gear retracted. The airplane slid sideways, striking a runway marker as it departed the runway, and came to rest in a field. Examination revealed that the right landing gear downlock mechanism could be overcome with physical force. Examination of the right landing gear actuator revealed that one of the six shims which separate the spacers and help guide the safety lock switch was out of position and lying on top of the lock assembly.
Probable cause:
Failure of the right landing gear locking mechanism.
Final Report:

Crash of a Piper PA-46-350P Malibu in Carlyle: 1 killed

Date & Time: Jan 22, 1996 at 1614 LT
Registration:
N800CE
Flight Phase:
Survivors:
No
Schedule:
Des Moines – Nashville
MSN:
46-22171
YOM:
1994
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
1
Captain / Total flying hours:
3858
Captain / Total hours on type:
2626.00
Aircraft flight hours:
202
Circumstances:
During flight, the airplane was cruising at flight level 210 in IFR conditions with turbulence and with the wind from about 255 degrees at 70 knots. The airplane drifted off course at about 1600 cst. At 1610:09, after about ten minutes of unrecognized heading changes, the pilot stated '. . . I've lost my gyro.' At 1610:15, the controller issued a no-gyro vector. At 1611:29, as the airplane was still turning (to a heading that would intercept the original course), the pilot stated 'we've lost aLL our instruments . . . please direct me towards VFR.' He was cleared to descend to 14,000 feet. At about that same time, he stated 'we're in trouble' and 'we've lost all vacuum,' then there was no further radio transmission from the airplane. The airplane entered a steep, downward spiraling, right turn. The left outer wing panel separated up and aft (in flight) from overload and impacted the left stabilizer. The airplane crashed, and parts that separated from the airplane were found over a four mile area. Investigation revealed evidence that the HSI heading card can fail without the HDG flag appearing. Although the pilot had reported the loss of instruments and vacuum, examination of the airplane revealed that the engine, flight controls, electrical system, pitot/static system and vacuum systems exhibited continuity. No malfunction was found that would have led to loss of pressurization or hypoxia.
Probable cause:
Spatial disorientation of the pilot, and his failure to maintain control of the airplane, which resulted in his exceeding the design stress limits of the airframe. A factor relating to the accident was: turbulence in clouds.
Final Report:

Crash of a Mitsubishi MU-2B-60 Marquise in Allentown

Date & Time: Jan 19, 1996 at 1930 LT
Type of aircraft:
Registration:
N888TP
Survivors:
Yes
Schedule:
Wilkes Barre - Allentown
MSN:
1541
YOM:
1982
Crew on board:
1
Crew fatalities:
Pax on board:
2
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
2265
Captain / Total hours on type:
350.00
Aircraft flight hours:
2788
Circumstances:
The flight was on the ILS approach to runway 6, broke out of the clouds at 500 feet, and then re-entered the clouds. The airplane had not yet touched down when it drifted to right of the runway centerline and struck a snow bank located in the grass to the right of the runway, between the runway and the taxiway. The pilot stated he was just starting the missed approach when the accident occurred, and '...that there was no indication of a malfunction of the aircraft.' The reported ceiling was, 100 sky obscured, and the visibility was 1/4 mile, wind 040 degrees, 6 knots.
Probable cause:
The pilot's failure to comply with IFR procedures in that he attempted an instrument approach with visibility below the required minimums, and his delayed execution of a missed approach. A factor was the reduced visibility due to clouds.
Final Report:

Crash of a Piper PA-46-350P Malibu in Peachtree City: 2 killed

Date & Time: Jan 16, 1996 at 0900 LT
Registration:
N9210F
Survivors:
No
Schedule:
Lakeland – Peachtree City
MSN:
46-22119
YOM:
1991
Crew on board:
2
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
2
Captain / Total flying hours:
1080
Captain / Total hours on type:
92.00
Aircraft flight hours:
1064
Circumstances:
During the preflight briefing, the pilot was informed of reduced visibility and low ceiling in the vicinity of the destination airport, at the approximate time of the planned arrival. Upon arriving in the Atlanta area, the pilot was issued radar vectors to a final for the localizer runway 31 approach. The pilot was also given the current Atlanta altimeter setting, and was cleared for the localizer runway 31 approach. The airplane collided with a 60-foot tall light pole at a nearby baseball complex 2 miles short of the runway. The weather observation from the Hartsfield International Airport indicated that visual weather conditions prevailed at the time of the accident. However, according to a witness at the accident site, the weather conditions were foggy with reduced visibility. The wreckage distribution path was 2,467 feet right of the localizer course. The minimum descent altitude for this approach, using Atlanta's altimeter setting, was 1260 feet. The ground check of the localizer and DME facility was within normal operating range. Examination of the aircraft navigational radios also tested within normal ranges. The average field elevation in the vicinity of the accident site is 800 feet. The pilot's toxicological examinations detected pseudoephedrine (decongestant), phenylpropanolamine (decongestant), and chlorpheniramine (antihistamine). No samples were available to quantify the blood levels of these medications.
Probable cause:
The pilot's failure to follow the published instrument approach procedure. The fog was a factor.
Final Report: